ML17340A306

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Application to Amend License DPR-31,permitting Return to Power Operation.Results of Steam Generator Insps Conducted During Oct 1980 Power Outage Forwarded.Class III Fee Encl
ML17340A306
Person / Time
Site: Turkey Point 
Issue date: 10/22/1980
From: Robert E. Uhrig
FLORIDA POWER & LIGHT CO.
To: Eisenhut D
Office of Nuclear Reactor Regulation
Shared Package
ML17340A307 List:
References
L-80-349, NUDOCS 8010280297
Download: ML17340A306 (6)


Text

REi'UL<

RY INFORMATION DISTRIBUTI'YSTEM (RIDS)

ACCESSION NBRe80102802V7 DOC,DATE: 80/10/22 Nb.~ ARIZED:

NO DOCKET FACIL:50-2+0 Turkev Point P lent A Unit 5r F1 ori de Power end L40ht 0

05000250 AUTH~ NAME 'UTHOR AFFILIATION UHRIG R.E.

F.lorida Power 8 Light Co ~

REGIS,NAME RECIPIENT AFFILIAT'ION EISENHUTFD,G, D.ivision of Licens ng

SUBJECT:

Application to amend License DPR-31Fpermittlng return to, power operation. Results of steam generator insps conducted during Oct 1980 power outage forwarded, Class III fee encl.

DISTRIBUTION CODE:

A001S COPIES RECEIVED:LTR 3.

ENCL 5 SIZE:~$39 TITLE: General.Distribution for after Issuance of Operating License---

NOTES:

RECIPIENT ID CODE/NAblE ACTION VARGAg S ~

04 INTERNAL: D/DIRFHUM FAC08 NRC PDR 02 OR ASSESS BR 10 EXTERNAL: ACRS 09 NSIC 05 COPIES L'ffTR ENCL 13 13 1

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1 1

0 16 16 1

1 RECIPIENT ID CODE/NAME IE,E REG FILE LPDR 06 11 01 03 COPIES LTTR ENCL 2

2 0

1 1

1 1

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~4'r ~ 8 1gao TOTAL NUMBER OF COPIES REQUIRED:

LTTR 38 ENCL

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FLORIDA POWER 8L LIGHTCOMPANY October 22, 1980 L-80-349 Office of Nuclear Reactor Regulation Attention:

Mr. Darrell G. Eisenhut, Director Division of Licensing U.

S.

Nuclear Regulatory Commission Washington, D.C.

20555

Dear Mr. Eisenhut:

Re:

Turkey Point Unit 3 Docket No. 50-250 Steam Generator Inspections The results of the Turkey Point Unit 3 steam generator inspections conducted during the current outage are attached.

The inspections which were performed in accordance with Turkey Point Unit 3 operating license DPR-31 showed no new phenomena and verified that the general pattern of denting in Unit 3 is within predictable limits and consistent with previous inspections of the Turkey Point Units.

The general criteria applied for steam generator inspections and preventive plugging are the same as previously applied to Turkey Point Units 3 and 4 to provide in excess of six months of operation.

This approach provides reasonable assurance of steam generator tube integrity such that safe operation of the unit during normal full power operation and during hypothetical accident conditions is assured for an operati ng period in excess of six effective full power months.

Therefore, the implementation of this program with the resulting preventive plugging, enables continued safe full power operation of Turkey Point Unit 3 for a period in excess of six months.

Total steam generator tube plugging at the conclusion of the current outage will be approximately 20-4X.

This is conservatively bounded by the 25K tube plugging ECCS analysis.

The results of this inspection and the preventive tube plugging program have been reviewed by the Turkey Point 'Plant Nuclear Safety Committee and the Florida Power 8 Light Company Nuclear Review Board.

They have concluded that based on the inspection results, the implemented plugging pattern, and previously submitted analyses, that the return of Turkey Point Unit 3 to full DDI power operation for at least six effective months does not involve an unreviewed safety question.

In accordance with condition E.5 of operating license DPR-31, Florida Power 8

Light Company requests permission to return Unit 3 to power operation.

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'Darrell G. Eisenh Office of 'Nuclear Reactor Regulation Page 2

Based on our current schedule, we could be ready to resume power operation by October 27, 1980.

We will keep you advised of any significant changes.

We have determined that this is a Class III request in accordance with 10 CFR 170.

Accordingly, a check for $4',000 is enclosed.

Very truly yours, Robert E. Uhrig Vice President Advanced Systems 8 Technology REU/RJA/pah Attachment cc:

J.

P. O'Reilly,,Region:II Harold F. Reis, Esquire

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