ML17335A391

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Forwards Insp Rept 50-315/98-25 on 981112-19.No Violations Noted.Insp Re Establishment of Restart Metric Indicators to Gage Plant Readiness for Restart & to Evaluate Progress in Engineering Resolution of Ice Condenser Issues
ML17335A391
Person / Time
Site: Cook 
Issue date: 12/09/1998
From: Grobe J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Powers R
AMERICAN ELECTRIC POWER CO., INC.
Shared Package
ML17335A392 List:
References
50-315-98-25, NUDOCS 9812160089
Download: ML17335A391 (8)


See also: IR 05000315/1998025

Text

CATEGORY 2

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

CCESSION NBR:9812160089

DOC.DATE: 98/12/09

NOTARIZED: NO

DOCKET

FACIL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana

M

05000315

AUTH.NAME

AUTHOR AFFILIATION

GROBE,J.A.

Region

3

(Post

820201)

RECIP . NAME

RECIPIENT AFFILIATION

POWERS,R.P.

American Electric Power Co., Inc.

SUBJECT:

Forwards insp rept 50-315/98-02

on 981112-19.No violations

noted.

RECIPIENT

ID CODE/NAME

PD3-3

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SIZE:

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(50 Dkt)-Insp Rept/Notice

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'OTE TO ALL "RZDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DZSTRZBUTION LISTS

OR REDUCE THE NUMBER OF COPIES

RECEZVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL

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TOTAL NUMBER OF COPIES

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December 9,

1998

Mr. R. P. Powers

Senior Vice President

Nuclear Generation Group

American Electric Power Company

500 Circle Drive

Buchanan, Ml 49107-1395

'UB

JECT:

NRC INSPECTION REPORT NO. 50-315/98025(DRS)

Dear Mr. Powers:

On November 19, 1998, the NRC completed a special inspection at your D. C. Cook, Unit 1

reactor facility. The inspection was an examination of'activities conducted under your license as

they relate to your establishment of restart metric indicators to gage plant readiness for restart

and to evaluate the progress in engineering resolution of ice condenser issues.

Because the

restart metrics factor into your assessment

of plant readiness for restart, the NRC Manual

Chapter 0350 Restart Panel willcontinue to monitor your progress in meeting established

performance goals for these metrics. The enclosed report documents the results of the

inspection.

4

'he 22 restart metric indicators developed, demonstrated

substantive progress toward

achieving a data collection system to provide semiguantitative measurement tools for assessing

plant process and programmatic readiness for restart.

The metric performance indicators with

more potential value measured process product quality, such as 50.59 Quality, Calculation

Quality and Root Cause Quality, or effectiveness, such as Corrective Actions Effectiveness.

A recent Performance Assurance department assessment

identified weaknesses

in the grading

process used for safety evaluations, which indicated that more work is needed to effectively

implement the restart metric indicator of 50.59 Quality. Additionally, the corrective action for this

finding, to mentor engineering department personnel, may artificiallyinfluence the safety

evaluation quality measurement for engineering.

Progress was observed in engineering resolution of issues pertaining to the ice condenser with

the establishment of ice basket damage criteria and a systematic approach to incorporation of

ice condenser information into the Updated Final Safety Analysis Report.

However, resolution

of previous NRC ice condenser findings had not progressed to a point that supported a final

NRC review.

In accordance with 10 CFR 2.790 of the NRC'S "Rules of Practice," a copy of this letter, the

enclosures,

and your response to this letter, ifyou choose to provide one, willbe placed in the

NRC Public Document Room (PDR).

98i2fh0089

98%209'DR

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UNITED STATES

NUCLEAR REGULATORYCOMMISSION

REGION III

801 WARRENVILLEROAD

USLE, ILUNOIS60532-4351

December 9, 1998

Mr. R. P. Powers

Senior Vice President

Nuclear Generation Group

American Electric Power Company

500 Circle Drive

Buchanan, MI 49107-1395

SUBJECT:

NRC INSPECTION REPORT NO. 50-315/98025(DRS)

Dear Mr. Powers:

On November 19, 1998, the NRC completed a special inspection at your D. C. Cook, Unit 1

'eactor facility. The inspection was an examination of activities conducted under your license as

they relate to your establishment of restart metric indicators to gage plant readiness for'restart

and to evaluate the progress in engineering resolution of ice condenser issues.

Because the

restart metrics factor into your assessment

of plant readiness for restart, the NRC Manual

Chapter 0350 Restart Panel willcontinue to monitor your progress in meeting established

performance goals for these metrics. The enclosed report documents the results of the

'nspection.

The 22 restart metric indicators developed, demonstrated

substantive progress toward

achieving a data collection system to provide semi-quantitative measurement tools for assessing

plant process and programmatic readiness for restart.

The metric performance indicators with

more potential value measured process product quality, such as 50.59 Quality, Calculation

Quality and Root Cause Quality, or effectiveness, such as Corrective Actions Effectiveness.

A recent Performance Assurance department assessment

identified weaknesses

in the grading

process used for safety evaluations, which indicated that more work is needed to effectively

implement the restart metric indicator of 50.59 Quality. Additionally, the corrective action for this

finding, to mentor engineering department personnel, may artificiallyinfluence the safety

evaluation quality measurement for engineering.

Progress was observed in engineering resolution of issues pertaining to the ice condenser with

the establishment of ice basket damage criteria and a systematic approach to incorporation of

ice condenser information into the Updated Final Safety Analysis Report.

However, resolution

of previous NRC ice condenser findings had not progressed to a point that supported a'final

NRC review.

In accordance with 10 CFR 2.790 of the NRC'S "Rules of Practice," a copy of this letter, the

enclosures, and your response to this letter, ifyou choose to provide one, willbe placed in the

NRC Public Document Room (PDR).

I.

il',

. R. Powers

We willgladly discuss any questions you have concerning this inspection.

Sincerely,

Original /s/ John A. Grobe

John A. Grobe, Director

Division of Reactor Safety

Docket No.: 50-315

License No.: DPR-58

Enclosure:

Inspection Report 50-315/98025(DRS)

cc w/encl:

J. Sampson, Site Vice President

R. Eckstein, Chief Nuclear Engineer

D. Cooper, Plant Manager

R. Whale, Michigan Public Service Commission

Michigan Department of Environmental Quality

Emergency Management

Division

Ml Department of State Police

D. Lochbaum, Union of Concerned Scientists

Distribution:

RRB1 (E-Mail)

RPC (E-Mail)

Project Mgr., NRR w/encl

J. Caldwell, Rillw/encl

C. Pederson, Rill w/encl

B. Clayton, Rillw/encl

SRI DC Cook w/encl

DRP w/encl

TSS w/encl

DRS (2) w/encl

Rill PRR w/encl

Q~P.UBL'IC'IE-'01'/enyct,'.;~~

Docket File w/encl

GREENS

IEO (E-Mail)

DOCDESK (E-Mail)

DOCUMENT NAME: G:DRS(DCC98025.wpd

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