ML17333B032
| ML17333B032 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 09/05/1997 |
| From: | Fitzpatrick E INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| AEP:NRC:1202E, NUDOCS 9709160220 | |
| Download: ML17333B032 (4) | |
Text
CATEGORY 1 REGULA~ INFORMATION DZSTRIBUTZO1lSTEM (RIDE)
ACCESSION NBR:9709160220 DOC.DATE: 97/09/05 NOTARIZED: NO FACIL:50-315 Donald C.
Cook Nuclear Power Plant, Unit 1, Indiana M
50-316 Donald C.
Cook Nuclear Power Plant, Unit 2, Indiana M
AUTH'.NAME AUTHOR AFFILIATION FITZPATRICK,E.E American Electric Power Co., Inc.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
DOCKET 05000315 05000316
SUBJECT:
Informs of discovery of inconsistency between input component cooling water (CCW) temp a procedurally allowed max CCW temp in spent fuel pool analyses.Holtec will perform rev to util spent fuel pool analyses.
DISTRIBUTION CODE:
A001D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: OR Submittal: General Distribution NOTES:
E RECIPIENT ID CODE/NAME PD3-3 LA HICKMANFJ INTERNA : FILE CENTE 1
'D 'B NRR/DSSA/SPLB NUDOCS-ABSTRACT EXTERNAL: NOAC COPIES LTTR ENCL RECIPIENT ID CODE/NAME PD3-3 PD NRR/DE/ECGB/A NRR/DRCH/HICB NRR/DSSA/SRXB OGC/HDS2 NRC PDR COPIES LTTR ENCL D
E N
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)
ON EXTENSION 415-2083 C)
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 13 ENCL
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indiana Michigan Power Company 500 Circle Drive Buchanan, Ml 491071395 lNQlANA SllCNIGAN PWKR September 5,
1997 AEP: NRC: 1202E Docket Nos.:
50-315 50-316 U. S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, D.
C.
20555 Gentlemen:
Donald C.
Cook Nuclear Plant Units 1 and 2
SPENT FUEL POOL ANALYSIS NOTIFICATION An inconsistency between the input component cooling water (CCW) temperature and the procedurally allowed maximum CCW temperature was discovered in the spent fuel pool analyses of record duxing the course of answering questions from the NRC architect engineer design inspection team.
At our request, Holtec is performing a revision to our spent fuel pool analyses.
Because the CCW temperature inconsistency is less than 4', it is expected that the revised analyses will yield similar results to those previously submitted.
The results will be transmitted to the NRC as an addendum to our request to change the refueling operations decay time technical specification, AEP:NRC:1202 submittal, dated November 16, 1994.
Approval of AEP:NRC:1202 is required to support oux'nit 2
5% thermal power. uprate
- request, submittal AEP:NRC:1223, dated July 11, 1996.
Sincerely,
'E.
E. Fitzpatrick Vice President E
vlb A. A. Blind A. B. Beach MDEQ -
DW & RPD NRC Resident Inspector J.
R. Padgett P g tM l
'P709i60220 970905 PDR ADQCK 050003i5 P
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