ML17328A538
| ML17328A538 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 01/05/1990 |
| From: | Alexich M INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | Davis A NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| AEP:NRC:1090L, NUDOCS 9001120267 | |
| Download: ML17328A538 (6) | |
Text
ACCELERATED DISTRIBUTION DEMONSTPATION SYSTEM
/
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9001120267 DOC.DATE: 90/01/05 NOTARIZED: NO DOCKET FACIL:50-315 Donald C.
Cook Nuclear Power Plant, Unit 1, Indiana 05000315 AUTH.NAME AUTHOR AFFILIATION ALEXICH,M.P.
(formerly Indiana' Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Responds to NRC 891206 ltr re violations noted in Insp Rept 50-315/89-29.
DISTRIBUTION CODE:
IE01D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:
RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD AEOD/TPAD NRR SHANKMAN,S NRR/DOEA DIR 11 NRR/DREP/PRPB11 NRR/DST/DIR 8E2 NUDOCS-ABSTRACT OGC/HDS1 RES MORISSEAU,D EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1
1 1
1 1
1 1
1 1
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RECIPIENT ID CODE/NAME GIITTER,J.
AEOD/DEIIB DEDRO NRR/DLPQ/LPEB10 NRR/DREP/PEPB9D NRR/DRIS/DIR NRR/PMAS/ILRB12 O~IEBERMAN,J
~WW~F N 02 RGN3 FILE 01 NRC PDR COPIES LTTR ENCL 1
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NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WARM CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 20079) TO ELIMINATEYOUR NAMEFROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 24 ENCL 24
Indiana Michigan Power Company P.O. Box 16631 Coiurnbus. OH 43216 Z
INDIANA AIICHIGAN PQWER AEP:NRC:1090L Donald C.
Cook Nuclear Plant Unit 1 Docket No. 50-315 License. No.
DPR-58 NRC INSPECTION REPORT NO. 50-315/89029 (DPR)
U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.
20555 Attn: Mr. A. B. Davis January 5,
1990
Dear Mr. Davis:
This letter is in response to Mr.
W. L. Axelson's letter dated December 6,
- 1989, which forwarded the report on the routine safety inspection conducted by the resident inspectors.
This inspection was conducted October 4 through November 16,
- 1989, on activities at the Cook Nuclear Plant Units 1 and 2.
The Notice of Violation attached to Mr. Axelson's letter identified'one Severity Level IV violation.
The violation is addressed in the attachment to this letter.
This document has been prepared following Corporate procedures which incorporate a reasonable set of. controls to ensure its accuracy and completeness prior to signature by the undersigned.
Sincerely, M..P. Ale ich Vice President ldp cc:
D. H. Williams, Jr.
A. A. Blind - Bridgman R.
C. Callen G. Charnoff NRC Resident Inspector
- Bridgman NFEM Section Chief
'igloo.-::i
'00105 pgp
+DOCK 0
ATTACHMENT TO AEP:NRC'109OL
RESPONSE
TO NRC NOTICE OF VIOLATION
VIOLATION "Unit 1 Technical Specification Limiting Condition for Operation 3.5.2 requires two independent ECCS subsystems shall be OPERABLE. in MODES 1, 2 and 3, with ACTION stipulations limited to the case of one ECCS subsystem inoperable.
Unit 1 Technical Specification 3.0.3 requires, when a Limiting Condition for Operation is not met (e.g., neither ECCS subsystem OPERABLE) except as provided in associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which the specification does not apply.
Contrary to the above,-on September 13, 1989, Unit 1 was in MODE 1 for one hour and eight minutes with neither independent ECCS subsystem OPERABLE.
One subsystem (Train A) was inoperable due to ongoing maintenance on safety injection pump 1'N, while the other (Train B) was inoperable due to testing conditions which defeated, the Train automatic actuation logic.
Action was not initiated within one hour to place the unit in a MODE in which the Specification did not apply.
This is a Severity Level IV violation (Supplement 1)."
RESPONSE
TO VIOLATION On September 13, 1989, it was identified that the Unit 1 Train B safety injection (SI) pump had been made inoperable by solid state protection system (SSPS) surveillance testing, while the Train A SI pump was isolated for valve leak repairs.
This event occurred because the testing and maintenance was scheduled for the same
- day, the surveillance procedure did not contain guidance to ensure that opposite train equipment is operable, and the Shift Supervisor and Unit Supervisor'ailed to recognize that the Train B.SI pump would be made inoperable by the SSPS testing.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED The involved Unit 1 surveillance procedures (1-THP 4030.STP.410 and 1-THP 4030.STP.411) were revised on September 21, 1989, to add a requirement for the Shift Supervisor to ensure that the opposite train equipment is operable.
The Unit 2 procedures did not require revision because they had been previously revised to include the requirement.
- Also, a memorandum was issued to Operations Department personnel as a reminder of the requirement for maintaining opposite train equipment operable during SSPS testing on the other train.
CORRECTIVE ACTION TO BE TAKEN TO AVOID FURTHER VIOLATION Prior to this event, the instrumentation surveillance schedules were not used as an integral part of the routine daily work coordination process.
In response to this event, the job planners have been given direction to consider the surveillance schedules as an integral part of the routine work coordination process.
Additional reviews of the work planning process have been conducted and further actions are being planned to improve the planning and scheduling process.
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An'dministrative control (PMSO 113) was placed in effect on November 22, 1989, that requires personnel to review surveillance test procedures prior to their use on operable equipment'during unit operation to ensure that the procedure specifies what equipment will be made inoperable by the'est.
This review involves a significant effort consisting of a thorough review by the group responsible for the procedure, which is followed by reviews from two licensed Senior Reactor Operators.
The majority of applicable procedures used on a routine basis have been reviewed and have been revised as needed.
The remaining applicable procedures will be reviewed, as required by PMSO 113, prior to their use.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance was achieved on September 13,
- 1989, when the Train B SSPS testing was completed, which restored on Train B SI pump automatic start capability.