ML17324A711

From kanterella
Jump to navigation Jump to search
Insp Repts 50-315/86-06 & 50-316/86-06 on 860203-26.No Violation or Deviation Noted.Major Areas Inspected:Actions on Previous Findings & LER on 860203 Re Estimated Critical Condition Calculation for Unit 2 Startup
ML17324A711
Person / Time
Site: Cook  
Issue date: 03/11/1986
From: Mccormickbarge, Ring M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17324A710 List:
References
50-315-86-06, 50-315-86-6, 50-316-86-06, 50-316-86-6, NUDOCS 8603170368
Download: ML17324A711 (11)


See also: IR 05000315/1986006

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION III

Reports

No. 50-315/86006(DRS);

50-316/86006(DRS),

Docket Nos.

50-315;

50-316

Licenses

No.

DPR-58;

DPR-74

Licensee:

American Electric Power Service Corporation

Indiana

and Michigan Power

Company

1 Riverside Plaza

Columbus,

OH

43216

Faci l ity Name:

D.

C.

Cook Nucl ear Pl ant,

Units 1 and

2

Inspection At:

D.

C.

Cook Site,

Bridgman,

MI

Inspection

Conducted:

February 3,

1986 through February 26,

1986

Inspector:

M.

L. McCormick-Barger

5-6-sk

Date

Approved By:

M. A. Ring, Chief

Test Programs

Section

'5-<l<<t4

Date

Ins ection

Summar

Ins ection

on Februar

3

1986 throu

h Februar

26

1986

Re orts

No.

50-315/86006(DRS

. 50-316 86006(DRS

previous inspection findings, licensee

event reports

estimated critical

condition calculation for a Unit 2 startup

on February 3, 1986, core thermal

power, Unit 1 Cycle 9 rod worth measurements,

Unit 1 Cycle

9 moderator

temperature coefficient measurement,

and core power distribution limits.

The

inspection involved 54 inspector-hours

onsite

and two inspector-hours offsite by

one

NRC inspector.

Results:

No violations or deviations

were identified.

Bb03i703b8

Bb0311

PDR

ADDCN, 050003l6

8

PDR,

,DETAILS

1.

Persons

Contacted

A. Blind, Assistant, Plant Manager

R. Baker, Operations

Superintendent

S.

Gibson, Technical-Engineering

Department

Head

W. Hennen,

Nuclear Engineering Supervisor

Verteramo,

Nuclear Performance

Engineer

F. Stietzel, guality Control Superintendent

J.

Nadeau,

AEPSC guality Assurance

"Denotes

those attending the exit interview on February 26, 1986.

2.

Licensee Action on Previous

Ins ection Findin

s

a 0

b.

C.

(Closed)

Unresolved

Item (316/84-16-01):

Appendix A-205 of

Procedure

2 THP 4030.

STP.330,

Revision 5, "Surveillance of Core

Distribution Limits," contained incorrect Technical Specification

acceptance

criteria.

During this inspection,

the inspector

reviewed

Procedure

2 THP 4030.

STP.330,

Revision 7,

and the corresponding

procedure for Unit 1 (1THP 4030.

STP.330,

Revision 9) and found that

the Technical Specification limits, contained in Appendix A, for each

of these

procedures

agreed with the Unit 2 and Unit 1 Technical

Specifications,

respectively.

The inspector

had

no further concerns.

(Closed)

Unresolved

Item (316/84-16-02):

The procedure results for

Procedure

12

THP 6040. PER. 350, Revision 0, "Isothermal

Temperature

Coefficient Measurement

and Moderator Temperature Coefficient

Calculation," performed for the Unit 2 Cycle

5 startup

lacked

documentation

related to some unanticipated

slope

changes

in the

reactivity versus

temperature plots.

During this inspection,

the

inspector

reviewed the licensee's

actions which included

documentation

of the licensee's

evaluation pertaining to the

unanticipated

slope

changes

and

a revision to Procedure

12 THP

6040. PER. 350.

A note following Step

8. 6. 1 of Revision

1 of this

procedure

discusses

deviations

from a straight line for an

isothermal

temperature coefficient measurement

plot.

Based

on the

way this note was written, the inspector

was concerned it might be

misinterpreted to mean that,

should unusual plots occur in the

future,

no pursuit of the cause

would be necessary.

The licensee

made

a commitment to clarify the procedure prior to the Unit 2

Cycle

6 startup to ensure that an evaluation would be performed if

slope irregularities occurred in future tests.

This is considered

an open item (315/86006-Ol(DRS);

316/86006-01(DRS))

pending

procedure revision and subsequent

NRC review.

(Closed) Unresolved

Item (316/84-16-03):

During the performance of

Procedure

12 THP 4030.STP.307,

"Moderator Temperature Coefficient

Determination," for the Unit 2 Cycle

5 startup,

Step 8.2 and the

associated

data sheets

were

mar ked "N/A" not applicable with no

justification given.

The use of "N/A" was not permitted without a

change

sheet at the time this step

was marked "N/A."

However,

based

on the inspector's

review of the corrective action which included

documentation of the justification for the "N/A," the justification

was reasonable

and'here

was

no safety significance to skipping this

step

and the associated

data sheets.

In addition, generic

corrective actions

were taken.

Several

Plant Manager Instructions

(PMIs) were revised to address

the use of "N/A" during performance

of procedures

including PMI-2010, "Plant Manager

and Department

Head

Instructions,

Procedures,

and Associated

Indexes,"

and PMI-6040,

"Performance/Engineering

Test Procedures."

Step 3.1. 2 of PMI-2010

stated,

in part, that "It is expected that as procedures

are

revised,

instructions for partial completion will be addressed

on a

case

by case basis."

The inspector discussed

this with the Nuclear

Engineering Supervisor

who indicated that the procedures

used

by the

Nuclear Group had been

reviewed and,

where appropriate,

revised to

identify procedure

steps that are optional

under certain conditions

and can, therefore,

be marked "N/A."

The inspector

reviewed

numerous

examples of procedures

used by the Nuclear Group which had

been revised to address

the use of "N/A."

There

was

a statement

that appeared

in several

Nuclear Group procedures

(for example:

"~THP 6040.PER.356,

"Reactivity Computer Checkout" ) that concerned

the inspector

because it might be misinterpreted

as giving unlimited

authority to Test Engineers

as

opposed to controlling the use of

"N/A" through procedural

allowances

as described

in PMI 2010.

The

statement

was:

"Only those sections

deemed appropriate

by the test

engineer

need

be completed for each specific test."

The licensee

committed to look into clarification of that statement.

This is

considered

an open item (315/86006-02(DRS);

316/86006-02(DRS))

pending licensee action and subsequent

NRC review.

No violations or deviations

were identified, however,

two areas

require further review and will be followed as

open items.

3.

Licensee

Event

Re orts

Through discussions

with licensee

personnel

and review of records,

the

following Licensee

Event Report

(LER) was reviewed to determine that

reportability requirements

were met,

and corrective

and preventive

actions

were accomplished

in accordance

with Technical Specifications.

The following LER is considered

closed:

LER 315/84009:

A flux map taken at 99K power on March 21,

1984,

indicated that the heat flux hot channel factor (F~) approximately

0.4X.

Power level

was subsequently

reduced to 96K power.

Reanalysis

demonstrated

that this was

an indicated rather

than

actual violation based

on conservatisms

incorporated in the original

flux map analysis.

The reanalysis

indicated that it would be

permissible to return to 99.7X power.

Further reanalysis utilizing

a burnup dependent

V(z) indicated that it would be possible to

return to 103X power without violating the

F~ Technical

1

Specification limit.

Power was then returned to lOOX power.

Since the Technical Specification limit was not actually violated,

this

LER was submitted

as

a Voluntary LER.

The inspector

reviewed the following records:

Unit 1 Cycle 8 Flux Map 108-35,

March 21, 1984, Option No. 6, Job

No.

1084,

2-D Analytical Factors (with 3X penalty applied to

F ).

Unit 1 Cycle 8 Flux Map 108-35,

March 21, 1984, Option No. 6, Job

No. 979,

3-D Analytical Factors,

V(z) was not core burnup dependent.

Unit 1 Cycle 8 Flux Map 108-35,

March 21, 1984, Option No. 6, Job

No. 1601,

2-D Analytical Factors

(with 1X penalty applied to

F ),

core burnup dependent

V(z) factor, Control

Bank

D at 216 steps.

Unit 1 Cycle 8 Flux Map 108-36,

March 27, .1984, Option No. 3, Job

No. 2546,

3-D Analytical Factors,

Control

Bank

D at 220 steps.

Unit 1 Control

Room Log Book 24, March 21 through 25, 1984.

The inspector

had

no concerns

based

on the review.

No violations or deviations

were identified.

4.

Estimated Critical Condition Calculation for a Unit 2 Startu

on

Februar

3

1986

During a Unit 2 reactor startup

on February 3, 1986, the reactor failed

to achieve criticality within the limits predicted

by the estimated

critical condition calculation.

The inspector discussed this with licensee

personnel

and reviewed the following records:

Condition Report 2-02-86-132, "Failure to Achieve Criticality on

Unit 2 Reactor

as Predicted

by the Estimated Critical Condition

Calculation," initiated on February 3, 1986.

Procedure

2-OHP 4021.001.011,

Revision 2, (with Change

Sheet

No.

1

attached),

!'Determination of Critical Conditions."

Procedure

2-OHP 4021.001.002,

Revision 7, "Reactor Start-up."

Data/Signoff Sheets for Procedure

2-OHP 402.001.011,

"Determination of

Critical Conditions," performed

on August 16,

1985, October 31, 1985,

February 1, 1986 and February 3,

1986 (recalculation following the

Unit 2, February 3, 1986, startup termination).

Individual Training Records for the nuclear performance

engineer

who

preformed the estimated critical conditions calculation

on February 1,

1986.

Unit 2 Control

Room Log Book for February 3, 1986.

t

M

V

A 1/m plot is performed for every Unit 2 startup in accordance

with

Procedure

2

OHP 4021.001.002,

"Reactor Startup,"

and,

using this plot, the

reactor operators

determined that criticality would not occur within the

limits of the Estimated Critical Condition (ECC) calculation.

The reactor

startup

was terminated at 6: 51 a.m.,

and all control

banks were fully

inserted

by 7:05 a.m..

The licensee's

investigation

showed that a value was

used in the

ECC

calculation which was obtained,off of an inappropriate

curve from a Unit 2

Technical

Data Book figure.

(The figure contained

several

curves

and,

whereas

the

ECC calculation procedure

specified the figure number, it did

not specify which of the curves

should

be used).

Although the curve used

was not the one typically used, it was conservative

and, therefore,

was

accepted

by the two Senior Reactor Operators that signed off on the

calculation.

The inspector

reviewed the training records of the

individual that performed the

ECC calculation.

These

records

showed that

the individual had received training for the "Determination of Critical

Conditions" procedure.

In addition, the individual had performed

an

ECC

calculation

on two previous occasions

(August 16,

1985 and October 31,

1985)

and on both of these

occasions

the calculation

was performed

correctly and had been

checked

by another

member of the Nuclear Group.

After determining the cause of the error in the

ECC calculation,

the

licensee

recalculated

the estimated critical conditions

and, during the

reactor startup that followed, went critical within the limits of the

calculation.

The licensee's

actions to prevent future errors related to

the selection of an improper curve from a Technical

Data Book figure

included, revisions of Units 1's

and Unit 2's

ECC calculation procedures

to identify the specific curve that should

be used.

In addition, the

licensee

reviewed other operations

and nuclear performance

procedures

to

determine if similar revisions

were warranted in other procedures.

As a

result of this review, the licensee

intended to revise

one additional

procedure

(12 THP 4030.STP.308,

"Boron Curve Update" ).

Based

on the

licensee's

corrective actions

and the fact that this appeared

to be an

isolated occurrence,

the inspector

has

no further concerns.

No violations or deviations

were identified.

Core Thermal

Power

The inspector

reviewed licensee

procedures

and results to verify that the

calculation of core thermal

power was technically correct

and that

results indicated that reactor power was within prescribed limits.

The

inspector utilized the following documents

during the review:

Procedure

1 OHP 4030. STP. 029, Revision 8, "Reactor

Thermal

Power

Determination."

Procedure

2

OHP 4030.STP.029,

Revision 5, "Reactor Thermal

Power

Determination."

I

I4

lf

1[

e

Procedure

12 THP 4030.STP.219,

Revision 3, "Thermal

Power

Measurement

and Reactor

Coolant System

Flow Rate," performed for

Unit 1 Cycle 9, October 23,

1985 through January

18,

1986.

Data/Signoff Sheet

6. 1 for Procedure

1 OHP 4030.STP.029,

Revision 7,

"Reactor Thermal'ower Determination'

for the following dates:"

January l-ll, 1985

a'nd January

29 through, April 5,

1985.'ata/Signoff

Sheet 6.3 for Procedure

1 OHP 4030.STP.030,

Revision 11,

"Operations Shift Surveillance

Checks, (Modes 1, 2, 3, 4), for the

following dates:

February

15 through March 31, 1985.

Computer Printout - Daily Trend, Block Data for Unit 1, March 1985.

No violations or deviations

were identified.

6.

Unit 1

C cle

9 Rod Worth Measurements

The inspector

reviewed the Unit 1 Cycle

9 rod worth measurement

procedure

for technical

adequacy

and verified that the, results satisfied the

acceptance

criteria.

The following documents

were used in this review:

Procedure

1 THP SP. 101, Revision 0,

"Rod Worth Verification Tests

Utilizing RCC Bank Interchange,"

dated October 8,

1985 and performed

for Unit 1 Cycle

9 on November 15,

1985.

WCAP-10862,

"Core Physics Characteristics

of the Donald

C.

Cook

Station Nuclear Plant (Unit 1, Cycle 9)," August 1985.

No violations or deviations

were identified.

7.

Unit 1

C cle 9 Isothermal/Moderator

Tem erature Coefficient

The inspector

reviewed the Unit 1 Cycle

9 low power physics test

procedure

related to isothermal

and moderator temperature coefficient

measurement

for technical

adequacy

and verified that the results

satisfied the acceptance

criteria.

The following documents

were used in

this review:

12

THP 6040. PER.350,

Revision 1, "Isothermal

Temperature Coefficient

(ITC) Measurement

and Moderator Temperature Coefficient (MTC)

Calculation," dated April 15,

1985 and performed for Unit 1 Cycle 9

on November 14,

1985.

WCAP-10862,

"Core Physics Characteristics

of the Donald

C.

Cook

Station Nuclear Plant (Unit 1, Cycle 9)," August 1985.

Comments related to this review are contained in Par'agraph

2.b.

No violations or deviations

were identified.

1

'I

l

I

I

tf

V

'l

~

4

'

Core Power Distribution Limits

The review of licensee

procedures

and results related to core power

distribution limits for Unit 1 Cycle 8 and the startup of Cycle

9 began

during

NRC Inspection 315/85034;

316/85034 (refer to Paragraph

5 of

Inspection

Report

No. 315/85034;

316/85034 for details).

During this

inspection the inspector

reviewed

one additional

document related to core

power distribution limits:

Technical Specification Clarification No. 17, Technical

Specification

3. 2. 4, "Application of the quadrant

Power Tilt

Technical Specification,"

reviewed by the Plant Nuclear Safety

Review Committee

on January 8, 1980.

The Technical Specification Clarification identified above, will be

referred to NRC's Office of Nuclear Reactor Regulation

(NRR) for further

review and evaluation.

This will be followed as

an open item

(315/86006-03(DRS);

316/86006-03(DRS))

pending completion o'f NRR's review.

No violations or deviations

were identified, however,

one item requires

further review and will be followed an an open item.

9.

~0en Items

Open items are matters

which have

been discussed

with the licensee,

which

will be reviewed further by the inspector,

and which involve some action

on the part of the

NRC or licensee

or both.

Open items disclosed

during

the inspection are discussed

in Paragraphs

2.b, 2.c and 8.

10.

Exit Interview

The inspector

met with licensee

representatives

(denoted in Paragraph

1) on

February 26,

1986 to discuss

the scope

and findings of the inspection.

The

licensee

acknowledged

the statements

made

by the inspector with respect to

items discussed

in the report.

The inspector also discussed

the likely

informational content of the inspection report with regard to documents

or

processes

reviewed

by the inspector during the inspection.

The licensee

stated that portions of the rod bank interchange

procedure

(1 THP SP. 101)

and the core physics characteristics

report

(MCAP-10862) were considered

proprietary but that references

to them would not be.