ML17308A169

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Insp Rept 50-335/85-29 on 851104-08 & 12-15.Violation Noted: Inadequate Procedure for Removal of Upper Guide Structure
ML17308A169
Person / Time
Site: Saint Lucie 
Issue date: 12/17/1985
From: Jape F, Mathis J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17308A167 List:
References
50-335-85-29, NUDOCS 8512270441
Download: ML17308A169 (10)


See also: IR 05000335/1985029

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-335/85-29

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket No.:

50-335

Facility Name:

St. Lucie

1

License No.:

DPR-67

Inspector:

J. L. Mathis

Approved by:

ape,

Sectio

ie

Engineering

Branch

Division of Reactor Safety

Results:

One violation was identified - Inadequate

procedure

for removal of

upper guide structure.

I

Inspection

C

ducted:

November 4-8,

1985 and

November 12-15,

1985

c~- r 7,'~ SS

Date Signed

Accompanying Personnel:

W. S.

Kim, Korea Advanced

Energy Research

Institute

Y. H. Ryu, Korea Advanced

Energy Research

Institute

oP ~

ate

1gne

SUMMARY

Scope:

This routine,

unannounced

inspection entailed

84 inspector-hours

at the

site in the areas

of preparation

for refueling, refueling activity, and spent

fuel pool activity.

8512270441

851219

PDR

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REPORT DETAILS

Persons

Contacted

Licensee

Employees

  • K. N. Harris, Site Vice President of St. Lucie
  • T. Dillard, Maintenance

Superintendent

  • C. A. Pell, Technical Staff
  • R. Frechette,

Chemistry Superintendent

  • C. L. Wilson, Mechanical

Maintenance

  • J. Krumins,

Power Plant Engineer

  • H. F. Buchanan,

Health Physics

Superinteqdent

N. Roos, guality Control

(gC) Supervisor

J. Walsh,

gC Inspector

M. H. Mosley, .Refueling Coordinator

E. Wunderlich, Reactor

Engineer Supervisor

P. Tusing, Reactor

Engineer

Other

licensee

employees

contacted

included

engineers,

technicians,

operators,

mechanics,

office personnel.

Other Organizations

construction

craftsmen,

security force members,

and

Jim Viebrock, Nuclear Assurance

Corporation

(NAC) Vice President

H. Cross,

Exxon Nuclear Service

NRC Resident

Inspectors

  • R. Crlenjak, Senior

Resident

Inspector

  • H. Bibb, Resident

Inspector

  • S. Elrod, Section Chief

NRC

  • Attended exit interview

Exit Interview

The inspection

scope

and findings were summarized

on November 15,

1985, with

those

persons

indicated in paragraph

1 above.

The inspector

described

the

areas

inspected

and

discussed

in detail

the

inspection

findings.

j;No

dissenting

comments

were received

from the licensee.

I,

Violation (50-335/85-29-01),

Inadequate

procedure for removal

of~'upper

guide structure internal,

paragraph

5.

The licensee

did not identify as proprietary

any of the materials

provided

to or reviewed

by the inspector during this inspection.

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Licensee Action on Previous

Enforcement Matters

This subject

was not addressed

in the inspection.

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Unresolved

Items

Unresolved

items were not identified during the inspection.

Preparation for Refueling (80705), Unit

1

II

The St.

Lucie, Unit 1 nuclear

plant entered

mode six for refueling

on

October 31,

1985.

During the

outage

the inspector verified that prepara-

tions and conditions for defueling were in accordance

with NRC requirements.

The inspector

reviewed the following procedures

and documents:

OP 1-1600023,

Refueling Sequencing

Guidelines

j

OP 1-1630024,

Refueling Machine Operation

OP 1-1630023,

Fuel Transfer

System Operation

OP 1-1630022,

Spent

Fuel Handling Machine

OP 1-1630025,

Fuel Handling Building Ventilation System-Periodic

Test

GMP 1-M-0015, Reactor

Vessel

Maintenance-Sequence

of Operations

j,

St. Lucie Unit 1, Cycle 7, Safety Analysis Report

The

above

procedures

were

analyzed

for embodiment of the

necessary

'test

prerequisites,

preparations,

instructions,

acceptance

criteria and te'chnical

content.

On the morning of November 6, 1985, while removing the St. Lucie Unit'

core

internals

upper guide structure

(UGS) in preparation for defueling,

one of

three lifting rig attachments

gave

way.

This placed

the

upper

guide

structure

(UGS) in

a tilted position with its full weight of approximately

45

tons

supported

by the

remaining

two attachment

points.

Refueling

operations

were

immediately

stopped

with the structure

suspended

in

an

apparently

stable position with its bottom at

a level approximately two feet

below the reactor vessel

flange.

Florida Power

and Light (FPSL) declared

an

unusual

event at

10:45 a.m.,

(EST) in accordance

with the plant emer'gency

plan.

Immediately after the incident occurred

the licensee

designed

and

fabricated

an auxiliary lifting rig to aid in the removal of the

upper',

guide

structure.

Florida

Power

and Light succeeded

in lifting the core internals

UGS free of the reactor vessel

on November

9 and the structure

was placed in

its planned location in the refueling cavity.

After the

UGS was placed in

the refueling cavity

a preliminary inspection

revealed

some minor damage to

the regular lifting rig, but no significant

damage

to either the

UGS or core

barrel.

The inspector

reviewed

General

Maintenance

Procedure

Number~ 1-M-

0015,

Rev.

12,

Reactor

Vessel

Maintenance-Sequence

of Operations

which was

used to remove

the

UGS.

Procedure

1-M-0015 contained

provisions to torque

the lifting bolts to 50 ft. lbs once the three lifting bolts were

engaged

into the

threaded

holes

of the

UGS.

However,

there

was

no provision

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to verify that

the lifting bolts

were fully engaged

as specified

in

CE

Instruction Manual,

IP-19367-485-164-1,

Reactor

Internal Lift Rig Instruc-

tion Manual.

10 CFR 50, Appendix B, Criterion V,

as

implemented

by

FPSL

Topical Report

(FPLTgAR 1-76A), Section

T(R 5.0, Instructions,

Procedures

and

Drawings,

Rev.

5 requires that activities affecting quality shall beprescribed

by documented

instructions,

procedures,

or drawings, of a type appropriate

to

the circumstances

and shall

be accomplished

in accordance

with these,instruc-

tions, procedures,

or drawings.

Instructions,

procedures

or drawings shall

include

appropriate

quantitative

or qualitative

acceptance

criteria for

determining that important activities

have

been satisfactorily accomplished.

Contrary to the

above,

the

licensee

did not ensure

that the

procedure

1-M-0015, Reactor

Vessel

Maintenance-Sequence

of Operation for removal of

UGS included

an appropriate qualitative acceptance

criteria for determining

whether

the lifting bolts were fully engaged

in the

UGS flange.

This is a

violation against

10 CFR 50 Appendix B, Criterion

V and is identified

as

violation 50-335/85-29-01.

6.

Refueling Activities (60710)

Defueling for Unit

1 started

November 10,

1985

and

ended

on

November

14,

1985.

The licensee

placed

217 fuel

assemblies

into the spent fuel 'pool.

The inspector witnessed

at least

two shifts of defueling activities from the

control

room, refueling floor, and

spent fuel

pool

area.

Defueling

was

performed

in

accordance

with the controlling procedure

for refueling,

OP-1-1600022,

Rev.

14, Unit 1 Refueling Operation.

The inspector

observed

defueling to verify the following:

a)

Direct communication

was

established

between

the control

roomj', and

reactor building.

b)

Staffing

requirements

were

in accordance

with Technical

Specifica-

tions.

c)

Control of personnel

access

to the spent fuel pool areas.

d)

Changes

to

procedures

were

made

in accordance

with administrative

procedures.

e)

Licensee maintained

good housekeeping

in the refueling area.

f)

Radiological

controls

were

maintained

in accordance

with approved

procedures.

g)

Appropriate steps

and

gC hold points were signed off.

Within the areas

inspected,

no violations or deviations

were identified.

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Spent

Fuel

Pool Activity (86700)

On November

13 and 14,

1985, the inspector

observed

fuel handling operations

during fuel

movement

in the spent fuel

pool

area

and reviewed

procedures

related

to fuel handling to verify that the following were included in the

procedures:

a)

Provisions for verifying prior to fuel handling that the

spent ~fuel

pool ventilation

system

was operable.

b)

Provision for verifying that

minimum water level for the spent, fuel

pool

was monitored during fuel handling operations.

c)

Provision for verifying that the spent fuel pool storage

area radiation

and airborne radioactivity monitors were operable.

d)

Provision for verifying that the spent fuel pool cleaning

and cooling

systems

were operable.

e)

Provision for verifying prior to fuel handling that the spent fuel pool

area

crane

interlocks

or physical

stops

could prevent

the crane1lfrom

passing

over fuel storage

locations.

Fuel sipping

was

performed

by Nuclear

Assurance

Corporation

(NAC) in'he

spent fuel pool for reload

spent fuel in accordance

with the

NAC procedure

and

FPSL's Letter of Instruction

No. 1-0-19 (LOI-19).

After completion of

fuel sipping,

assemblies

identified as

suspect

leakers

were ultrasonically

tested

(UT) by Exxon Nuclear

Company

(ENC) to determine

which fuel piris were

leaking.

This effort was coordinated

by

FPKL with Combustion

Engineering

(CE)

and

NAC.

Out of the total

number of fuel assemblies

sipped

and UT'ed,

nine

(9)

were

confirmed leakers.

Exxon Nuclear

Company

provided

a fuel

assembly

reconstitution

procedure

to

be performed

on those

confirmed IExxon

fuel assembly

leakers

that will be reloaded for cycle 7,

and

CE supplied

a

fuel

assembly

reconstitution

procedure

to

be performed

on those

confirmed

CE fuel assembly

leakers that are intended to be reloaded for cycle

7i core.

The inspector

reviewed the

ENC evaluation of St. Lucie Unit

1 fuel recons-

titution, dated

November 5,

1985,

and the

CE evaluation for fuel reconsti-

tution, dated

October 28,

1985.

The results of the review confirmed~',that

there

were

no unreviewed

safety questions.

The following are

some of the

conditions that were used to assure criticality safety:

a)

Replacing

absorber

rods with fuel rods

b)

Placing fuel rods in guide tubes

c)

Placing four bundles together in a 2x2 array

Prior to final core verification,

CE and

ENC will provide documentation

to

FPSL that reconstituted

fuel assemblies

are certified mechanically safe for

continued

use in accordance

with the provisions of 10 CFR 50.59.

Within the areas

inspected,

no violations or deviations

were identified.

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