ML17291A646

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Insp Rept 50-397/95-01 on 950109-12.No Violations Noted. Major Areas Inspected:Liquid & Gaseous Radioactive Waste Mgt Programs Including Quality Assurance,Radioactive Liquid & Gaseous Effluent Sys & Repts of Radioactive Effluents
ML17291A646
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 02/01/1995
From: Murray B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17291A645 List:
References
50-397-95-01, 50-397-95-1, NUDOCS 9502150027
Download: ML17291A646 (27)


See also: IR 05000397/1995001

Text

APPENDIX

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-397/95-01

License:

NPF-21

Licensee:

Washington Public Power Supply System

3000 George Washington

Way

P.O.

Box 968,

MD 1023

Richland,

Washington

Facility Name:

Washington Nuclear Project-2

Inspection At:

Richland,

Washington

Inspection

Conducted:

January

9-12,

1995

Inspector:

J.

B. Nicholas,

Ph;D.,

Senior

Radiation Specialist

Facilities Inspection

Programs

Branch

Approved:

aine

urray,

ie

Facilities Inspection

Program

Branch

ate

Ins ection

Summar

Areas

Ins ected:

Routine,

announced

inspection of the liquid and gaseous

radioactive waste

management

programs

including quality assurance;

radioactive

liquid and gaseous

effluent systems;

reports of radioactive effluents;

engineered-safety-feature

air cleaning ventilation systems;

and

a review of

Licensee

Event Reports 397/94-012,

397/94-019,

and 397/94-021.

Results:

The radioactive waste effluent management

program

was being properly

implemented

(Section

1. 1).

The chemistry department

organizational

structure

and staffing met

requirements

(Section

1. 1).

The chemistry department

had experienced

very low turnover of technical

personnel

(Section

1. 1).

Comprehensive

quality assurance

audit

and assessment

programs of the

radioactive waste effluent program

and Offsite Dose Calculation

Manual

were implemented

(Section

2. 1).

9502l50027

950208

PDR

ADOCK 05000397

8

PDR

~

The corrective action program

was implemented properly (Section

2. 1).

~

A thorough quality assurance

audit was performed of the contractor

used

to perform the engineered-safety-feature

(ESF) air cleaning

systems'urveillance

tests

(Section

2. 1).

~

Good liquid and gaseous

radioactive waste effluent programs

were being

properly implemented

(Sections

3. 1 and 4. 1).

~

Radioactive Effluent Release

Reports

were submitted in a timely manner

and contained

the required information (Section

5. 1).

~

A good program was established

for testing the high efficiency

particulate air (HEPA) filter and charcoal

adsorption units in the

(ESF)

air cleaning

systems

(Section

6. 1).

Summar

of Ins ection Findin s:

~

Licensee

Event Reports

397/94-012,

397/94-019,

and 397/94-021

were

reviewed

(Section 7).

Attachments:

Attachment

1

Persons

Con'tacted

and Exit

Heeting'ttachment

2.

Attachment 3-

Summation of all Liquid Effluent,Releases

Summation of all Airborne Effluent Releases

Attachment

4 Haximum Annual

Doses

from Gaseous

and Liquid

Effluent Releases

Attachment

5 - Liquid Effluent Release

Summary...

Attachment

6 - Gaseous .Effluent,Release

Summary

-3-

DETAILS

1

ORGANIZATION AND MANAGEMENT CONTROLS

(84750)

The inspector

reviewed the organization

and staffing regarding the radioactive

waste effluent program to determine

agreement

with commitments in the Updated

Safety Analysis Report

and compliance with the requirements

in Technical Specification 6.2.

1. 1

Discussion

The inspector verified that the organizational

structure of the chemistry

department,

which is responsible for the implementation of the radioactive

waste effluent program,

was

as defined in the Updated Safety Analysis Report

and Technical Specifications.

It was noted that the chemistry department

was

assigned

the sole responsibility for implementing the radioactive waste

effluent program effective October

1993.

The chemistry department

organization

had three functional

areas

each

headed

by a supervisor or

technical specialist

who reported directly to the chemistry manager.

One of

these functional

areas

was responsible for implementing the radioactive waste

effluent program.

The assignment

of the chemistry department

placed the

implementation of the radioactive waste effluent program all within one

department

under the operations

department.

Management

control procedures

were reviewed for the assignment

of

responsibilities

for the management

and implementation of the radioactive

waste effluents program.

The chemistry department

was assigned

the

responsibility for preparing radioactive waste release

permits,

evaluating the

radioactive waste effluent releases,

calculating the radiation doses resulting

from the releases to'he environment,

and maintaining the radioactive waste

effluent release

data.

The inspector determined that the duties

and

responsibilities of the chemistry department

specified in the procedures

were

being implemented.

A group of 15 chemistry technicians staffing

6 rotational

shifts within the chemistry operations

functional

area

along with a senior

radiochemist

and technical specialist

assigned

to the radioactive waste

effluents functional

area

were responsible for collecting

and analyzing

radioactive waste effluent samples,

preparing the effluent release

permits,

and implementing the radioactive waste effluents program.

The inspector

interviewed several

of the chemistry staff responsible for the implementation

of the radioactive

waste effluents program

and determined that they were

familiar with the requirements

of the radioactive waste effluents program

and

maintained

a high level of performance.

The inspector

reviewed the staffing of the chemistry department

and determined

it to be adequate

and in accordance

with licensee

commitments.

There

had

been

a very low turnover of personnel

within the chemistry department

since the

previous

NRC inspection of this area in August 1993.

gO

1.2

Conclusions

The chemistry department

organizational

structure

and staffing met Technical

Specification requirements.

The radioactive

waste effluent management

program

was being implemented in accordance

with station procedures.

The chemistry

department

had experienced

a very low turnover of personnel

during the past

17 months.

2

EQUALITY ASSURANCE

PROGRAM (84750)

The inspector

reviewed the quality assurance

audit and assessment

programs

regarding the radioactive waste effluent program activities to determine

agreement

with commitments in the Updated Safety Analysis Report

and

compliance with the requirements

in Technical Specification 6.5.2.8.

2. 1 Discussion

The 'inspector

reviewed the quality assurance

audit schedules

for 1993,

1994,

and

1995; audit plans

and checklists;

and the qualifications of the quality

assurance

auditors

who performed the audits of the radiological

and non-

radiological

environmental

and effluent monitoring programs,

and Offsite Dose

Calculation Manual.

The review of the quality assurance

audit schedules

indicated that the audit of the radiological

environmental

monitoring and

radiological effluent programs

was scheduled

on

a

12 month frequency.

The

quality assurance

audit of the Offsite Dose Calculation

Manual

was scheduled

on

a 24 month frequency.

The audits were scheduled

in compliance with

Technical Specification audit frequency requirements.

Reports of quality assurance

audits performed during the period January

1993

through

December

1994 of the areas

related to the performance of the

radioactive waste effluent program were reviewed for scope,

thoroughness

of

program evaluation,

and timely followup of identified deficiencies.

The

audits

were performed in accordance

with quality assurance

procedures

and

schedules

by qualified auditors.

The reviewed audits of the radiological

and

non-radiological

environmental

and effluent monitoring programs,

and Offsite

Dose Calculation

Manual

and its implementing procedures

were of good quality

and provided satisfactory oversight

and evaluation of the licensee's

performance

in implementing the radioactive waste effluent program

and meeting

the Technical Specification

and Offsite Dose Calculation

Manual requirements.

The inspector

reviewed guality Assurance

Audit Report 293-618,

"Radiological

and Non-Radiological

Environmental

and Effluent Monitoring," dated

November

19,

1993, which was conducted

by an audit team that included

members with

radiochemistry

and radioactive waste effluent program experience.

Regulatory

Guide 4. 15, Revision

1, "guality Assurance for Radiological Monitoring

Programs-Effluent

Streams

and the Environment,"

was used

as the basis for

development of the audit scope

and checklists.

The inspector

reviewed the

audit checklist

and found it to be appropriate

in that it addressed

all

aspects

of the radiological liquid and gaseous

effluent program.

The audit

reviewed the radiological liquid and gaseous

effluent monitoring programs

including sampling,

analyses,

and radiological effluent release

procedures;

instrument calibration (i.e. isotopic calibration of the

new reactor building

elevated

release

point stack monitor);

and procedure

implementation of

Regulatory

Guide 4. 15 and Offsite Dose Calculation

Manual requirements.

The

audit identified two findings which were closed during the audit

and eight

recommendations

for improvement.

No deficiencies

were identified with the

radiological liquid and gaseous

effluent monitoring programs.

The inspector

reviewed guality Assurance

Audit Report 294-066,

"Radiological

and Non-Radiological

Environmental

and Effluent Monitoring Programs,"

dated

November

18,

1994,

which was conducted

by an audit team that included

members

with radiochemistry

and radioactive

waste effluent program experience.

The

audit reviewed,

in part,

the radiological liquid and gaseous

effluent

monitoring programs

and the implementation of Offsite Dose Calculation

Manual

requirements.

The audit results

indicated that the radiological

and non-

radiological

environmental

and effluent monitoring programs

were properly

implemented

and met program

and regulatory requirements.

However, the audit

identified six program deficiencies

which were documented

in Problem

Evaluation

Requests

(the station corrective action document).

Two Problem Evaluation

Requests

(PER 94-0911

and

PER 94-0943)

were initiated

to document identified problems with the timely completion of commitments

associated

with pre-operational

testing of the reactor building stack effluent

monitor.

The two Problem Evaluation Requests

were closed in a timely manner.

PER 94-0926

documented

several

identified activities required

by the Offsite

Dose Calculation

Manual which were associated

with the operation of the

gaseous

radwaste

system,

the land use census,

and atmospheric

dispersion

factors

and were not addressed

in the Plant Procedure

Manual.

The audit noted

that

no procedure

steps

were found which would initiate or implement main

plant vent release

monitor setpoint

changes

in the event of running the

Standby Offgas Treatment

System in the charcoal

bypass

mode.

The audit also

noted that chemistry procedures

did not contain guidance

on evaluating the

Land Use Census results for inclusion in the Radioactive Effluent Release

Report or the Offsite Dose Calculation Manual.

Atmospheric dispersion factors

from the station's

meteorological

tower were to be evaluated

annually;

however,

there

was

no procedure

guidance for performing the annual

evaluation

of the atmospheric

dispersion factors,

and the audit team could not find any

documentation

of the annual

evaluation of the atmospheric

dispersion factors

being performed in 1994.

Responses

to

PER 94-0926 were currently being

prepared

by the chemistry department for evaluation

and acceptance

by the

quality assurance

department for closure of the Problem Evaluation

Request.

PER 94-0927

documented

the findings that

an incorrect reporting format was

used to identify the Process

Control

Program revisions in the

1993 Radioactive

Effluent Release

Report,

and that the chemistry department

person calculating

the

31 day gaseous

effluent dose

was not performing the calculations properly

and did not have

a through understanding

of the

GASPAR II computer code.

Responses

to

PER 94-0927 were currently being prepared

by the chemistry

department for evaluation

and acceptance

by the quality assurance

department

for closure of the Problem Evaluation Request.

The audit team's

review of

Offsite Dose Calculation

Nanual

implementing procedures

resulted in the

issuance

of three suggestions

and

one recommendation

for program procedural

improvements.

The inspector

reviewed guality Assurance

Technical

Assessment

Report 93-006,

"Sulfuric Acid Transfer

To The Circulating Water Basin," dated

June

30,

1993.

Approximately 1000 gallons of concentrated

sulfuric acid were inadvertently

transferred

from the acid storage

tank to the neutralization tank in the

makeup water treatment

system in the basement

of the General

Services

Building.

Neutralization with caustic

was attempted,

but leakage of acid

through fittings prevented

completion of the neutralization with only about

a

third of the acid being neutralized.

The acid was then

pumped to the

circulation water basin

and neutralized with soda

ash.

The technical

assessment

presented

a very through evaluation of the potentially dangerous

situation.

The licensee

used

a contractor to .perform in-place filter testing

and

laboratory charcoal

adsorber

analyses

on the station's

ESF air cleaning

systems.

The licensee

used

an audit of the air cleaning

systems filter

testing contractor

performed

by

a Nuclear Procurement

Issues

Committee audit

team led by the licensee

during the period November 15-17,

1994, to evaluate

the performance of the contractor to perform the required tests

and to retain

his current status

on the licensee's

qualified suppliers list.

The inspector

reviewed the audit performed

on the contractor

and determined that the audit

was satisfactory to evaluate

the contractor's abilities to perform the

Technical Specification required

analyses

and surveillance activities.

The

audit identified three deficiencies

which were documented

in guality Finding

Reports.

Responses

to the guality Finding Reports

were not due from the

contractor until January

20,

1995.

Therefore,

the responses

were not

available for review at the time of the inspection.

The deficiencies did not

directly impact the contractor's

performance of the filter system testing or

the charcoal testing.

The inspector verified that the licensee

had also

performed

annual

evaluations of the contractor's

program

as required to retain

its current status

on the licensee's

qualified suppliers list.

2.2

Conclusions

guality assurance

audits of the radioactive waste effluent program

and Offsite

Dose Calculation

Hanual

were performed

as required.

These audits were

technically comprehensive

and provided

good program evaluation

and management

oversight, identified deficiencies,

and

made recommendations

for program

improvement.

The corrective action program

was

implemented properly.

A good

quality assurance

technical

assessment

which monitored the neutralization of

approximately

1000 gallons of sulfuric acid was performed.

A good audit

and

annual

evaluations

of the contractor

used to perform safety-related

air

cleaning systems'urveillance

testing

and analyses

were performed

as required

to retain the contractor's

current status

on the licensee's

qualified

suppliers list.

3

LIQUID RADIOACTIVE WASTE EFFLUENTS

(84750)

The inspector

reviewed the liquid radioactive

waste effluent program including

liquid waste processing,

liquid waste sampling

and analyses,

procedures

for

control

and release

of radioactive liquid waste effluents,

and surveillance

tests to determine

agreement

with commitments in the Updated Safety Analysis

Report

and compliance with the requirements

in Technical Specifications 6.8. 1,

6.8.4.d,

and 6. 14;

and the Offsite Dose Calculation

Manual Section 6.2. 1 and

Table 6.2.1.1.1-1.

4

3. 1

Discussion

The inspector

reviewed the licensee's

implementation of the liquid radioactive

waste effluent program

and Offsite Dose Calculation

Manual to ensure

compliance with sampling

and analyses

requirements,

analyses

sensitivities,

analytical results,

surveillance tests,

radioactive waste liquid effluent

control procedures,

and offsite dose results

from radioactive liquid

effluents.

The inspector

reviewed selected

procedures

governing the release

of liquid

radioactive waste effluents.

These

procedures

provided for the following:

recirculation

and sampling of the radioactive liquid waste;

radionuclide

analyses

of the radioactive liquid waste prior to release;

calculation of

effluent release

rate, effluent radiation monitor setpoints,

projected offsite

radionuclide concentrations,

and offsite doses prior to release;

and the

verification and recording of effluent discharge

flow rates,

effluent volume

discharged,

effluent discharge radiation monitor readings,

and dilution

parameters

during the release.

The inspector

reviewed

a representative

number of batch radioactive waste

liquid release

permits for the period January

1,

1994 through

December

31,

1994.

It was determined that the processing,

sampling,

and

analyses

of radioactive

waste liquid effluent and the approval

and performance

of batch liquid radioactive waste discharges

were conducted

in accordance

with

Offsite Dose Calculation

Manual requirements.

Quantities of radionuclides

released

in the liquid effluents were within the limits specified in the

Offsite Dose Calculation Manual.

Offsite doses

were calculated

according to

the Offsite Dose Calculation

Manual

and were within the required limits.

The

inspector verified that the licensee

was performing the Offsite Dose

Calculation

Manual required

analyses

on composite

samples of batch radioactive

liquid releases

for gross

alpha, tritium, strontium-89,

strontium-90,

and

iron-55.

The inspector

inspected

the chemistry laboratory

and radiochemistry counting

facility and determined that the licensee

had sufficient state-of-the-art

analytical

instrumentation

to perform the required radiochemistry analytical

measurements

of the radioactive waste effluents.

The inspector

inspected

the

radwaste building and the liquid radioactive waste processing

equipment

including the liquid radioactive waste floor drain tank and the two equipment

drain tanks

and the local

sample points at each of the liquid radioactive

waste storage

tanks for collecting representative

samples

from the respective

tanks prior to preparing effluent release

permits.

The liquid l adioactive

waste processing

and storage

systems

were installed

as described

in the

Updated Safety Analysis Report

and operated

in accordance

with station

procedures

to ensure

compliance with Offsite Dose Calculation

Manual

requirements.

The inspector determined that

no design modifications

had

been

made to the

liquid radioactive

waste

management

systems

during 1992,

1993,

and

1994.

3.2

Conclusions

The licensee

was implementing

a liquid radioactive waste effluent program in

accordance

with the Technical Specifications

and the Offsite Dose Calculation

Manual.

The quantities of radionuclides

released

in the liquid radioactive

waste effluents were within the Offsite Dose Calculation

Manual limits.

Offsite doses to the environment

from the liquid radioactive waste effluents

had

been calculated

using Offsite Dose Calculation

Manual methodologies,

and

the dose results

were within Offsite Dose Calculation

Manual limits.

The

licensee

had not made

any major equipment or design modifications to the

radioactive liquid waste

management

systems

during 1992,

1993,

and

1994.

4

GASEOUS

RADIOACTIVE WASTE EFFLUENTS

(84750)

The inspector

reviewed the gaseous

radioactive

waste effluent program

including gaseous

waste processing,

gaseous

waste

sampling

and analyses,

and

procedures

for the control

and release of gaseous

waste effluents to determine

agreement

with commitments in the Updated Safety Analysis Report

and

compliance with the requirements

in Technical Specifications 6.8.1, 6.8.4.d,

and 6. 14;

and the Offsite Dose Calculation

Manual Section 6.2.2

and Table

6.2.2.1.2-1.

4.1

Discussion

The inspector

reviewed the licensee's

implementation of the gaseous

radioactive

waste effluent program

and Offsite Dose Calculation

Manual to

ensure

compliance with sampling

and analyses

requirements,

analyses

sensitivities,

analytical results,

surveillance tests,

radioactive waste

gaseous

effluent control procedures,

and offsite dose results

from radioactive

gaseous

effluents.

The inspector

reviewed selected

procedures

governing the continuous

and batch

releases

of gaseous

radioactive waste effluents.

These

procedures

provided

for the sampling

and analysis of the radioactive

gaseous

waste effluents,

calculation of effluent release

rate, calculation of projected offsite

radionuclide concentrations

and doses,

and calculation

and verification of

gaseous

effluent radiation monitor setpoints prior to release;

recording of

dilution parameters

during the release;

and verification of effluent discharge

flow rates

and effluent volume discharged.

The inspector

reviewed selected

gaseous

waste

sample

analyses

for samples

from

the main plant vent, turbine building vents,

and radwaste building vent

continuous

releases

and selected

gaseous

waste release

permits for batch

releases

for containment

vents

and purges for the period January

1,

1994

through

December

31,

1994.

It was determined that the sampling,

analyses,

and

discharge of the radioactive

gaseous

effluents

and the approval of the

radioactive

gaseous

waste containment

vents

and purges

were conducted

in

accordance

with Offsite Dose Calculation

Manual requirements.

guantities of

gaseous

and particulate radionuclides

released

were within the limits

specified in the Offsite Dose Calculation Manual.

Offsite doses

had

been

calculated

according to Offsite Dose Calculation

Manual methodologies

and were

within required limits.

Particulate effluent composite

sample

analyses

for

gross

alpha,

strontium-89,

and strontium-90

had

been

performed

and met Offsite

Dose Calculation

Manual requirements.

The inspector determined that

no major

equipment or design modifications

had

been

made to the radioactive

gaseous

waste

management

systems

during

1993

and

1994.

/

4.2

Conclusions

The licensee

was implementing

a gaseous

radioactive waste effluent program in

accordance

with the Technical Specifications

and the Offsite Dose Calculation

Manual.

The quantities of radionuclides

released

in the gaseous

radioactive

waste effluents were within the Offsite Dose Calculation

Manual limits.

Offsite doses

to the environment

from the gaseous

radioactive waste effluents

had

been calculated

using Offsite Dose Calculation

Manual methodologies,

and

the dose results

were within Offsite Dose Calculation

Manual limits.

The

licensee

had not made

any major equipment or design modifications to the

radioactive

gaseous

waste

management

systems

during

1993

and 1994.

5

REPORTS

OF RADIOACTIVE EFFLUENTS

(84750)

The inspector

reviewed reports

concerning radioactive

waste

systems

and

effluent releases

to determine

compliance with the requirements

of 10 CFR Part 50.36(a)(2),

Technical Specifications 6.9. l. 11

and 6. 14,

and the Offsite Dose

Calculation

Hanual

Section 6.4.2.

5. 1

Discussion

/

The inspector

reviewed the Semiannual

Radioactive Effluent Release

Reports for

the time periods January

1,

1992 through June

30,

1992,

and July 1,

1992

through

December

31,

1992,

and the Annual Radioactive Effluent Release

Report

for the time period January

1 through

December

31,

1993.

The reports

were

written in the format described

in NRC Regulatory

Guide 1.21,

Revision

1, June

1974,

and contained

the information required

by the Offsite Dose Calculation

Manual.

During the time period January

1 through

December

31,

1992, the

licensee

performed

161 liquid batch releases,

75 containment

vents,

and

15

containment

purges.

During the time period January

1 through

December 31,

1993,

the licensee

performed

201 liquid batch releases,

52

containment

vents,

and

19 containment

purges.

-10-

The licensee

reported

two abnormal

releases

of radioactive liquid waste during

1992

and

no abnormal effluent releases

during 1993.

Problem Evaluation

Requests

292-0622

and 292-0671

documented

the

1992 abnormal

release

events.

During the performance of the monthly batch release

composite for the month of

May 1992,

one batch release

sample out of 24 batch releases

for that month was

found to be missing.

The missing

sample

was attributed to the fact that the

original entry of the batch release

in the Liquid Release

Log was voided.

The

voided log entry resulted

in the disposal of the sample

as

a terminated

release.

The loss of the sample

had very little impact

on the analytical

results of the monthly and quarterly composite

analyses for tritium, gross

alpha,

strontium-89; strontium-90,

and iron-55.

The inspector

reviewed the

licensee's

description

and followup actions

concerning

the missing

sample

and

determined that the licensee

had determined

the root cause of the event

and

had taken appropriate corrective action.

At no time were

any Offsite Dose

Calculation

Manual

dose or release

concentration limits exceeded.

The second

abnormal

release

event

happened

on June

11,

1992, with a partial

release

of Floor Drain Tank TK-9 before its radioactivity analysis

was

completed.

Using

a release

authorization permit for Equipment Drain Tank

TK-4B, the radwaste

control

room operator mistakenly started to release

Floor

Drain Tank TK-9, which he

knew had

been

sampled.

However, the radioactivity

analysis

and release

authorization for Floor Drain Tank TK-9 had not been

completed.

The radwaste

control

room operator terminated the release

of Floor

Drain Tank TK-9 when

he noted

no decrease

in the Equipment Drain Tank TK-4B

tank level

he thought

he was releasing.

Approximately 11,750 gallons of

radioactive liquid waste effluent were released

from Floor Drain Tank TK-9 to

the river before the release

was terminated.

The inspector reviewed the

licensee's

description

and followup actions concerning the abnormal

release

event

and determined that the licensee

had determined

the root cause of the

event

and

had taken appropriate

corrective action.

At no time were any

Offsite Dose Calculation

Manual

dose or release

concentration limits exceeded.

Both Problem Evaluation

Requests

were closed

by the licensee.

Effluent monitoring instrumentation

had not been out of service in excess of

Technical Specification requirements

during

1992

and

1993.

The inspector

reviewed

changes

(Amendments

11,

12,

13,

14,

15,

and

16) to the

Offsite Dose Calculation Manual, which were

made

and approved

by the Plant

Operations

Committee during

1992

and

1993.

The changes

were well documented

in the Radioactive Effluent Release

Reports

as required

by the Offsite Dose

Calculation Manual.

Summaries of the radioactive liquid and gaseous

effluent releases

and

associated

doses for 1992

and

1993 are presented

in Attachments

2 through

6 to

this inspection report.

5.2

Conclusions

The licensee

had submitted the Radioactive Effluent Release

Reports for 1992

and

1993 in

a timely manner,

and the reports

contained all the required

information presented

in the format described

in

NRC Regulatory

Guide 1.21.

The abnormal

radioactive liquid effluent releases

did not exceed

any Offsite

Dose Calculation

Hanual limits.

Changes

to the Offsite Dose Calculation

Hanual

were properly documented.

6

AIR CLEANING SYSTEMS

(84750)

The inspector

reviewed the engineered-safety-feature

air cleaning

systems

testing

program to determine

agreement

with the commitments

in the Updated

Safety Analysis Report

and compliance with the requirements

in Technical Specifications 4.6.5. 1, 4.6.5.3,

and 4.7.2.

6. 1

Discussion

The inspector

reviewed selected

procedures

and surveillance test results

and

records for the surveillance testing of the

ESF air cleaning

systems

which

contained

HEPA filters and activated

charcoal

adsorbers.

The inspector

verified that the procedures

and surveillance tests

provided for the required

periodic functional checking of the

ESF air cleaning systems'omponents,

evaluation of the

HEPA filters and activated

charcoal

adsorbers,

and the

replacement

and in-place filter testing of the filter systems.

Selected

records

and test results for the time period January

1993 through

December

1994 for the standby

gas treatment

system

and control

room emergency

filtration system

were reviewed.

The in-place filter testing,

activated

charcoal

laboratory tests,

and the control

room emergency filtration system

pressure

testing were performed in accordance

with approved

procedures

by a

contract laboratory

and the licensee,

and the test results

were verified to be

within Technical Specification limits except for the test results

documented

in Licensee

Event Reports94-012,

94-019,

and 94-021.

The inspector noted

that the

ESF air cleaning systems'perating

hours

was being tracked

by the

control

room on the daily shift log to meet the Technical Specification

requirement for testing the two

ESF air cleaning systems'ctivated

charcoal

.

adsorber material

at least every

18 months or after every

720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> of

operation.

6.2

Conclusions

The

ESF air cleaning

systems

conformed to the commitments in the Updated

Safety Analysis Report

and met the Technical Specification requirements.

The

ESF air cleaning

systems

were tested

in accordance

with Technical

Specification requirements,

and the test results

were within Technical

Specification limits except for the test results

documented

in Licensee

Event

Reports94-012,

94-019,

and 94-021.

-12-

7

ONSITE REVIEW OF LICENSEE EVENT REPORTS

(92904)

7.1

0 en

Licensee

Event

Re ort 397 94-012:

Control

Room

Emer enc

Filter

WMA-FU-54B Ino erable

Due to Leakin

Delu

e

Su

1

Isolation Valve

On June

23,

1994,

approximately five inches of water was discovered

in the

bottom of the control

room emergency filter unit, WMA-FU-54B.

The water

came

from leakage

past

a deluge

system isolation valve (FP-V-WMA/21), which had

been

observed to be leaking in March 1994 but had not been repaired.

This

caused

the control

room emergency filter unit's charcoal filter to be

inoperable.

Spring-loaded

check valves installed in the filter unit's bottom

drain lines trapped

the water in the filter unit wetting the charcoal filter

bed

and causing it to be not available to perform its design safety function.

Immediate corrective action taken

by the licensee

included replacing the

leaking deluge

system isolation valve, cleaning the filter unit,

and replacing

and testing the charcoal filter bed.

The inspector reviewed the licensee's

corrective actions

and the safety

significance of the event.

In the event of an accident,

the filter unit

actuates

to protect the control

room personnel

from airborne particulate

and

iodine radioactivity by pressurizing

the control

room with filtered air.

Because five inches of water had collected in the bottom of the filter unit,

the iodine removal efficiency of the charcoal filter bed

was significantly

reduced,

and the charcoal filter unit was not able to perform its design

safety function.

The inspector

reviewed the radiological

dose significance of

the event in the case of an accident during the time the filter unit was not

available to filter and remove radioactive iodine from the incoming air to the

control

room and the subsequent

radiation

dose to the control

room personnel.

As described

below, the inspector

reviewed the licensee's

radiological

dose

calculations

performed to determine

the safety significance

and potential

radiological

consequences

as

a result of the event.

Formal resolution

and

closure of this event will be documented

in

NRC Inspection

Report

50-397/94-34.

7.2

0 en

Licensee

Event

Re ort 397 94-019:

Gasket Missin

From Main

Control

Room Air Handler

WMA-AH-51B Precludes

Associated

Emer enc

Fan

WMA-FN-54B From Sufficientl

Pressurizin

The Control

Room

On November 21,

1994, with the plant at

100 percent

power, control

room

emergency

fan unit WMA-FN-54B failed to pressurize

the main control

room

sufficiently to meet Technical Specification surveillance

requirements.

A

missing gasket,

removed October

26,

1994,

from access

door

3 of the main

control

room air handling unit WMA-AH-54B, caused air leakage

around the door

with the missing gasket

and precluded sufficient main control

room

pressurization

to meet Technical Specification surveillance

requirements.

Pressurization

of the main control

room during the event of an accident is

part of the design function of the control

room emergency air handling unit to

protect control

room personnel

and maintain control

room habitability.

During

a loss of coolant accident,

a protection signal automatically isolates

the

-13-

normal'control

room ventilation system

and initiates emergency pressurization

of the control

room.

Technical Specifications

require that each

emergency

fan

unit be capable of pressurizing

the main control

room to 0. 125 inches of water

column with respect to adjacent

areas

to prevent unfiltered air inleakage.

During the surveillance testing of control

room emergency

fan unit WHA-FN-54B,

the emergency

fan unit only pressurized

the main control

room to 0.05 inches

of water column failing the surveillance test.

A new door gasket

was

installed

on access

door 3 on November 22,

1994,

and the main control

room air

handling unit WMA-AH-54B and associated

emergency

fan unit WHA-FN-54B were

retested

on November

23,

1994.

The main control

room air handling unit again

failed its surveillance pressurization

test

due to an unrelated

work activity

performed

on November

22,

1994,

as described

in Licensee

Event Report 94-021.

As described

below, the inspector

reviewed the safety significance

and

potential radiological

consequences

as

a result of the event.

Formal

resolution

and closure of this event will be documented

in

NRC inspection

report 50-397/94-34.

7.3

0 en

Licensee

Event

Re ort 397 94-021:

Holes Cut In Main Control

Room

Floor Penetration

5016 Precludes

Redundant

Emer enc

Fans

WMA-FN-54A B

From Pressurizin

The Control

Room Sufficientl

To Meet The

A licable

Surveillance

On November 23,

1994, with the plant at

100 percent

power, it was determined

during the performance of a routine pressurization

surveillance test of the

main control

room that

a flow path created

by a barrier impairment in the main

control

room floor to the cable spreading

room through penetration

5016

located

under instrument

panel

H13-P682 prevented

emergency

fan unit

WHA-FN-54B from pressurizing

the main control

room sufficiently to meet

Technical Specification requirements.

The main control

room barrier

impairment

was caused

by two holes cut in the main control

room floor into the

cable spreading

room below the main control

room on November 22,

1994.

This

event prevented

both redundant

control

room emergency

fans,

WHA-FN-54A(B),

from pressurizing

the main control

room sufficiently to meet Technical

Specification surveillance

requirements.

The licensee's

assessment

of the

surveillance test results

indicated that the main control

room still would

have

been

amply pressurized

to prevent infiltration of air during

a postulated

accident involving a radioactive release.

The two holes in penetration

5016

were sealed

approximately

one hour after the failure of the initial

pressurization

surveillance test of the main control

room.

The main control

room pressurization

surveillance test

was performed,

and the main control

room

pressurization

capability by both emergency

fans

WHA-FN-54A(B) was verified.

As described

below, the inspector

reviewed the safety significance

and

potential radiological

consequences

as

a result of the event.

Formal

resolution

and closure of this event will be documented

in

NRC inspection

report 50-397/94-34.

'h

During the inspection,

the inspector reviewed the design

and operation of the

main control

room emergency air handling

and associated filtration units

identified in the three related

Licensee

Event Reports

summarized

above.

The

inspector interviewed the system engineer responsible for the main control

room emergency air handling units,

performed

a walkdown of the main control

room emergency air handling units

and inspected

the failed equipment

identified in the Licensee

Event Reports for repair

and operability.

The

inspector also reviewed

how the failed equipment affected the designed

performance of the main control

emergency air handing units

and the

consequences

its failure caused

in radiologically protecting the control

room

personnel

and maintaining control

room habitability in the event of an

accident.

As

a result of the first event reported in Licensee

Event Report 94-012,

inoperability of the charcoal filter bed in the main control

room filter unit

WMA-FU-54B, the licensee

performed

an evaluation to determine

the radioactive

iodine dose to control

room personnel

from a hypothetical

dropped fuel bundle

accident during the time the main control

room emergency air handing unit

charcoal filter bed

was not available to perform its design function.

The

licensee'sed

the postulated

dropped fuel bundle design basis

accident

scenario

to evaluate

the radiological

consequences

to the control

room

personnel

since the reactor

had

been in cold shutdown for a maintenance

outage

since April 26,

1994.

The licensee

used the computer

code

"PADD" with design

basis

source

term input of the isotopic concentrations

of iodines

and noble

gases

taken from the Updated Safety Analysis Report,

Table 15.7-20 for

airborne radioactivity in the secondary

containment

due to a fuel handling

accident,

to perform the radiological

dose calculations for the postulated

scenario.

The results of the evaluation,

assuming that the accident

happened

35 days after shutdown of the reactor

and

no filtration was available,

indicated that the 30 day integrated radiation dose to the control

room

personnel

would be quite low.

The calculated radiation

dose results

indicated

that the whole body 30 day integrated

dose to control

room personnel

would be

approximately 2.6 E-04

Rem,

and the 30 day integrated thyroid dose would be

approximately 2.7 E-03

Rem.

The inspector postulated

a "worst case"

accident

which could have

happened

while the reactor

was at

100 percent

power prior to the shutdown April 26,

1994,

since there

was indication of leakage

past the deluge valve in March

1994.

The inspector requested

the licensee

to perform radiation

dose

calculations

based

on the postulated

designed

basis loss of coolant accident

scenario

as

an additional evaluation of the radiological

consequences

resulting from the events

described

in the above

Licensee

Event Reports.

The

licensee

used the computer

code

"PADD" with source

term input of the isotopic

concentrations

of iodines

and noble gases

taken from design basis

source

term

calculations

performed

by the computer

code

ORIGIN which very closely

approximated

the iodine and noble gas isotopic airborne radioactivity isotopic

concentrations

presented

in the Updated Safety Analysis Report,

Table 15.6-13

for airborne radioactivity in the primary containment

due to

a design basis

loss of coolant accident,

to perform the radiological

dose calculations for

the postulated

scenario.

The calculated radiation

dose result indicated that

-15-

the 30-day integrated thyroid dose would be approximately 8.6

Rem based

on the

assumptions

of no main control

room air filtration, a primary containment to

secondary

containment leak rate of 0.05 percent

per day,

and

a secondary

containment

bypass

leak rate of 0.33 standard

cubic feet per hour as measured

during the plant's eighth refueling outage

in the

summer of 1993.

These

values

were below the General

Design Criterion

19 of Appendix A, to

10 CFR Part 50, values of 5

Rem whole body

gamma dose,

30

Rem beta skin dose,

and

30

Rem thyroid dose

from exposure to direct radiation from external

sources

and

from airborne radioactivity within the control

room to control

room personnel.

Therefore,

a significant, but not an overexposure,

thyroid radiation dose

could have

been received

by control

room personnel

during the time the main

control

room air filtration unit was possibly inoperable

and the reactor

was

operating at

100 percent

power and all other redundant safety

systems

were

also inoperable

and not available.

ATTACHMENT 1

1

PERSONS

CONTACTED

1. 1

Licensee

Personnel

  • J. Parrish,

Vice President,

Nuclear Operations

J.

P. Albers, Radiation Protection

Manager

  • A. L. Alexander,

Lead Effluents Technical Specialist,

Chemistry

R. J.

Barbee,

Manager,

Technical

Services

A. S. Barber,

Technical Specialist, guality Assessments

  • P.

R.

Bemis,

Manager,

Regulatory

Programs

  • D. A. Bennett,

Acting Chemistry Manager

I. H. Borland, Technical Specialist,

guality Assessments

  • W. S. Davison,

Manager,

Plant Support Assessments

  • K. B. Lewis, Compliance

Engineer,

Regulatory

Programs

  • H, P.

Hedges,

Corporate

Chemist

R. L. Koenigs,

Manager,

Design Engineering

C.

R. Madden,

Technical Specialist,

guality Assessments

  • R. D. Madden,

Technical Specialist,

guality Assessments

J.

W. Massey,

Technical Specialist,

Operations

Event Analysis Resolution

  • J. J. Muth, Hanager,

Plant Assessments

  • L. H. Nolan,

Radwaste

Supervisor

  • J. H. Pedro,

Compliance

Engineer,

Regulatory

Programs

C. J.

Schwarz,

Operations

Manager

J.

D. Snyder,

Plant Support Engineering

  • J. H. Swailes,

Plant Manager

  • D. A. Swank,

Licensing Manager,

Regulatory

Programs

B. L. Twitty, Principal

Engineer,

guality Assessments

J.

C. Wiles, Technical Specialist,

guality Assessments

C. J.

Zimmer,

System Engineer

1.2

NRC Personnel

R. Barr, Senior Resident

Inspector

D. Prouix, Resident

Inspector

In addition to the personnel

listed above,

the inspector contacted

other

personnel

during the inspection.

  • Denotes

personnel

that attended

the exit meeting

on January

12,

1995.

2

EXIT MEETING

An exit meeting

was conducted on'anuary

12,

1995.

During this meeting,

the

inspector reviewed the scope

and findings of the report.

The licensee did not

express

a position

on the inspection findings documented

in this report.

The

licensee

did not identify as proprietary,

any information provided to, or

reviewed by, the inspector during the inspection.

ATTACHMENT2

SNHATION OF ALL LI UIO EFFLUENT RELEASES

QUARTER

1

QUARTER 2

QUARTER 3

QUARTER 4

QUARTER

1

QUARTER 2

QUARTER 3

QUARTER 4

1.

Number of Batch

Releases

2. Fission

8 Activation

Products

(Curies)

3. Tritium (Curies)

4. Oissolved

8 Entrained

Noble Gases

(Curies)

5. Waste Volume Released

(liters)

16

4.7 E-03

4.5 E-01

<5.0 E-04

9.2 E+05

53

6.5 E-02

2.6 E+00

<1.1 E-04

3.0 E+06

70

2.2 E-02

4.9 E+00

1.0 E-03

4.0 E+06

22

3.0 E-03

2.8 E+00

1.3 E-03

1.3 E+06

28

7.0 E-03

1.3 E+Ol

<2.3 E-04

1.6 E+06

41

6.8 E-02

7.7 E+00

1.2 E-04

2.4 E+06

77

1.1 E-01

7.9 E+00

3.4 E-03

4.4 E+06

55

1.8 E-02

5.6 E+00

1.4 E-03

3.1 E+06

A%IACHMENT3

SUHHATION OF ALL AIRBORNE EFFLUENT RELEASES

QUARTER I

QUARTER 2

QUARTER 3

QUARTER 4

QUARTER

1

QUARTER 2

QUARTER 3

QUARTER 4

1.

Number of Vents/Purges

Released

2. Fission

8 Activation

Products

(Curies)

3. Total Iodine-131

(Curies)

4. Particulates

with Half

Lives > 8 days (Curies)

5. Tritium (Curies)

7.8 E+01

2.4 E-03

2.3 E-02

6.4 E+00

33/2

6.6 E+00

2.1 E-03

4.5 E-03

2.3 E+00

3.3 E+01

1.4 E-03

2.4 E-03

1.4 E+01

42/13

3.3 E+01

2.6 E-03

5.8 E-03

2.6 E+01

4.3 E+01

8.4 E-03

3.5 E-03

5.1

E+01

9.2 E+00

2.5 E-03

2.3 E-03

4.8 E+01

52/19

7.8 E+01

1.4 E-03

4.2 E-03

3.7 E+01

1.2 E+01

7.0 E-04

1.3 E-02

1.5 E+01

ATTACHMENT4

HAXIHIIIANNUAL DOSES

FROH GASEOUS AND LI UID EFFLUENT RELEASES

Liquid Effluents

Mhole Body

Organ (Liver)

Gaseous

Effluents

Noble Gas

Ganea (Air Dose)

Beta (Ail Dose)

0.03 mrem

0.04 mrem

0.12 mrad

0.11 mrad

3 mrBll

10 mrem

10 mrad

20 mrad

I.IX

0.4X

1.20K

0.53K

Iodine-131,

Iodine-133,

Tritium, and

Particulates

with Half Lives > 8 days

0.14 mrem

15 mrem

0.92K

.'.;P>:."'..",,'"',".'.",'.":g>:.:,.Ile~t;'.,'.'of,-'.kgmlta'"'.5'.': .";,.:,:<<@i

Liquid Effluents

'Mhole Body

Organ (Liver)

Gaseous

Effluents

Noble Gas

Gama (Air Dose)

Beta (Air Dose)

Iodine-131,

Iodine-133,

Tritium, and

Particulates

with Half Lives > 8 days

0.12 mrem

0.19 mrem

0.10 mrad

0.07 mrad

0.18 mrem

3 mrem

10 mrem

10 mrad

20 mrad

15 mrem

4. 01<<

1.9X

1.02K

0.34K

1.19K

ATTACHMENT5

LI UID EFFLUEKT RELEASE SUMMARY

Kumber of Batch Releases

Total Fission and Activation

Products

Released

(Curies)

Total Tritium Released

(Curies)

Total Dissolved and Entrained

Gases

Released

(Curies)

Total Gross Alpha Released

(Curies)

Waste

Volume Released (liters)

Total Whole Body Dose

(mrem)

Maximum Organ Dose

(mrem)

161

9.5 E-02

1.1

E+01

2.3 E-03

0.0 E+00

9.2 E+06

3.3 E-02

4.0 E-02

201

2.1 E-01

3.4

E+01

5.0 E-03

5.2 E-10

1.1

E+07

1.2 E-01

1.9 E-01

ATTACHMENT6

GASEOUS EFFLUENT RELEASE SUHHARY

Number of Vents 5 Purges

Total Fission and Activation

Products

Released

(Curies)

Total Iodine-131 Released

(Curies)

Total Particulates with Half

Lives )8 Days Released

(Curies)

Total Gross Alpha Released

(Curies)

Total Tritium Released

(Curies)

Garana Air Dose

(mrad)

Beta Air Dose (mrad)

Haximum Organ

Dose

(mrem)

88

1.5 E+02

8.3 E-03

3.6 E-02

0.0 E+00

4.9

E+01

0.12E+00

0.11E+00

0.14E+00

71

1.4 E+02

1.3 E-02

2.3 E-02

1.3 E-10

1.3 E+02

0.10E+00

0.07E+00

0. 18E+00