ML17286A686

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Insp Rept 50-397/91-04 on 910114-0217.Violations Noted.Major Areas Inspected:Control Room Operations,Licensee Action on Previous Insp Findings,Operational Safety Verification,Maint & Surveillance Programs & LERs
ML17286A686
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 03/19/1991
From: Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17286A684 List:
References
50-397-91-04, 50-397-91-4, NUDOCS 9104080219
Download: ML17286A686 (21)


See also: IR 05000397/1991004

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report No:

Docket No:

Licensee:

50-397/91-04

50-397

Washington Public Power Supply System

P. 0.

Box 968

Richland,

WA 99352

Facility Name:

Washington Nuclear Project

No.

2 (WNP-2)

Inspection at:

'NP-2 site near Richland, Washington

Inspection

Conducted:

January

14 - February

17,

1991

Inspectors:

R.

C. Sorensen,

Senior Resident

Inspector

D. L. Proulx, Project Inspector

Approved by:

P.

H. J hnson,

Chief

React

Projects

Section

3

Date

igned

Summary:

Ins ection

on Januar

14 - Februar

17

1991

50-397/91-04

Areas Ins ected:

Routine inspection

by the resident inspector

and

a region-

ase

inspector of control

room operations,

licensee

action

on previous

inspection findings, operational

safety verification, surveillance

program,

maintenance

program, licensee

event reports,

special

inspection topics,

procedural

adherence,

occupational

safety,

and review of periodic reports.

During this inspection,

Inspection

Procedures

61726,

62703,

71707,

71710,

90712, 90713,

92700,

92701,

92702,

93001

and 93702 were utilized.

Safet

Issues

Mana ement

S stem

SINS

Items:

None.

Results:

General

Conclusions

and

S ecific Findin

s

Si nificant Safet

Matters:

None.

Summar

of Violations and Deviations:

One violation was identified,

invo ving fai ure to proper y test the standby

gas treatment

system in

accordance

with Technical Specification requirements.

0 en Items

Summar

Four followup items

and

one

LER were closed;

one

new item was

opene

.

~1040S02i9

9i03>9

PD4

ADOCK 05000 '97

9

PDR

DETAILS

Persons

Contacted

J. Baker, Plant Manager

  • L. Harrold, Assistant Plant Manager

C. Edwards, guality Control Manager

  • R. Graybeal,

Health Physics

and Chemistry Manager

  • J. Harmon, Maintenance

Manager

  • H. McGilton, Operational

Assurance

Manager

"A. Hosier, Licensing Manager

S. Davison, guality Assurance

Nanager

  • R. Koenigs, Generation

Engineering

Manager

  • S. McKay, Operations

Manager

  • J. Peters,

Administrative Manager

G. Gelhaus,

Assistant Technical

Manager

W. Shaeffer, Assistant Operations

Manager

  • R. Webring, Plant Technical

Manager

The inspectors

also interviewed various control

room operators, shift

supervisors

and shift managers,

maintenance,

engineering, quality

assurance,

and management

personnel.

"Attended the Exit Meeting on February

19, 1991.

Plant Status

At the start of the inspection period, the plant was operating at

100%

power.

Power was reduced

on February

16 to approximately

70$ power due

to problems with the "A" reactor feedwater

(RFW) turbine governor.

The

"A" RFW pump was

removed from service

and the actuator for the turbine

governor

was replaced.

The "A" RFW pump was returned to service

on

February

17

and reactor

power was in the process

of being returned to

100% at the end of the inspection period.

Standb

Gas Treatment

SGT

S stem Surveillance Testin

Problems

61726)

On January

24, the licensee

performed

a surveillance test of the

upstream

charcoal

adsorber

bed

on the "A" train of SGT, in accordance

with Plant Procedures

Manual

(PPN) 7.4.6.5.3.6,

"SGT System Adsorber

Bypass

Leakage Test,-" Revision 5.

This test is conducted

by injecting

Freon at

a point upstream of the charcoal

bed

and measuring

the Freon

concentrations

both upstream

and

downstream of the charcoal

bed.

The

results

are acceptable if the downstream concentration is less

than'.05%

of the upstream concentration,

indicating no significant bypass

leakage.

Each train of SGT at WP-2 contains

two separate

charcoal

beds

in series,

and they had normally been tested

separately.

Unsatisfactory

results

were obtained for the upstream

bed

on January

24,

and the "A"

train of SGT was declared

inoperable.

A Problem Evaluation Request

'(PER)

was initiated and was addressed

by the Management

Review Committee

(MRC) on January

25.

MRC dispositioned

the

PER for Generation

Engineer-

ing review and evaluation.

Later

on January

25, Generation

Engineering

determined

the "A" train of SGT to be operable

and the Technical

, Specification

(TS) action statement

was exited.

On January

28 the

I

inspector

reviewed the

PER to determine

the rationale for returning the

"A" train to an operable status.

The inspector

noted that,

as

a result of the

PER, the licensee

revised

PPN 7.4.6.5.3.6

to test both charcoal

adsorber

beds concurrently, in

series..

The inspector also noted from review of the procedure that the

sample points both upstream

and downstream of the charcoal

beds

were

moved,

and the injection point was moved also.

The charcoal

beds in

both trains were then retested

concurrently

and their operability (when

treated

as

one integral adsorber unit in each train) was demonstrated.

The inspector

subsequently

verified that this test method, after the

procedure revision, satisfied

the

TS for testing of the charcoal

beds.

Each train of SGT at WNP-2 also contains

two separate

high efficiency

particulate air (HEPA) filter banks in series

(one upstream

and

one

downstream of the charcoal

adsorber

bed), with four HEPA filters in each

bank.

The

HEPA filters have

bypass

leakage testing requirements

similar

to t'>>ose for the charcoal

adsorber

beds,

except that particulate dioctyl

phthalate

(DOP) is used for the

HEPA filters in place of Freon.

The

TS

direct that bypass

leakage testing for*the HEPA filters and charcoal

beds

be conducted

per the guidance in Regulatory Positions C.5.c,

and

C.5.d, respectively, of Regulatory

Guide 1.52.

These Regulatory

Positions of Regulatory Guide 1.52 direct this testing to be conducted

per Sections

10 and 12, respectively, of ANSI Standard

N510-1975.

Sections

10 and

12 of ANSI N510-1975 both state specifically that

Section

9 of ANSI N510-1975 is

a prerequisite.

Section

10 also states

that if the

HEPA filter system contains

more than

one

bank of filters in

series,

each

bank must be tested separately.

Section

9 of ANSI N510-1975,

"Air-Aerosol Mixing Uniformity Test,"

states

that it is to be performed once

upon completion of initial SGT

system installation,

and after modification or major repair.

It is not

required

each time an in-place test of the

HEPA filters or adsorbers

is

conducted.

The purpose of this test is to verify that tracer

(DOP

or'reon)

injection and sample points are located

so

as to provide .proper

mixing of the tracer in the air approaching

the

HEPA filter bank or

adsorber

stage.

The testing

done pursuant,to

Section

9 validates

the

injection and sample points which are to be used for all subsequent

bypass

leakage testing per Sections

10 and 12, so that the testing

performed pursuant to these

sections is meaningful

and representative.

The inspector

reviewed preoperational

test SLT-S39.0-5

and portions of

preoperational

test SLT-S39.0-4,

both conducted in 1983 (after initial

SGT system installation) to comply with Section

9 of ANSI N510-1975.

These preoperational

tests

did in fact'stablish

the injection and

sample points to be-used

in subsequent

bypass

leakage testing performed

per Sections

10 and

12 of ANSI N510-1975.

The inspector

noted that

an

injection manifold was used for injecting

DOP to challenge

the down-

stream

HEPA filter bank.

The 1983 preoperational

test confirmed that

..

this injection manifold ensured

a homogeneous

mixture of the

DOP and air

approaching

the

KEPA filters such that

a representative

upstream

sample

would be obtained.

In addition, the

1983 preoperational

testing of the

charcoal

beds validated tracer injection and sample locations for two

different test methods for testing the charcoal

units separately

or

0-

concurrently.

The validated

method for testing the charcoal

beds

sepa-

rately, which the licensee

had

done before the procedure

change dis-

cussed

above,

also required that manifolds

be used for tracer injection

and upstream

sampling

when testing the downstream

charcoal

bed.

Other-

wise, per SLT-S39.0-5,

the adsorber

beds

were to'be tested concurrently.

Licensee

personnel

responsible for testing

SGT were questioned

about the

use of the injection and sampling manifolds and, to their knowledge,

they had never

been

used.

Failure to use the injection manifolds for

testing the downstream

HEPA filter bank,

and the injection and sampling

manifolds for testing the downstream

charcoal

bed, is

a violation of TS Section 4.6.5.3.b.

1 (Violation 397/91-04-01).

The licensee

appears

to

have .corrected

the portion of this violation which pertains to the

charcoal

beds

by making the procedure

change

discussed

above.

However,

this change

appears

to have

been

made

because

acceptable

test results

could not be obtained

when the beds

were tested

separately,

not because

the licensee

was aware that the previous test method

was in violation of

the requirements.

The portion of this issue involving the charcoal

beds

is therefore not considered

to be

a licensee-identified violation.

On February

1 at 9:00 p.m., after the inspector

noted that the procedure

for testing the downstream

HEPA filter was incorrect, the licensee

entered

TS 4.0.3, which allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to successfully

complete

a sur-

veillance test that has not been

performed

as required.

The licensee

attempted

to validate the injection method that had been

used for test-

ing the downstream

HEPA filters by conducting

a test per Section

9 of

ANSI N510-1975.

The results failed the acceptance

criteria.

They were

finally able to successfully test the downstream

HEPA filter bank by

removing the upstream

HEPA filters and using its previously established

injection and sample points.

The upstr

am bank was then tested after

reinstallation.

TS 4.0.3

was exited at about 12:00 p.m.

on February 2.

Additional concerns

expressed

to the licensee

included:

PPN 7.4.6.5.3.5,

"SGT System

HEPA DOP Test

and Visual Inspection,"

did not indicate, specifically where injection and sample ports were

located.

Sample

and injection ports

on the filtration units themselves

were

only identified by writing in black marker pen.

There was incon-

sistency in the labeling for injection and sample points between

the "A" and "B" trains, especially

where the downstream

HEPA

filters were concerned.

Conversations

with licensee

personnel

responsible for SGT testing indicated that for the downstream

HEPA

filters the intended injection point was in doubt.

Confusion existed

as to,whether the

1975 or 1980 version of ANSI

N510 applied for bypass

leakage testing of SGT or other safety

related filtration systems.

Some differences exist between

the two

which may be significant,

and Regulatory Positions

C.5.c

and C.5.d

of Regulatory Guide 1.52 specifically endorse

the

1975 version.

The licensee

has

committed to the

1980 version in the

FSAR.

This

issue

was resolved

in subsequent

discussions

with cognizant

licensee

personnel.

4

The licensee

issued

a

PER to document

and resolve the

SGT testing

deficiency.

A Level I root cause

evaluation

was initiated to determine

why the original preoperational

tests

had not been followed.

Licensee

Event Report

(LER)91-003,

issued after the

end of the inspection

period, also discussed

this issue.

One violation was identified,

as discussed

above.

4.

Previousl

Identified

NRC Ins ection Items

92701,

92702

The inspectors

reviewed records,

interviewed personnel,

and inspected

plant hardware relative to licensee

actions

on previously identified

inspection findings:

a.

Closed

Part

21

Re ort 90-03-P - Potential

Problem with Rockbestos

Ca

es w>t

KS-500 Insu at>on

Rockbestos,

a vendor of electrical

cable,

submitted

a Part

21

report to the

NRC concerning

a discrepancy

in Rockbestos

cable with

certain silicon rubber insulation.

This insulation

was designated

KS-500.

The discrepancy

involved the use of the wrong activation

energy in the calculation for its equipment qualification.

Use of

the wrong activation energy would adversely

impact the environ-

mental qualification of the cable.

A copy of the Part

21 report

was sent to each licensee to which this type of cable

had been

supplied, including the Supply System.

After a search of records,

the licensee

determined that the cable

originally bought under the purchase

order referenced

by Rockbestos

had been received at the WNP-3/5. projects.

No cable

had

been

transferred

from either

WNP-3 or WNP-5 to WNP-2.

In addition,

no

procurement history for this type of cable

was found for WNP-2,

indicating that that

no cable of this type had

been

purchased

from

Rockbestos for use at WNP-2.

Further, it was determined that the

cable received

by WNP-3 had

been sold to a contractor for

non-nuclear

use.

This item is closed.

b.

Closed

Followu

Item 397/90-28-02 - Drawin

Revision Not Issued

for Cross-connected

Contro

Room

nstrument

Power

Su

ses

A deficiency was discovered

by the licensee

in October

1990 involv-

ing 24

VDC power supplies for certain control

room instrumentation.

Class

lE power supplies

had effectively been cross-connected

with

non-Class

lE power supplies,

rendering safety related instruments

susceptible

to faults

on non-safety related

power supplies.

This

was the result of a design

change that had

been

implemented

in 1983

by a Burns

and

Roe engineer.

The applicable drawing had not been

updated to reflect the design

change that had implemented this

wiring error.

The inspector left this item open to determine if

this was

a generic

problem.

In response,

the licensee

reviewed several

design

changes

imple-

mented during the

1983 time frame.

All had correctly updated

design

documents with the exception of the one discussed

above.

Thus, it appeared that the problem was

an isolated

one,

and that

the design engineer at the time had neglected

to modify the panel

connection

diagram

as required to reflect the as-built

configuration.

This item is closed.

co

(Closed

Followu

Item 397/90-31-03 - Weaknesses

in Im lementation

of Co d Weather

Pre aratsons

Several

weaknesses

were identified with regard to implementation of

the cold weather preparation

program.

They were corrected

as

follows:

+

One circuit on the heat trace

panel in the Condensate

Storage

Tank

(CST) pit area

had

a low temperature

alarm,

even though

the ambient temperature

was

above the alarm point of 35

degrees

at the time.

Operations

submitted

an

MWR and the

problem was corrected.

The procedure for cold weather operations,

PPM 1.3.37, stated,

"Ensure there is no debris in the

CST pit area that could plug

the drain and flood."

However, several

inches of water were

observed in the

CST pit area, indicating that the drain was

indeed plugged,

and appeared

to hamper efforts to check the

heat trace

panel in the area.

Per the Assistant Operations

Manager,

the normal drain system for the

CST pit has never

been

used

because

the radiation monitor originally installed

in the drain piping was-inadequate

for the application.

Therefore,

the

CST pit has

always

been

pumped to the turbine

building sump via a temporary

pumping arrangement,

making the

process

a difficult one."

The Assistant Operations

Manager

stated that the

CST pit will be

pumped out when the water gets

one inch deep or greater,

and

PPM 1.3.37 will be revised to

reflect this.

Various heat trace panels

were being checked

once

a day by

equipment operators

even though

PPM 1.3.37 stated that these

panels

should

be checked

by each shift when they are in

service during cold weather.

The Assistant Operations

Manager

stated that the equipment operator log sheets

would be changed

to require that heat trace

panels

be checked

each shift for

continuity and low temperatures.

This item is closed.

d.

Closed)

Followu

Item 397/BS-32-01 - Discre ancies/Concerns

e ar

sn

W

o

s

scat>ons

The inspector

had reviewed the licensee's

implementation of the

Anticipated Transient Without Scram

(ATWS) rule,

10 CFR 50.62,

and

l

had determined that followup inspection

was necessary

to resolve

certain aspects

that were incomplete at the time of the inspection.

These aspects,

and their resolutions,

are itemized below:

Some operators

had not been

aware of the manual

reset charac-

teristic of the alternate

rod insertion

(ARI) system,

or of

the minimum required time to reset.

The inspector interviewed

a number of licensed

operators,

and found that they were fami-

liar with the manual reset function of ARI and were aware that

there

was

a minimum time to wait before attempting to reset.

In addition, this minimum time to reset

(45 seconds)

had

been

incorporated into the applicable

emergency

operating

procedure

that th'e control

room operators

follow when responding to an

ATWS event.

At the time of the previous inspection,

ARI modifications

had

not been

added to the simulator.

The inspector verified that

ARI modifications installed in the plant had

been

added to the

simulator.

The licensee's

ATWS Criteria Design Implementation

Review

document

had identified certain

commitments

associated

with

ATWS implementation that were not complete.

The inspector

verified by reviewing applicable

documentation that all

18

issues

remaining

open at the time of the inspection in the

Design Implementation

Review Document

had subsequently

been

completed.

The logic scheme

used for the

ATWS recirculation

pump trip

(RPT)

had been

a one out of two taken

once for each recircu-

lation pump. This logic was different from the one out of two

taken twice scheme that had

been found acceptable

by the

NRC.

The licensee

subsequently

modified the

RPT logic to

a one out

of two taken twice for each recirculation

pump.

This item is considered

closed.

5.

0 erational

Safet

Verification

71707

93001

a ~

Plant Tours

The following plant areas

were toured

by the inspectors

during the

course of the inspection:

Reactor Building

Control

Room

Diesel

Generator Building

Radwaste

Building

Technical

Support Center

Turbine Generator Building

Yard Area and Perimeter

b.

The followin

items were observed

durin

the tours:"

(4)

(5)

(6)

(7)

(g)

0 eratin

Lo s

and Records.

Records

were reviewed against

ec naca

peer

icatson

an

administrative control procedure

requirements.

Nonitorin

Instrumentation.

Process

instruments

were observed

or corre at>on

etween

c annels

and for compliance with

Technical Specification requirements.

S~tif

N

i

.

C

1

d lif

i

9

b

d

for conformance with 10 CFR 50.54.(k), Technical Specifica-

tions,

and administrative

procedures.

The attentiveness

of

the operators

was observed

in the execution of their duties.

and the control

room was observed

to be free of distractions

such

as

non-work related

radios

and reading materials.

E ui ment Lineu s.

Valves

and electrical

breakers

were veri-

fie

to

e 1n t e position or condition required

by Technical

Specifications

and administrative

procedures

for the applic-

able plant mode..

This verification included routine control

board indication reviews

and conduct of partial

system

lineups.

Technical Specification limiting conditions for

operation

were verified by direct observation.

E ui ment Ta

in

.

Selected

equipment, for which tagging

requests

ha

been initiated, was observed

to verify that tags

were in place

and the equipment

was in the condition

specified.

General

Plant

E ui ment Conditions.

Plant equipment

was

o serve

for indicatsons

of system leakage,

improper lubrica-

tion, or other conditions that would prevent the system from

fulfillingits functional requirements.

Annunciators were

observed to ascertain their status

and operability.

Fire Protection.

Fire fighting equipment

and controls were

df

Ih dpi<on practices

to determine

whether the licensee's

program was being implemented in

conformance with facility policies

and procedures

and in

compliance with regulatory. requirements.

The inspectors

also

observed

compliance with Radiation

Work Permits,

proper

wearing of protective equipment

and personnel

monitoring

devices,

and personnel

frisking practices.

Radiation

monitoring equipment

was frequently monitored to verify

operability

and adherence

to calibration frequency.

4

II

(10) Plant Housekee

inc.

Plant conditions

and material/equipment

storage

were

o served to determine

the general

state of

cleanliness

and housekeeping.

Housekeeping

in the radio-

logically controlled area

was evaluated with respect to

controlling the spread

of surface

and airborne contamination.

(11) ~Securit

.

The inspectors

periodically observed

security

practices

to ascertain

that the licensee's

implementation of

the security plan was in accordance

with site procedures,

that

the search

equipment at the access

control points

was

operational,

that the vital area portals were kept locked

and

alarmed,

and that personnel

allowed'ccess

to the protected

area

were

badged

and monitored

and the monitoring equipment

was functional.

C.

( 12)

Occu ational Safet

.

Plant conditions which could result in

an occupationa

ris

, such

as exposure to toxic non-radio-

active materials,

were monitored

by the inspectors.

The

inspectors

periodically monitored for other such industrial

hazards

in the workplace.

Safet

S stem Malkdowns

Selected

engineered

safety features

(and systems

important to

safety)

were walked

down by the inspector to confirm that the

systems

were aligned in accordance

with plant procedures.

During

the walkdown of the systems,

items

such

as lub} ication of major

components

and cooling water/ventilation were inspected

to deter-

mine that they were operable

and in a condition to perform their

required functions.

The inspectors

also verified that system

valves were in the required position by both local

and remote

position indication,

as applicable.

Accessible portions of the following systems

were walked down on

the indicated dates.

~Sstem

Dates

Scram Discharge

Volume System

125V

DC Electrical Distribution,

Divisions

1 and

2

February

4

January

30

250V

DC Electri ca 1 Distributi on

No violations or deviations

were identified.

January

30

6.

Survei 1 l ance

Tes tin

61726

a.

Surveillance tests

required to be performed

by the Technical

Specifications

(TS) were reviewed

on

a sampling basis to verify

that:

( 1)

a technically adequate

procedure

existed for performance

of the surveillance tests;

(2) the surveillance tests

had

been

performed at the frequency specified in the TS and in accordance

with the

TS surveillance

requirements;

and (3) test results

satisfied

acceptance

criteria or were properly dispositioned.

Portions of the following surveillance tests

were observed

by the

inspectors

on the dates

shown:

Procedure

Descri tion

Dates

Performed

7.4.8.1.1.2.1

Nonthly Operability of

Emergency Diesel Generators

(EDGs)

January

15

7.4.6.5.3.6

7.4.3.6.23

Standby

Gas

Treatment'ystem

Adsorber Bypass

Leakage Test

'ecirculationFlow Channel

"B" Upscale

or Inoperable

Control

Rod Block

February

1

February

5

10. 2. 77TP

Reactor

Closed Cooling

(RCC)

February

6

Heat Exchanger

"B" Flush

Chemical

C1eaninq

While observing the conduct of the

EDG surveillance test

on January

15, the inspector noted the following:

Step

18 on page

16 of PPH 7.4.8.1.1.2.1

is

a prerequisite

step in

which the operator verifies that Standby Service Water

(SSW) flow

is 1650-1750 gallons per minute (gpm).

However, according to the

local gauge,

the flow rate of SSW was actually 1810

gpm, outside:

the required

band.

The operator

noted this discrepancy

and

reported the out of specification flow rate to the control room.

The operators

in the control, room replied that since the logs for

an operating diesel

generator

allowed

a wider control

band

(1400-2200

gpm), the

SSW flow was satisfactory.

The local operator

then signed off the prerequisite

step,

and the surveillance

continued

through completion.

The inspector questioned

why a procedure

change

was not initiated

prior to continuing with the surveillance in order to clearly

document

and rectify the discrepancy.

This would also allow an

improvement of the procedure

to make it more feasible the next time

it was worked.

Finally, since this was

a Technical Specification

required

surveillance test,

the inspector questioned

why a sound

technical justification was not provided for deviating from certain

steps of it.

During discussions

with the Assistant Operations

Hanager,

he stated

'hat

this problem had minimal safety significance

because

the

J

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0

higher flow rate was anticipated

by operations

personnel

and did

not affect

EDG operability.

The

SSW system

was also being operated

in the "splash

mode" (which bypasses

the spray

pond spray nozzles

during cold weather), resulting in less

back-pressure

in the

SSW

system,

and therefore

a higher flow rate in the system.

However,

the Assistant Operations

Manager stated that the procedure

would be

revised to allow for higher flow rates

when the

SSW system is

operated

in the above-mentioned

cold weather lineup.

No violations or deviations

were identified.

7.

Evaluation of the Licensee's

Self Assessment

Ca abilit

40500)

The inspector

conducted

interviews with several

personnel

associated

with the licensee's

oversight groups,

and reviewed Plant Operations

Committee

(POC) minutes,

the Operational

Experience

Assessment

(OEA)

group's monthly summaries

and recommendations,

and inspection reports

ir~ued by Technical

Ass"-ss.-.=-:.=.~s

~ a;.sonnel.

During this inspection,

the

inspector ascertained

that the licensee

appeared

to be in compliance

with the Technical Specifications

(TS) and appeared

to have strong

programs for these oversight groups.

Some'xamples

of the particular

~ "".>ngths are listed below:

POC is required

by the

TS to meet monthly to discuss plant

operations

and approve

Licensee

Event Reports

(LERs), replies to

Notices of Violations

(NOYs), changes

to the TS,

and other items.

Pi7i actually meets at least weekly,

and sometimes

even more often,

which keeps

POC closely involved with plant operations.

OEA reviews events from other utilities,

INPO reports,

Generic

Letters

and other items in the nuclear industry to determine if

action needs to be taken at

WNP-2 to prevent similar occurrences

or

correct similar problems.

The inspector

noted several

examples of

significant recommendations

that kept the licensee

ahead of

potential

problems.

For example, at the Grand Gulf nuclear

power

plant, the licensee lost control of a fuel bundle during refueling

due to problems with certain refueling bridge equipment.

The

OEA

at WNP-2 recommended

that the refueling equipment at WNP-2 be

checked for similar problems prior to use.

Upon inspection,

some

of the problems

noted with the'rand

Gulf refueling equipment were

noted at WNP-2 also.

Thus, the licensee

took timely action to

correct these

problems before they became

more significant.

Technical

Assessments

performs inspections

similar to the

NRC and

INPO.

Technical

Assessments

has

some experienced

personnel

(including former operators)

who are highly knowledgeable

in the

areas

they inspect.

A Safety System Functional

Inspection

(SSFI)

of the

SSW system,

performed recently

by the group,

made approxi-

mately

70 observations

and was generally of high quality.

In

addition, Technical

Assessments

issued

an Outage Modification

Inspection'hat identified several significant issues.

No violations or deviations

were identified.

0

,

I

Plant Maintenance

(62703

During the inspection period, the inspector

observed

and reviewed

documentation

associated

with maintenance

and problem investigation

activities to verify compliance with regulatory requirements

and with

administrative

and maintenance

procedures,'equired

gA/l}C involvement,

proper use of clearance

tags,

proper equipment alignment

and use of

jumpers,

personnel

qualifications,

and proper retesting.

The inspector

verified that reportability for these activities was correct.

The inspector witnessed

portions of the following maintenance

activities:

~D

Investigation of oil leak from

Division I

EDG per AR 2330.

Recalibrate

(Diesel Mixed Air)

DMA-TIS-ll/1 per

AR 2248

Replace

rubber rollers

on south fuel

preparation

machine per

AR 1413

Dates

Performed.

January

14

January

14

February

1

No violations or deviations

were identified.

Licensee

Event

Re ort (LER

Followu

90712

92700

The following LER associated

with an operating

event

was reviewed

by the

inspector.

Based

on the,information provided in the report it was

concluded that reporting requirements'had

been met, root causes

had

been

identified, and corrective actions

were appropriate.

The below LER is

considered

closed.

LER

NUMBER

91-01

DESCRIPTION

RCIC-V-8 ESF Actuation

Due to Failed Electronic

Component in Leakage Detection System

No violations or deviations

were identified.

Review of Periodic

and

S ecial

Re orts

90713

Periodic

and special

reports

submitted

by the licensee

pursuant to

Technical Specifications 6.9.1

and 6.9.2 were reviewed

by the inspector.

This review included the following considerations:

the report contained

the information required to be reported

by NRC requirements,

and the

reported

information appeared

valid.

Within the scope of the above,

the

following report was reviewed

by the inspector.

Monthly Operating

Report "for December,

1990.

No violations or deviations

were identified.

12

11.

Exit Meetin

30703

The inspector

met with licensee

management

representatives

periodically

during the report period to discuss

inspection status,

and

an exit meet-

ing was conducted with the indicated personnel

(refer to paragraph

1)

on

February

19,

1991.

The scope of the inspection

and the inspector's

findings,

as, noted in this report, were discussed

with and acknowledged

by the licensee

representatives.

I

The licensee did not identify as proprietary any of the information

reviewed by or discussed

with the inspector during the inspection.

e

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