ML17263A981
| ML17263A981 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 03/06/1995 |
| From: | Mecredy R ROCHESTER GAS & ELECTRIC CORP. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| Shared Package | |
| ML17263A982 | List: |
| References | |
| NUDOCS 9503160234 | |
| Download: ML17263A981 (2) | |
Text
P RIC)RIWY (ACCELERATED RIDS PROCESSING)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9503160234 DOC.DATE: 95/03/06 NOTARIZED: NO DOCKET N
FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G
05000244 AUTH.NAME AUTHOR AFFILIATION MECREDY,R.C.
Rochester Gas
& Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Forwards LER 95-001 re pressurizer safety valves lift
.settings found above TS tolerance during post-svc test,due to setpoint shifts.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTRI ENCL SIZE'-
TITLE: 50.73/50.9 Licensee Event Report (LER),&nciden Rpt, etc.
F NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244 F
RECIPIENT ID CODE/NAME PD1-3 PD INTERNAL: AEOD/SPD/RAB
~FILE CEHTER+02 NRR/DE/EELB NRR/DISP/PI PB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DSSA/SPLB RES/DSIR/EIB EXTERNAL: L ST LOBBY HARD NOAC MURPHY,G.A NRC PDR COPIES'TTR ENCL 1
1 1
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RECIPIENT ID CODE/NAME JOHNSON,A AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DOPS/OECB NRR/DRCH/HICB NRR/DRSS/PRPB NRR/DSSA/SRXB RGN1 FILE 01 LITCO BRYCE,J H
NOAC POORE,H.
NUDOCS FULL TXT COPIES LTTR ENCL 1
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1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE O'ASTE! CONTACTTHE DOC!:LIESTCONTROL DESK. ROOWI PI.37 (EVE 504-2083 ) TO E LIMNI!
iATE YOI.'R FAME F ROTI DISTRIBUTIONLISTS I'OR DOCL'RIED'I'S YOL'Oi "I'L'ED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: 'LTTR 26 ENCL 26
1ND ROCHESTER GAS ANDElE'CTRIC CORPORATION
~ 89 FASTAtrENUE, ROCHESTER, N, Y Id6d9 0001 AREA CODE 716 $66.2700 ROBERT C. IrtECREDY Vice President Hucteor Operotions March 6, 1995 U.S. Nuclear Regulatory Commission Document Control Desk Attn:
Allen R. Johnson PWR Project Directorate I-3 Washington, D.C. 20555
Subject:
LER 95-001, Pressurizer Safety Valves Lift Settings Found Above Technical Specifications Tolerance During Post-service Test, Due to Setpoint Shifts, Results in Independent Trains Being Considered Inoperable R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (vii) (D), which requires a report of, "any event where a single cause or condition caused at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a single system designed to... mitigate the consequences of an accident", the. attached Licensee Event Report LER 95-001 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecredy xc:
U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9503i60234 950306 PDR ADOCK 05000244 S