ML17263A648

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Monthly Operating Rept for Apr 1994 for Re Ginna Nuclear Power Plant
ML17263A648
Person / Time
Site: Ginna 
Issue date: 04/30/1994
From: Ploof R, Widay J
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9405190105
Download: ML17263A648 (9)


Text

ACCELERATED DI~~BUTION DEMONSTRATION SYSTEM

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Cl REGULATORY INFORMATION DISTRIBUTXON SYSTEM (RIDS)

ACCESSION NBR:9405190105 DOC.DATE: 94/04/30 NOTARIZED:

NO FACIL:50-244 Robert Emmet. Ginna Nuclear Plant, Unit 1, Rochester G

AUTH.NAME AUTHOR AFFILIATION PLOOF,R.D.

Rochester Gas 6 Electric Corp.

'IDAY,J.A.

Rochester Gas

!l: Electric Corp.

RECXP.NAME RECIPIENT AFFILIATXON DOCKET 05000244

SUBJECT:

Monthly operating rept for Apr 1994 for RE Ginna Nuclear Power Plant.W/940510 ltr.

DISTRIBUTION CODE:

IE24D COPIES RECEIVED:LTR ENCL SIZE:

TXTLE: Monthly Operating Report (per Tech Specs)

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).

05000244 D

RECIPIENT XD CODE/NAME PD1-3 PD INTERNAL: AEOD/DOA R+B~Qjy~AB REG FILE 01 EXTERNAL EGS(G BRYCE g J H

NSIC COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME JOHNSON,A AEOD/DSP/TPAB NRR/DRIL/RPEB RGN1 NRC PDR COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 D

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NOTE TO ALL"RIDS" RECIPIENTS:

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PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAMEFROM DISTRIBUTION LIKES FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 11 ENCL 11

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jijijj(si/lirrrr ROCHESTER GASANDELECTRICCORPORATION o 89EASTA VENUE, ROCHESTER, N.Y. 14649%001 JOSEPH A. WIDAY Plant Manager Ginna Nuclear Plant TELEPHONE AREA CODE 7 I6 546-2700 GINNA STATION May 10, 1994 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

Monthly Report for April, 1994 Operating Status Information R.

E. Ginna Nuclear Power Plant Docket No.

50-244

Dear Sir:

Pursuant to our Technical Specification 6.9.1, attached herewith is the monthly operating status report for Ginna Station for the month of April, 1994.

Very truly yours,

a. 9 se h A. Wida Plant Manager JAW:tjn Attachments c:

Mr. Thomas T. Martin NRC (1)

Q ElgQQ O q405i~0>

K 05000244 05 rtt40450 eDR nOOCX R

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DOCKET N 50-244 DATE May 11, 1994 COMPLETED BY Ronald D. Ploof TELEPHON (315) 524-4446 Ext.67 E

GST TUS 1.

Unit N R.E. GINNA NUCLEAR POWER PLANT Notes:

2.

Reporting Period April, 1994 3.

Licensed Thermal Power (MWt):

1520 4.

Nameplate Rating (Gross MWo):

490 5.

Design Electric Rating (Net MWo):

470 6.

Maximum Dependable Capacity (Gr 490 7.

Maximum Dependable Capacity (Ne 470 8.

If Changes Occur in Capacity Rating (Items Number 3 Through 7) Since Last Report, Give Reason:

9.

Power Lovel to Which Restricted, If Any (Not MWe):

10. Reason For Restrictions, If Any:

This Month Yr.-to-Date Cumulative' 11.

Hours in Reported Period 12.

Number of hours Reactor Was Critical 13.

Reactor Reserve Shutdown Hours 14.

Hours Generator On-line 15.

Unit Reserve Shutdown Hours 16.

Gross Thermal Energy Generated (MWH) 17.

Gross Electrical Energy Generated (MWH) 18.

Not Electrical Energy Generated (MWH) 19.

Unit Service Factor (%)

20. Unit Availability Factor (%)
21. Unit Capacity Factor (using MDC Not) (%)
22. Unit Capacity Factor (using DER Net) (%)

23 Unit Forced Outage Rate (%)

720.0 301.2 0.0 247.4 0.0 283107.0 94581.0 88952.0 34.4 34.4 26.3 26.3 6.2 2855.9 1800.5 0.0 1910.8 0.0 2486791.0 844651.0 801386.0 66.9 66.9 59.7 59.7 2.3 214103.9 170326.9 1688.0

+

167662.8 8.5

'37442804.0 78528010.0 74536759.0 78.3 78.3 75.2 75.2 5.6 24.

Shutdowns Scheduled Over Next 6 Months (Typo, Date and Duration of Each):

25. If Shutdown At End of Report Period, Estimate Dato of Startup:

26.

Units in Test Status (Prior to Commercial Operation):

Forcast Achiovod INITIALCRITICALITY INITIALELECTRICITY COMMERCIALOPERATION

'UMULATIVETOTALCOMMENCING JANUARY 1, 1975

" CUMULATIVETOTALCOMMENCING NOVEMBER 8, 1969

AVERAGE DAILYUNIT POWER LEVEL DOCKET NO: 50-244 UNIT: R.E.

Ginna Nuclear Power Plant DAT Ma 1

1994 COMPLETED BY:

Ronald Plo f TELEPHONE:

315 524-4446 Ext.

673 MONTH A ril 1994 DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 17.

2.

18.

19.

168 20.

309 5.

21.

429 6.

22.

462 7.

23.

480 8

~

24.

482 9

~

25.

482 10'6.

132 27.

12.

28.

13.

29.

194 14.

30.

479 15'1.

16.

INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in reporting month.

Compute to the nearest whole megawatt.

"I

REPORT hlONTH 4

DO(:KET NO.

I/Nll'NAMl:.R.E. GINNA NUCLEAR POWER PlANT UNIT SHUTDOWN AND POWER REDUCTIONS

(.OhfPLI(1 I'.D BY Rona% KGB 1

1'f:.f fipfI()NI:.315-524-4446 X673 t

J Ho.

Date 0

I r.o e o o oX O~

C0 a0 I

~ o8 ac vt o tt'V7 C

X 0

Cl Licensee Event Report tf Em 0

0 Ill o IA C0 LA a0 Q

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Cause 5 Corrective Action to Prevent Recurrence 94'-04 94-05 4-26-94 4-27-94 F

15.6 B

11.5 A

94-008 JB Steam leak on HP Turbine instrument fitting~longer fitting installed.

Main feedwater regulating valve failed to move.

Replaced positioner=

style.

F:

Forced S:

Scheduled stv. 4%$

4949 Reason:

A-Equipment Failure (Explain) 8-hfaintcnance or Test C-Refueling D-Regulatory Restriction E-Operator Training Bt License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain) 3 hlcthod:

I-hlanual 2-hlanual Scratn.

3-Automatic Scram.

4-Other (Explain)

Fxhibit G - Instructions for Preparation of Data Entry Shccts for Liccnscc Event Rcport (LER) File (NURE(-

016I)

Exhibit I - Same Source

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO: 50-244 UNIT: R.E.

Ginna Nuclear Power Plant DATE: Ma 10 1994 COMPLETED BY:

Ronald Ploof TELEPHONE:

315 524-4446 Ext.

673 MONTH A ril 1994 The unit came on-line on 4/18/94 from its annual maintenance and refueling outage and returned to full power on 4/23/94.

On 4/26/94, the unit shutdown

.to repair a

small instrument line steam leak on the HP turbine.

The unit was placed back on-line on 4/27/94.

At approximately 40%

power, the unit tripped off-line on 4/27/94 on its way to full power due to low S/G level caused by a faulty main feedwater regulatory valve.

The unit was placed back on-line on 4/28/94 and returned to full power on 4/30/94.

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