ML17263A547
| ML17263A547 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 03/03/1994 |
| From: | Lazarus W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17263A548 | List: |
| References | |
| 50-244-94-01, 50-244-94-1, NUDOCS 9403150008 | |
| Download: ML17263A547 (19) | |
See also: IR 05000244/1994001
Text
U. S. NUCLEAR REGULATORYCOMMISSION
REGION I
Inspection Report 50-244/94-01
License: DPR-1S
Facility:
R. E. Ginna Nuclear Power Plant
Rochester Gas and Electric Corporation (RG&E)
Inspection:
Inspectors:
January
1 through February 7, 1994
T. A. Moslak, Senior Resident Inspector, Ginna
E. C. Knutson, Resident Inspector, Ginna
Approved by:
hief, Reactor Projects Section 3B
INSPECTION SCOPE
Date
I
Plant operations,
maintenance,
engineering,
safety assessment/quality
verification, and plant
support,
9403i50008
9'40304
FDR
ADOCV. 0S000aee
8
Operations
EXECUTIVE SUMVIARY
Lake water intake structure icing twice forced 50 percent power reductions during a two day
period in January.
In both cases, prompt action to secure a circulating water pump prevented
reduced screenhouse
water level from affecting service water pump operability. The apparent
cause was reduced intake structure heater efficiency due to zebra mussel infestation, coupled
with record-low temperatures.
Corrective action to double the heater supply voltage has been
effective. Throughout this event, the operations staff demonstrated strong attention-to-detail and
strict adherence to procedures.
Strong management involvement, site and corporate engineering
support, quality assurance
oversight, and trade support were evident.
However, the control of
emergency maintenance, particularly requirements for PORC review, could be better delineated
in the governing procedure.
Maintenance
Two containment pressure instruments were discovered to have been inoperable since June 1992
due to blockage of the common sensing line that connects the associated
pressure transmitters
with containment.
Licensee review of this event is in progress.
Trial-basis
implementation of voluntary entry into limiting condition for operation
action
statements for the purpose of conducting preventive maintenance was examined.
The need for
such
maintenance
was
carefully
evaluated
by
the
licensee,
with justification
based
on
probabilistic risk analysis results.
The licensee implemented effective operational controls over
such maintenance.
During work on the "B" motor driven auxiliary feedwater pump, the large
number of maintenance
tasks to be accomplished,
along with the limited space at the work site,
resulted in some inefficiency due to congestion.
1
Plant Support
No deficiencies were noted in review of the licensee's
implementation of revised
requirements.
Safety Assessment/Quality
Verification
During this period, the licensee submitted Licensee Event Report (LER) Nos.93-006 and 93-
007.
These LERs were accurate,
met regulatory requirements,
and appropriately identified the
root cause.
TABLEOF CONTFWTS
EXECUTIVESQtlMARY
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1.0
OPERATIONS (71707)
1.1
Operational Experiences
1.2
Control of
Operations................................'.3
Power Reductions Required Due To Lake Water Intake Structure Icing
1.4
Licensee Action on Previous Inspection Findings ...............
1.4.1
(Closed)
Inspector
Follow
Item
(50-244/93-17-01)
Modify
Emergency Operating Procedure E-0 to Direct Manual Actuation
of Safety In~ection
1.4.2
(Closed)
Inspection
Follow Item
(50-244/93-17-02)
Enhance
Emergency Contingency Actions (ECA) Procedure ECA-0.0
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2.0
MAINTENANCE(62703, 61726)... ~...................
2.1
Preventive/Corrective Maintenance........ ~.....
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2.1.1
Routine Observations............,........
2.1.2
Containment
Pressure
Transmitters
Found Inoperable
Plugged Sensing Line
2.1.3
Voluntary
Entry
into LCO Action
Statements
to
Preventive Maintenance ...................
2.2
Surveillance Observations
2.2.1
Routine Observations..............
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3.0
PLANT SUPPORT (71707)
3.1
Radiological Controls...... ~.............
3.1.1
Routine Observations.......,........
3.1.2
Implementation of the Revisions to 10 CFR 20
3 ~2
Security
'3.2.1
Routine Observations..........,.....
3.3
Fire Protection ........................
3.3.1
Routine Observations .;..............
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4.0
SAFETY ASSESSMENT/QUALITY VERIFICATION
4.1
Periodic Reports .......;...........
4.2
. Licensee Event Reports...............
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5.0
ADMINISTRATIVE(71707, 30702, 94600)
5.1
Deep Backshift Inspection
5.2
Exit Meetings...... ~..............
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DETAILS
1.0
OPERATIONS (71707)
1.1
Operational Experiences
During normal power operations on the early morning ofJanuary 20, 1994, a decreasing
screen
house water level was identified. This condition indicated that the flow through the intake, canal
was not sufficient to support the service and circulating water flowdemand.
Actions were taken
to reduce this demand by reducing plant power and securing one of the two main condenser
circulating water pumps.
Additionally, the intake structure heater bar voltage supply w'as
increased
from 240 to 480 volts to-Muce frazil ice formation on the intake grating.
Subsequently,
normal screenhouse
water level was restored.
During the early morning hours
of the following day, the icing condition reappeared
and actions were successfully
taken to
restore water level by reducing power and again temporarily securing a circulating water pump.
Power was then escalated
and remained at 98 percent through the remainder of the inspection
period.
1.2
Control of Operations
Overall, the inspectors
found the R. E. Ginna Nuclear Power plant to be operated
safely.
Control room staffing was as required.
Operators exercised control over access to the'control
room.
Shift supervisors
maintained authority over activities and provided detailed turnover
briefings to relief crews.
Operators adhered to approved procedures
and were knowledgeable
of off-normal plant conditions.
The inspectors reviewed control room log books for activities
and trends,
observed
recorder
traces for abnormalities,
assessed
compliance with technical
specifications,
and verified equipment availability was consistent with the requirements
for
existing plant conditions.
During normal work hours and on backshifts, accessible
areas of the
plant were toured.
No operational inadequacies or concerns were identified.
1.3
Power Reductions Required Due To Lake Water Intake Structure Icing
Lake Ontario is the normal source of cooling water for the Ginna plant.
Cooling for operation
of the turbines that drive the main generator is provided by the circulating water system, while
the reactor plant and auxiliary systems are cooled by the service water system.
Both of these
cooling water systems draw suction from a common inlet bay in the screenhouse.
Lake water
is supplied to the inlet bay through an underground pipe that opens to a shielded intake structure,
located 3100 feet off shore;
On January 20, 1994, at 2:35 a.m., operators were alerted to slowly lowering water level in the
screenhouse
lake water inlet bay when level instrument channel LI-3007 alarmed on low level
(240 inches, or 20 feet; normal screenhouse
level is about 28 feet). The traveling screens {four
sets of vertically mounted, segmented
screen tracks that provide coarse filtration between the
inlet bay and the pump suctions) were inspected and found to be clean and free of ice.
Power
to the four groups of intake
structure
heaters
was
checked
and
found
to be normal
(approximately 40 amps per group). In light ofthe existing record low temperatures,
operators
suspected
that ice was forming on the lake intake structure bars and thus restricting fiow.
2
At 4: 14 a.m., in response to main control board alarm I-1, "Screen House Lo Level 17 Feet,"
operators commenced
a plant power reduction in accordance with site contingency procedure
(SC)-4.1, "Low Screenhouse.Water
Level."
In parallel with the power reduction,
plant
management
authorized alteration of the intake'heater
power supplies to increase
the supply
voltage from 240 volts to 480 volts; this action would increase the amperage of these heaters by
a factor of four.
The work was performed as emergency
maintenance,
as provided for by
administrative procedure (A)-1603, "Work Order Initiation." Three of the four intake heaters
were converted to 480 volts; the "C" intake heater was left connected to the 240 volt source
because
resistance
readings
were found to be lower than the other heaters,
indicating that
operation at higher voltage may'result in premature failure.
During the power reduction, a problem was noted with the screenhouse
water level indications.
Two independent instruments provide indication of screenhouse
water level; LI-3006 provides
- indication and annunciators on the main control board (MCB), and LI-3007 provides indication
via the primary plant computer system (PPCS).
Operators noted that the levels indicated by
these two instruments were diverging as screenhouse
water level was lowering.
To provide
reliable data, opeiations management
directed that screenhouse
water level be determined by
direct measurement,
using a weighted tape measure.
0
When power had been reduced to 50 percent, one of the two main circulating water pumps was
secured.
The resultant reduction in flow out of the water inlet bay had the prompt effect of
increasing level by approximately five feet. The increased voltage to the intake structure heaters
was also proving effective, with ice and zebra mussels being observed collecting in the traveling
screens.
By 8:40 a.m.,
normal screenhouse
water level had been
restored.
To resolve
discrepancies between PPCS and MCB level indications, calibration checks were performed, and
both instruments were found to be within acceptable
tolerances,
The instrument sensing lines
were blown down with air to eliminate any possible sources of blockage.
Following this action,
the level instruments indicated in close agreement.
The Plant Operations
Review Committee (PORC) subsequently
reviewed the divergent level
indications with respect to the requirements of emergency plan implementing procedure (EPIP)
1-0, "Ginna Station Event Evaluation and Classification."
EPIP 1-0 stipulates that a site area
emergency be declared if, "Screenhouse Intake Water Level is less than or equal to the 15'o
Level Alarm (1-9)." The lowest screenhouse
water level reached'prior to securing the circulating
water pump was approximately 15.5 feet; the fact that MCB annunciator I-9, "Screen House Lo-
Lo Level, 15 Feet," never alarmed indicates that the LI-3006 level never fell below 15 feet.
PORC concluded that EPIP 1-0 was overly conservative in declaring a site area emergency based
solely on low screenhouse
water level. This conclusion was based on recent industry guidance
on emergency
action level (EAL) determinations,
as well as on technical evaluation of the
minimum water level required for service water pump operability.
As written, the technical.
basis for declaring a site area emergency
at a screenhouse
water level of 15 feet was the
potential for loss of heat sink due to lowering lake level.
Preceding EAL determinations
(unusual event and alert) in EPIP 1-0 were based on progressively lower lake levels; however,
the criteria changed
from lake level to screenhouse
level for determination of a site area
emergency.
Consequently,
the procedure did not accurately account for low screenhouse
water
level, when it was not the result of correspondingly low lake level (as in the case of intake
structure icing).
At 12:02 p.m. on January 20, 1994, the plant commenced power escalation, and by 6:10 p.m.,
had returned to fullpower operation.
However, at 10:51 p.m., operators noted that screenhouse
water level was again slowly trending downward.
Plant power was again reduced to just below
50 percent and, at 9:27 a.m. on January 21, 1994, a main circulating water pump was secured.
This action was successful in restoring and stabilizing screenhouse water level. Again, quantities
of'ice and zebra mussels
were noted in the traveling screens
following the pump shutdown.
Later that day, full power operation was again restored,
with no subsequent
difficulties in
maintaining screenhouse
level.
From these observations,
the inspector concluded that the cause of these two instances of low
screenhouse water level was frazil ice formation on the intake structure bars. This ice formation
was the result of extreme winter conditions, along with reduced heater bar efficiency due to
zebra mussel infestation.
Higher intake structure temperature due to operation of the heaters at
480 volts appeared
to reduce the zebra
mussel infestation; this, along with more moderate
weather, restored the capability of the intake structure heater bars to retard ice formation.
The inspector assessed
the licensee's overall response to this event to have been good.
Strong
management involvement, site and corporate engineering support, quality assurance
oversight,
and trade support were evident throughout the event.
The inspector considered that control of
emergency maintenance, particularly requirements for PORC review, could be better delineated
in the governing procedure.
Additionally, the inspector considered that the licensee should have
recognized and expeditiously resolved the apparent disparity in EPIP 1-0 (that is, entry into a
site area emergency without having transitioned through an unusual event and alert), given the
relatively slow development of the event.
Throughout this event,
the operations staff demonstrated
strong attention-to-detail and strict
adherence
to procedures,
from the initial indications of decreasing
screenhouse
water level,
through responding to challenging operational concerns of electrical grid stability, condensate
depression,
elevated
circulating water discharge
temperatures,
and plant power reductions/
escalations.
The operators
demonstrated
an excellent understanding of their procedures
and
further enhanced
these procedures by capturing information gained through experiences during
this infrequent occurrence of water intake structure icing.
To gain additional insight on icing events,
the RG&E engineering
staff has
invited a
representative from the James A. Fitzpatrick Plant to discuss the lessons learned from the three
icing incidents that occurred there in 1993.
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1.4
Licensee Action on Previous Inspection Findings
1.4.1
(Closed) Inspector Follow Item'(50-244/93-17-01) Modify Emergency
Operating
Procedure E-0 to Direct. Manual Actuation of Safety Injection
On January
26,
1994,
the PORC
approved
procedure
change
notice (PCN) 93-3757
to
emergency
operating
procedure
E-O,
"Reactor Trip or Safety Injection," that modified
procedural step 4 by directing the operator to manually actuate safety injection (SI) ifrequired
by an annunciated alarm.
Although this procedure previously accomplished the desired system
alignment, PORC concluded that manually actuating SI was more expeditious and reliable than
having the operator initiallyperform individual component manipulations.
Through attendance at the PORC meeting, review of supporting documentation,
and discussion
with licensee representatives,
the inspector determined that the licensee appropriately responded
to the finding and had no additional questions on this matter.
1.4.2
(Closed) Inspection Follow Item (50-244/93-17-02) Enhance Emergency Contingency
Actions (ECA) Procedure ECA-0.0
On January 26, 1994, PORC approved PCN 93-3756 and PCN 93-3837, to ECA 0.0, "Loss of
AllAC Power," and emergency restoration (ER) procedure ER-D/G.2, "Alternate Cooling for
respectively.
These changes
enhance
operator guidance for
energizing buses
17 and 18 and starting service water pumps to provide EDG cooling following
a complete loss of offsite power.
Should use of normal service water be precluded, operators
are directed to ER-D/G.2 for alternative measures.
Through attendance at the PORC meeting, review of supporting documentation, and discussion
with licensee representatives,
the inspector determined that the licensee appropriately responded
to the finding and had no additional questions on this matter.
2.0
MAINTENANCE(62703, 61726)
2.1
Preventive/Corrective Maintenance
2.1.1
Routine Observations
The inspector observed portions of maintenance activities to verify that correct parts and tools
were utilized, applicable industry code and technical specification requirements were satisfied,
adequate
measures
were in place to ensure
personnel
safety and prevent damage
to plant
structures, systems, and components, and to ensure that equipment operability was verified upon
completion.
The following maintenance activities were observed:
e
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"Perform CPI-FLO-2002," performed
in accordance
with
calibration procedure
(CPI)-FLO-2002, "Calibration of 1B Motor Driven Auxiliary
Feedwater Pump Discharge Flow Loop 2002," revision 5, effective date April2, 1993,
observed January
10, 1994
The inspector observed electrical calibration checks at the instrument rack; as-
found calibration was satisfactory, no adjustments were required.
The inspector
observed excellent procedural adherence
and good coordination between the two
technicians involved:
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Work Order 19369324, "Perform CPI-PRESS-2030," performed in accordance with CPI-
PRESS-2030,
"Calibration of Motor Driven Auxiliary Feedwater
Pump B Discharge
Pressure Loop 2030," revision 6, effective date November 18, 1993, observed January
'0, 1994
The inspector observed calibration testing of pressure gauge PI-2190A; as-found
calibration
was
satisfactory,
no adjustments
were required.
The inspector
observed excellent procedural adherence
and good coordination between the two
'echnicians involved.
Work Order 19440277, "CV-4010 - Major Inspection," performed in accordance with
maintenance
procedure (M)-37.16H, "Inspection and Maintenance of Chapman-Crane
Tilting Disc Check Valve," revision 19, effective date November 15, 1992, observed
January
10, 1994
The inspector observed valve disassembly;
the valve was in good condition and
required no refurbishment beyond minor cleaning.
"MOV-4008 Limitorque Operator - Adjust Tripper Fingers,"
performed in accordance
with M-64.2, "Limitorque SMB-000 and SMB-00 Motor
Actuator Maintenance Procedure," revision 17, effective date February 3, 1993, observed
January
10, 1994
Limitorque motor actuators
can be operated
either by an installed motor or
manually, using a handwheel.
A manually operated
declutch lever is used to
switch from the motor operated
mode to the manual mode.
Once the declutch
lever has been depressed,
the actuator is designed to remain in the manual mode
without further operation of the declutch lever. This feature is performed by two
tripper fingers, which latch against an adjustment arm when the declutch lever is
depressed
and hold the clutch in the manual position.
Subsequently, ifthe motor
is operated,
cams that rotate only when the motor is running push the tripper
fingers offof the adjustment arm, and the clutch shifts back to the motor operated
position. This maintenance was initiated because continuous downward pressure
on the declutch lever was required to prevent the actuator from slipping into the
motor operated
mode
during
manual
valve operation,
indicating probable
misadjustment
of the
tripper
fingers.
This
aberrant
condition
does
not
compromise valve operability.
The procedure for setting the height of the tripper finger adjustment arm was not
in accordance
with the vendor's
current
guidance;
as
a result,
the initial
adjustment did not correct the problem.
The procedure was corrected by a PCN,
and proper alignment of the tripper finger adjustment arm was subsequently
obtained.
Acceptance testing, as specified in the original work package, did not specifically
test operation of the declutch lever; as a result, the fact that the initialadjustment
had been unsuccessful was not promptly identified. The specified acceptance
test
(the quarterly pump performance test) was not scheduled to be performed until
completion of all "B" train AFW system maintenance.
Through discussions with
personnel
who manually operated
the valve as a part of restoration from the
tripper finger adjustment, the inspector determined that the adjustment arm'ad
not been properly set.
The inspector informed the licensee of this finding while
the maintenance isolation was still in effect. As a result of rework to correct this
problem, the duration of the system outage exceeded
the planned duration by
several
hours;
had
the problem,
instead,
been
identified during the pump
performance
test, additional time would have been required to reestablish
the
maintenance isolation, reestablish system operational alignment after the rework,
and reperform the test.
The original job scope did not include motor removal.
Since a generic procedure
was used to perform the maintenance,
non-applicable portions were so annotated
as a part of the work package preparation.
During the course of the maintenance,
motor removal became necessary;
however, the work package was not reviewed
to ensure
that procedural items applicable to motor removal were reinvoked.
This deficiency was also noted by licensee QA during review of the completed
work package (Quality Assurance Observation Report 94-001:CEC).
"Replace Valves 8675A and 8675B and Piping," performed in
accordance
with M-37.134,
'-'Repairs
and Replacements
Threaded
Piping Components,"
revision 8, effective date May 13,
1993,
observed
January 25, 1994
Valves and piping make up the sample point for the "B" spent fuel pit cooling
system,
located at the pump discharge.
No deficiencies were noted; good QC
involvement was observed.
2.1.2
Containment Pressure Transmitters Found Inoperable Due To Plugged Sensing Line
The engineered safety features (ESF) system uses containment pressure as an initiating parameter
for several functions. A total of six pressure detectors (three 10-200 psia wide range and three
0-60 psig narrow range) provide input to the ESF system actuating logic, with two out of three
coincidence required to actuate the associated
ESF functions.
Detectors are connected
to the
containment atmosphere in pairs (one wide and one narrow range) through three separate sensing
lines. Allsix instruments provide indications in the control room; in addition, outputs from the
three narrow range detectors are monitored and archived by the PPCS.
On January 19, 1994, a control room operator observed that containment pressure narrow range
indicator PI-947 was indicating slightly lower than the other narrow range containment pressure
instruments.
Although the amount of deviation was within the tolerance specified for channel
comparison,
the operator
pursued
investigation.
A review of data archived by the plant
computer over the previous
18 days revealed
that PI-947 was not tracking with redundant
containment pressure indicators PI-945 and PI-949. A trouble report was submitted to initiate
corrective action.
On January 21, 1994, a calibration of the PI-947 pressure transmitter (PT-947) and associated
instrument loop was performed.
No equipment deficiencies were noted and no adjustment was
necessary.
Although this maintenance indicated that there was not a problem with PI-947, the
maintenance planner maintained the trouble report open, pending evaluation of new trending
data.
On February
1, 1994, the planner reviewed plant computer data archived subsequent
to
the calibration, and determined that PI-947 was still not tracking properly.
The planner then
brought this problem to the attention of the system engineer.
Prior to a routine equalization of containment pressure with atmosphere
on February 2, 1994,
test equipment was installed to monitor the outputs of PT-947 and the associated
narrow range
detector,
PT-948.
Test equipment
was also installed on one of the pressure
transmitters
connected
to each of the remaining two penetrations
that are used to measure
containment
pressure.
The outputs from these two detectors (PT-946 and PT-949) decreased
as expected in
response
to the pressure
decrease;
however, PT-947 and PT-948 outputs remained constant
throughout the pressure change, indicating that they were both inoperable.
In accordance with
technical specification table 3.5-2, the associated
ESF relays were tripped; in this condition,
continued power operation would be allowed until the next scheduled calibration of the affected
containment pressure instruments.
Troubleshooting revealed the problem to be a blockage in the common sensing line between
containment and the two pressure
detectors.
A temporary valve was installed at the open end
of the sensing line in containment.
This temporary boundary was demonstrated to be leak tight
using 120 psig air. The sensing line was then disassembled
at the containment penetration and
the obstruction, located in the portion of the sensing line within the containment penetration, was
dislodged using a metal rod.
The sensing line was then reassembled
and blown down with air
through the temporary valve. The obstruction consisted ofa black powder, which was collected
and retained for analysis.
Since the reassembled
sensing line had not been leak tested at the
point when the temporary valve was opened,
the. licensee entered a four hour action statement
per technical specification,3.6.3.1.a
for an inoperable containment isolation boundary.
The
sensing
line was
leak
tested
in accordance
with periodic
test procedure
(FIT)-23.17B,
"Containment Isolation Valve Leak Rate Testing, Pressure
Transmitters PT-947 and PT-948,
Penetration 203A," and returned to service approximately one hour later.
PT-947 was also
returned 'to service,
having been calibrated
as part of the troubleshooting effort and with
continued satisfactory operation having been verified during the penetration leak test,
Since no
quantitative testing had been performed on PT-948 during the troubleshooting, and since it was
nearly due for annual calibration gast performed March 1993), the decision
was made to
calibrate the instrument prior to returning it to service.
This was completed and PT-948 was
declared operational on May 4, 1993.
Through interviews with the personnel involved, observation of maintenance,
and review of
applicable documentation,
the inspector assessed
this to have been an excellent maintenance
effort. The inspector considered that the original identification of the problem was particularly
noteworthy.
The questioning attitude of an operator pursuing an indication that did not appear
correct resulted in identifying a degradation of the ESF actuating circuitry that was undetectable
within the existing scope of maintenance
and testing.
Site engineering was directly involved,
from identification of the problem through restoration of operability. Efforts of instrument and
control, health physics, and quality assurance
organizations were well coordinated.
Review of long-term historic data archived by PPCS revealed that the PT-947 tracking problem
had developed in May or June of 1992.
The inspector was concerned that this condition could
have gone undetected for so long a period of time. As of the close of the inspection period, the
licensee had initiated an investigation ofthis incident and was generating a licensee event report.
The inspector willcontinue to monitor the licensee's review, evaluation, and corrective actions
regarding this incident, through the licensee's
corrective action report (CAR) system (CAR
2087) and through review of the licensee event report.
2.1.3
Voluntary Entry into LCO Action Statements to Perform Preventive Maintenance
In anticipation of converting the plant to an extended (18 month) operating cycle in 1996, the
licensee is phasing in a program to enter into limiting conditions for operation (LCO) action
statements
to perform preventive maintenance
(PM) on a selective basis.
This change
in
maintenance
philosophy is a departure from the past scheduling practice in which PM was
accomplished at a time when safety equipment was not needed; e.g., during refueling outages.
An extended
operating
cycle would necessitate
scheduling
certain PM 'activities before
a
regularly scheduled plant shutdown.
To assess
the impact of such activities and identify the potential problem areas,
the licensee,
using probabilistic risk analysis (PRA) data, selected the "B" motor driven auxiliary feedwater
pump (MDAFP) and the "C" standby auxiliary feedwater pump (SAFP) to be removed from
service the weeks of January
10 and January
17, respectively, for the purpose of performing
various PM tasks.
To support these activities, PORC reviewed changes
to administrative (A)
procedures A-52.4, "Control of LimitingConditions for Operation For Operating Equipment,"
and A-1603, "Overview of the Ginna Station Work Control System," and relevant evaluations
that stipulated
additional controls to be imposed.
Constraints
to be applied during such
equipment outages included:
~ 'riticalpath activities would involve two shift coverage, alternating between the various
shops to avoid area congestion;
~
Spare parts would be verified to be in-stock prior to starting work;
Components that provide redundant safety function would be verified to be operable;
"C
The expected outage time for the affected safety-related equipment should be less than
50 percent of the allowed outage time stated in the technical specifications.
Prior to
commencing work, the shift supervisor would authorize any maintenance
activities;
however, ifthe planned work scope was projected to be greater than 50 percent of the
allowed outage time, approval by the Plant Superintendent would be required.
In developing additional controls, the licensee used the technical guidance contained in various
NRC documents
addressing
voluntary entry into LCO action statements
for maintenance
to
assure
that appropriate
safety principles were applied.
Additionally, PRA data was used in
making system selections to minimize risk probabilities.
The inspector reviewed the licensee's
relevant procedures,
evaluations,
and schedules,
and
observed
related
maintenance
activities in-progress.
Through
this review,
the inspector
concluded that the licensee has methodically evaluated performing PM on selected safety-related
equipment when operating at power.
Through observations of work in-progress on the "B" MDAFP and review of supporting work
packages,
the inspector determined that the tasks were expeditiously carried out, with the pump
being out-of-service for 37.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of a 7-day action statement.
The inspector confirmed that
redundant safety equipment was available during this period, including the "A" MDAFP, the
turbine driven auxiliary feedwater pump, and the "A" emergency
diesel generator.
With the
exception ofMOV-4008 (as discussed in section 2.1.1 ofthis report), work packages were found
to be appropriately detailed and identified the specific work scope.
Although a schedule was
developed to preclude work area congestion, the inspector did observe a significant number of
craft technicians (1&C, mechanics,
and electricians) working at the same time in the small area
of the "B" MDAFP. This condition did challenge the workers in carrying out their assignments.
The licensee
acknowledged
the inspector's
observation
and indicated that they planned
to
improve coordination of craft activities in future maintenance activities.
The inspector had no
further questions in this area.
2.2
Surveillance Observations
2.2.1
Routine Observations
Inspectors observed portions of surveillances to verify proper calibration of test instrumentation,
~
~
~
~
use of approved
procedures,
performance of work by qualified personnel,
conformance
to
limitingconditions for operation (LCOs), and correct system restoration following testing.
The
following surveillances were observed:
10
Performance Test (PT)-2.8M, "Component Cooling Water Pump MonthlyTest," revision
9, dated April2, 1993, observed January 6, 1994
PT-47. 10, "Spent Fuel Pit Charcoal Filtration System Efficiency Test," revision 6, PCN
94T-030, dated February 25, 1993, observed January 25, 1994-
~
PT-9.1.17, "Undervoltage Protection - 480 Volt Safeguard Bus 17," revision 9, dated
January
13, 1994, observed February 2, 1994
~
PT-2.2M, "Residual Heat Removal System - Monthly," revision 3, PCN 94T-0038,
effective date February 5, 1993, observed February 3, 1994
The inspector determined
through observing this testing that operations
and test personnel
adhered to procedures,
test results and equipment operating parameters
met acceptance criteria,
and redundant equipment was available for emergency operation.
3.0
PLANT SUPPORT (71707)
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3.1
Radiological Controls
3.1.1
Routine Observations
1
The inspectors periodically confirmed that radiation work permits were effectively implemented,
dosimetry was 'correctly wor'n in controlled areas,and
dosimeter
readings
were accurately
recorded, access to high radiation areas was adequately controlled, survey information was kept
current, and postings and labeling were in compliance with regulatory requirements.
Through
observations ofongoing activities and discussions with plant personnel, the inspectors concluded
that the licensee's radiological controls were generally effective.
3.1.2
Implementation of the Revisions to 10 CFR,20
All licensees were mandated to implement the broad changes that have been made to 10 CFR 20, "Standards for Protection Against Radiation," by January 1, 1994. In completing this effort,
licensee's were to revise radiological control procedures
and other associated
procedures,
such
as
emergency
preparedness,
administrative
and ALARA job planning;
upgrade
training
programs; and, post plant areas to comply with the new requirements.
k
The inspector reviewed
the status of RG&E actions
to implement these
changes,
through
procedure/record
reviews, plant tours, attendance
at general employee training sessions,
and
discussions with licensee representatives.
Based on this review, the inspector verified that about
140 radiation protection implementing and administrative procedures
have been upgraded and
were effective January 1, 1994; that NRC Form 4, "Radiation Exposure History," NRC Form 5,
11
"Monitoring Personnel Occupational Exposure," and NRC Form 439, "Report ofTermination,
Individual Occupational Exposure," reflect current requirements; and, that plant radiation areas,
based on the new criteria, were properly posted.
3.2
Security
3.2.1
Routine Observations
During this inspection period,
the inspectors
verified that x-ray machines
and metal and
explosive detectors were operable, protected area and vital area barriers were well maintained,
personnel were properly badged for unescorted or escorted access,
and compensatory
measures
were implemented when necessary.
No unacceptable conditions were identified.
3.3
Fire Protection
3.3.1
Routine Observations
The inspectors periodically verified the adequacy of combustible material controls and storage
in safety-related areas of the plant, monitored transient fire loads, verified the operability of fire
detection and suppression
systems,
assessed
the condition of fire barriers,
and verified the
adequacy of required compensatory
measures.
No discrepancies
were noted.
4.0
SAFETY ASSESSM~22tT/QUALITY VERIFICATION
4.1
Periodic Reports
Periodic reports
submitted by the licensee
pursuant
to Technical Specification 6.9.1 were
reviewed.
Inspectors verified that the reports contained information required by the NRC, that
test
results
and/or
supporting
information were
consistent
with design
predictions
and
performance specifications,
and that reported information was accurate.
The following report
was reviewed:
Monthly Operating Report for December
1993
No unacceptable conditions were identified.
4.2
Licensee Event Reports
Licensee Event Reports (LERs) submitted to the NRC were reviewed to determine whether
details were clearly reported,
causes
were properly identified, and corrective actions were
appropriate.
The inspectors also assessed
whether potential safety consequences
were properly
evaluated, generic implications were indicated, events warranted additional onsite follow-up, and
applicable requirements of 10 CFR 50.72 were met.
0
12
The following LERs were reviewed (Note:
date indicated is event date):
93-006, Feedwater Transient Results in a Lo-Lo Steam Generator Level and Subsequent
Reactor Trip. The cause was determined to be disconnection of the "A"-main feedwater
regulating valve positioner feedback linkage arm from the valve actuator linkage rod due
to disengagement of the screw from its nut.
(November 10, 1993)
I
93-007, High Source Range Flux Level During Reactor Startup Causes a Reactor Trip.
The cause was attributed to an operator inappropriately focusing his attention on P-6
status
lights (subsequently
found to be burned
out) rather
than
source
range
and
intermediate range indications.
(November 22, 1993)
The inspector
concluded
that the LERs were accurate,
met regulatory requirements,
and
appropriately identified the events root causes.
5.0
ADMINISTRATIVE(71707, 30702, 94600)
5.1
Deep Backshift Inspection
During this inspection period, a backshift inspection was conducted on February 7, 1994 and a
deep backshift inspection was conducted on January 20 and 22, 1994. The inspection on January
20 was in response
to the decreasing
screen house water level situation (See paragraph
1.3).
5.2
Exit Meetings
At periodic intervals and at the=conclusion of the inspection, meetings were'eld with senior
station management
to discuss
the scope and findings of inspections.
- The exit meeting for
inspection report 50-244/94-02 (engineering program inspection) was held on January 14, 1994,
by Mr. Harold Gregg.
The exit meeting for the current resident inspection report 50-244/94-01
was held on February
10, 1994, and was attended
by Mr. James Linville, Chief, Reactor
Projects Branch 3.