ML17263A498

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for Nov 1993 for Re Ginna Nuclear Power Plant.W/931210 Ltr
ML17263A498
Person / Time
Site: Ginna Constellation icon.png
Issue date: 11/30/1993
From: Dodge R, Widay J
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9312200008
Download: ML17263A498 (6)


Text

ACCELERATED DI RIBUTION DEMONST TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9312200008 DOC.DATE: 93/11/30 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME .AUTHOR AFFILIATION DODGE,R.E. Rochester Gas 6 Electric Corp.

WIDAY,J.A. Rochester Gas 6 Electric Corp.

RECIP.NAME RECIPIENT AFFILIATION R

SUBJECT:

Monthly operating rept for Nov 1993 for RE Ginna Nuclear Power Plant.W/931210 ltr. D DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: Monthly Operating Report (per Tech Specs NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 /

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PDl-3 LA 3 3 PD1-3 PD 1 1 JOHNSON,A 1 1 D

INTERNAL: AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1' NRR/DO+S/OEAB 1 1 NRR/DRI L/RPEB 1 Et M~ 01 1 1 RGN1 1 1 EXTERNAL EGGG BRYCE i J ~ H 1 1 NRC PDR 1 1 NSIC 1 1 R

D A

D D

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 14 ENCL 14

t zzp (zsumzs

'ii"'si iznirzut ROCHESTER GASANDELECTRICCORPORATION o 89EASTAVENUE, ROCHESTER, N.Y. 14649%001 JOSEPH A. WIDAY TELEPHONE Plant Manager AREA CODE 716 546.2700 Glnna Nuclear Plant GINNA STATION I

December 10, 1993 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

Monthly Report for November, 1993 Operating Status Information R. E. Ginna Nuclear Power Plant Docket No. 50-244

Dear Sir:

Pursuant to our Technical Specification 6.9.1, attached herewith is the monthly operating status report for Ginna Station for the month of November, 1993.

Very truly yours, Joseph A. Widay Plant Manager JAW:jkl Attachments c: Mr. Thomas T. Martin NRC (1) 9312200008 931130 i PDR R

ADOCK 05000244

..ZDR

4 OPERATING DATA REPORT DOCKET NO. 50-244

. 10 1993 COMPLETED 8 R rt ~ Dodge TELEPHONE 315 524-4446 Ext. 396 OPERATING STATUS 1 ~ Unit Nano: R.E GINNA NUCLEAR P(NER PLANT Notes Unit operating experiences outlined

2. Reporting Period: November 1993 on page 4.
3. Licensed Thermal Power (MWt): 1520 Nameplate Rating (Gross MWe): 490 5~ Design Electrical Rating (Het MWe): 470
6. Maximm Dependable Capacity (Gross MWe): 490
7. Maxiaun Dependable Capacity (Het MWe): 470
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level to Which Restricted, If Any (Het MWe):
10. Reasons For Restrictions, If Any:

This Month Yr.-to-Date Cunulative

  • 0
11. Hours In Report Period 720 8 016 210 906.45
12. Number of Hours Reactor Was Critical 574.50 6 817.79 167 782.46
13. Reactor Reserve Shutdown Hours 1 687.55 *
14. Hours Generator On-Line 558 6 765.25 165 008.38 15 ~ Unit Reserve Shutdown Hours 8.5 *
16. Gross Thermal Energy Generated (MWH) 731 946 9 812 672 233 856 425
17. Gross Electrical Energy Generated (MWH) 246 679 3 311 312 77 309 116
18. Net Electrical Energy Generated (MWH) 233 173 3 143 650 73 379 581
19. Unit Service Factor 77.50X 78.39X
20. Unit Availability Factor 77.50X 78.39X
21. Unit Capacity Factor (Using MDC Net) 68.90X 83.44X 75.32X 22 ~ Unit Capacity Factor (Using DER Het) 68.90X 83.44X 75.32X
23. Unit Forced Outage Rate 22.50/ 2.34X 5.73X
24. Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):

Refueli and maintenance March 4 1994. Duration-40 da s.

25. If Shut Down At End of Report Period, Estimated Date of Startup
26. Units In Test Status (Prior to Comnerciai Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION CUMULATIVE TOTAL COMMENCING JANUARY 1, 1975 CLNULATIVE TOTAL COMMENCING NOVEMBER 8, 1969

iAVERAGE DAILY UNIT POWER LEVEL t

DOCKET NO: 50-244 UNIT: R.E. Ginna Nuclear Power Plant ATE: De . 10 1993 COMPLETED BY:

Rob r E. Dodge TELEPHONE: 315 524-4446 Ext. 396 MONTH November 1993 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1~ 481 17. 403 2 ~ 482 18. -10 3 ~ 481 19. -10 4 ~ 481 20.

5. 481 21 ~ -10
6. 482 22.

7 ~ 481 23. 214

8. 482 24. 478

'8

9. 482 25. 479
10. 172 26. 480
27. 480 12 13 14.

'61 263 28.

29.

30.

480 480 479

15. 241 31. 481
16. 477 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in reporting month. Compute to the nearest whole megawatt.

DOCKET NO 50-244 UNIT NAhll'. R E. GINNA NUCLEAR POWER<PLAQT DATE De 10 3 UNIT SHUTDOWN AND POWER REDUCTIONS COhIPLI'.l ED BY Robert . ge REPORT hlONTH November TI'. LI'.Pl ION E. 31 5 524-4446 e xt . 396 L

0 c c c v licensee 0 lA Couse 8 Corrective 0 c 0

Ew 0 c Ho. Date 0 0 0 Event 0 0 0 Action to

~ 0 e 0 0 0 E Prevent Recurrence Q ~ It'. own C Report 0 EA 0

CL 93-05 11/10/93 43.57 LER-06 CH INS'EU A Feedwater Regulator Controller failure, unit shutdown.

93-06 11/14/93 37.05 A 1 HH HTEXCH Condenser tube leak, pawer reduction 93-07 11-17-93 118.33 -A 1= HI PIPE XX B S/G blowdown steam line leak, unit shutdawn.

l 3 F: Forced Reason: hlethod: Fxhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) l-hlanual for Preparation of Data B-hlaintenance or Test 2-hlanual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) oi6I)

E.Operator Training 8c License Examination F-Administrative G-Operational Error (Explain)

REV. 485 4949 H-Other (Explain) Exhibit I - Same Source

~ ~ V

~ ~

C NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO: 50-244 UNIT: R.E. Ginna Nuclear Power Plant DATE: ec. 0 1993 COMPLETED BY:

Ro 6r E.Dodge TELEPHONE: 315 524-4446 Ext. 396 MONTH November 1993 The events during the month of November were as follows:

On 11/10/93, a reactor trip occurred due to malfunction on A S/G feedwater regulating valve. The unit returned to service on 11/12/93.

On ll/14/93, while at 85% power level reduced load for condenser tube leak repair. The unit was returned to full load on ll/16/93.

On 11/17/93, commenced reactor shutdown due to steam leak in B S/G blowdown line. After repairs, the unit was restored to service on 11/22/93, and remained there at the end of the report period.