ML17252B273
| ML17252B273 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 08/06/1976 |
| From: | Harris S Commonwealth Edison Co |
| To: | US Atomic Energy Commission (AEC) |
| References | |
| Download: ML17252B273 (3) | |
Text
.., *-*-
\\~
~. I...-**.
- 1.
Repbrting Period: ()0()/ 76070/
through~t? 76073/.
Gross Hours in Reporting Period:
- 74=!:
- 2.
Currently Authorized Power Level MWt.e2S;2.7
- Design Electrical Rating (MWe-Net):
802
- 3.
Power Level to Which Rest.ricted (if any): --""'~....__.~:...-._.....~
- 4.
Reasons for Restrictions (if any):
Moll Section rr>*DA'fE.
- 5.
Number of Hours Reactor was *critical
.... z4fl:..,
~-~-~
'~/
- 6.
Reactor Reserve Shutdown. Hours *****.**..... __. __ o __
0 0
Hours Generator On Line ** * ****........ Z+/-:f. &-tZ'.3£. 3(p4Pt.
- 8.
Unit Reserve Shutdown Hours * * *
- *..... ____ o ____
0
'()
9 *. Gross "Thermal Energy Generated (MWH) **** ~ i,_7.,%7*;14 h,,'6Jf~f3! 6?;<S0~',
)
)
)J
- 10. 'Gross Electrica 1 Energy Generated (HWH) ****.fi.~O~B. ~l~~E8 -2?SJ4$:; *
- 11.
Net Electrical Energy Generated (MWH)
- ~ *~~.i2(8 12~ *Reactor Service Factor
- 13.
Reactor Availability Factor. * * * *
- * *
- 100 14 *. Unit Service Factor * * * * * * * * *.. * * *. /QQ
- 15.
- Un It Ava l1abi1 i ty Factor
- * * * * //)()
- 16.
Unit Capacity Factor (Using HOC) *******. 9/i&
- 17.
Unit Capacity Factor (Using Design MWe). * *
- fBZ.4
- 18.
Un t ~ Forced Outage Rate
<!).;;;.. _ _
SZ9 7/, ~
7;, &
60,/
!;;~.I
~G,S j(? c cJ
- 18. ;l_
- 19.
Shutdowns Scheduled Over:, Next 6 Months (Type._. Date~* and Du rat ion of Each):
Tl.J.S.131N. ~"'J) HPC, LJ/fHIN~ING-woR" /? 9
~r 7..;:ihfrrs S/\\/u(3d~t? <:;.. J;S.I //'V'Sr'Ec TION
. 7i I
1.::i..P H.RS
- 20.
If Shut down at end of Report Period, Estimate Date o Startup:
-W t1' -..
8396
i:*.
I
..r.:_,.
.. 'ltY PLAITT PO'.IER OUTPUT. e
- :*.--=.--=----.*
~.,__,.~~ l',Q!!&h,,.~J t: I 9 m-* *-----*-
~
J:;~ - *
':C---:R.!I.:.. ~verage Oa tly H\\Je-net
..:* ;.. *~.
. £!:z:
- . f.verage Daily H\\Je-net 1.
.* :{:39
.. 17
. 2*
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.. 11.
.. 12
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- . ** Ila
- . *.-.:*. : *15,,..
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- . £(.e,Cf:
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. 5~£
..5*7+/-
.S7<e
- ssq:
SfeG
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§0" s.r;*7 19
. *--**064":.
20 s~q.-
21
... S&/ *
- s:~*
- . 23 *
- S:-ws. *
'.,....... 3~~*
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' 25
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.* 26... :.. :(() l 27
... 4&6
. 28,~:
537
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- S0/
. Docket "J> *OS(}_ -,-.;;i. ~rci
- ~*~
~@OJ zrr
-. * ***-Date.. /iu C-; r;,*. I '77'7
- Completed By_ Y lJ. ;:-4-tvvj
~I(,r /Q*t( n,
"?.A~A
DOCl~ET IJO. 0..;x.J -~~ /
UNIT NAME *l>r1'Je°c~on.ZZ: REPORT M>NTH c/u~tl?7 ~ DATE6{;&-. ;.19Jd:OMPLF..TED BYS..
SUMMARY
UNIT 2 sm;WlY - JULY, 1976 TELEPHONE&'5':
- ~~ <:.:~'. - x ~;;l~s-~*;
nresden! 2 entered the month of July at 475 MWe and increasirtg. The major load limiting facto:rs--.. -*'"'.
- )
~'
were lo¥ condensate booster pump suction pressure and high circulating water inlet temperatureso Though not a limiting factor, the A recirculation pump motor was rmming warm.
The cooling lake lift puttps. were lost for approximately an hour ori 6/8/76 and 6(26/76.*
- The nionth ended with the unit at-approximately 800 MWe and yielding a.vailability/capacity factors of ~00/91.6 percent.
PU}.."l' SHUTOOWNS
.* TYPE.
f.\\ETHOD OF. SHUTT-1 N(i fJOWN THE NO.
DA.TE F-FORCED DURATION RFASON (1) REACTOR OR-* R c-CORRECT I VF. ACTION/COMMENTS S~CHEDULED HOtJRS I NG POW 2
I
. (1) REJ\\SON:
. A-mUIPHENT FAILURE.. (EXPIAm)
B-1~\\INT. on TEST (2).MEJtWD *.
. J.
MANUAL~
-~-. ~~NUAL.. SCRAM
, I 11
. ri 1.1
!1 c-nEFUELIHG n-nEGUIATORY RESTRICTION E-OPEilATO!l TRAINING AND
.3.
- 4.
OTHER (EXPLAIN).
=-*.
. I LICEMSE EXAIIDIATION F-ADM.HIISTAATIVE.
.*G~PERATIONAL ERROR (EXPL\\IN).
.
- H-OTHER {EXPLAIN)