ML17252A900
ML17252A900 | |
Person / Time | |
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Site: | Indian Point |
Issue date: | 06/08/1973 |
From: | Caldwell W Con Edison, Consolidated Edison Co of New York |
To: | O'Reilly J US Atomic Energy Commission (AEC) |
References | |
Download: ML17252A900 (2) | |
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Category:Letter
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Limit - Indian Point Unit 2 ML17252A8791973-12-0303 December 1973 Letter Regarding a 11/18/1973 Occurrence Relating to the Discovery of the Erroneous Setting for 1 of the Bistables Associated with Low Pressurizer Safety Injection Required by the Technical Specifications - Indian Point Unit No. 2 ML17252A8781973-11-30030 November 1973 Letter Providing Supplemental Information Concerning the 11/13/1973 Incident at Indian Point Unit No. 2 ML17252A8821973-11-19019 November 1973 Letter Concerning a 11/16/1973 Occurrence Regarding Periodic Tests and Calibration Checks Indicating the Setting for 1 of the Bistable Device Was Below the Technical Specification Requirements - Indian Point Unit 2 2018-05-21 |
Text
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,38 FR DC NEWYORK NY ,~, 06-08 61~P EDT S JA .ES P OREILLY DIR EGULATO Y OPERATIONS REGION t US ATO IC ENE GY COMMSISSION 970 BROAD ST NEWARK NJ 07102 r REI t DIAN POINT UNIT #2 -FACILITY OPERATING LICENSE OPR-20 IN ACCORDANCE ITH THE REQUIREMENTS OF TECHNICAL SPECIFICATION
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WE ISH TO INFORM YOU OF AN ABNORMAL OCCURRENCE,
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WHICH TOOK PLCE ON JUNE 7 ,973*
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CXJRING THE COURSE OF PERFORMING PERIODIC TESTS ANO CALBBRATION CHECKS RELATING TO REACTOR COOLANT FLOW AS REQUIRED BY THE
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FACLLYTY TECHNICAL SPEFICICATTONS, IT WAS DETERMI~D THAT THE FLOW TRIP SETTINGS WERE SLIGHTLY BELOW THOSE SPECIFIED TN SPECIFICATION 2.3~1, AT THE TIME OF THE OCCURENCE, THE REACTOR WAS CRITICAL AT ZERO P OWER FOR ZERO POWER PHYSICS TESTING, TN ACCORDANCE WITH THE REQUIREMENTS OF TECHN!CAL SPECTFTCATTON 6,2, NOTIFICATION OF THE CHAIRMAN OF THE NUCLEAR FACILITIES AFETY COMMITTEE HAS TAKEN PLACE.
R A FASANO OF YOUR OFFICE WAS ALSO NOTIFIED BY TELEPHONE ON JUNE g 1973 OF THE OCCURRENCE Y MR JOHN M MAKE ACE, CHIEF ENGI NEER, UNI T NO 2 Sf' 1201 IR5-60)
~E ARE CURRENTLY INVESTIGATING THE CAUSE OF THE OCCURRENCE ANO THE RESULTS OF OUR INVESTIGATION A D CORRECTIVE ACTION TAKEN WILL E SUBMITTED IN THE REQUIRED TEN DAY REPORT TO THE DIRECTOR OF LICENSING WILLIA~ E CALOWELL-CON EDISON CO 4 IRVI G PLACE NY NY ,0003 TELEX NB ,2 7339 SF-1201 (RMIJ)
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