ML17252A456

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Submittal of Reportable Occurrence Report No. 78-033/03L-0
ML17252A456
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 09/08/1978
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
78-033/03L-0
Download: ML17252A456 (2)


Text

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Comm.ealth Edison Dresden ear Power Station R.R. #1.

REGULATO' DOCKET AU OOPY S!

co Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr 1178-1257 James G. Keppler, Regional Director September 8, 1978 Directorate of Regulatory Operations - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137

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Reportable Occurrence Report fl78-033/03L-0, Docket //050-249 is hereby submitted to your office in accordance with.Dresden Nuclear Power Station *Technical Specification 6.6.B.2.(a), reactor protection system or engineered safety feature instrllinent settings which are fqund to

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~ t be less conservative than those established by the technical specifications but which do not prevent the.fulfillment of the functional requirements of affected systems..

. nson Station Superintendent Dresden Nuclear Power Station BBS/deb Enclosure cc:

Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC

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1 Q LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) i 1

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[iDJ I rll LI DI RI s I 3 101 o Io I - Io Io Io Io Io I-Io Io IG)l 4 I 1 ! 1 I 1 I 1 101 I 10 l

8' 9 I LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON~T/

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~~~~~~ L!:J© I o I s I o I o I o I 2 I 4 I 9 101 o I s 1 2 11 I t I s 10 I o I 9 I o I s I 7 I s I G) 8 60 61

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DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80

.:,;*- EVE~T DESCRIPTION AND PROBABLE CONSEQUENCES@

@ID 'I Wh~le performing surv. DIS 250-1, MSL Hi Flow Isol. Sw.

dpis 3-261-2C tripped at I

CD]:Jli3~.5 psid.

(T.S. limit</= 115.0 psid at 120% Flow; Table 3.2.1).

The 16 MSL Hi I

CQ:ill* I Flpw Isol. Sw. 's provide containment isolation whenever primary integrity required.

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[~JII I sa:fety. significance minimal because both trip sys. were operable and would have l

EQI[J is'olated containment at 111.5 psid, conservative to T.S. limit of 115 psid.

Similar jIE) I ev~nts ref. in _LER. f/050-249/1977'-4; 78-022/03L-O, 78-027/03L-0 & 78-028/03L-0 also

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a SYSTEM CODE I II B!@

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\\~;REPORT Ll7 ! 8 I

NUMBER 21 22 CAUSE CAUSE CODE SUBCODE w@ w@

11 12 13 SEQUENTIAL*

REPORT NO.

! o I 31 31 COMPONENT CODE IIN Isl Tj*RI ul@

18 OCCURRENCE.

CODE' I o I 3 I 23 24 26 27 28 29 COMP.

VALVE SU8CODE.

suBCODE L..!.J w@

. 19 20 REPORT TYPE LU 30 1-i 31 ACTION FUTURE.

EFFECT SHUTDOWN r::::;..

ATTACHMENT NPRD-4 FORM 5UB.

PRIME COMP.

SUPPLIER REVISION NO.

L2J 32 COMPONENT MANUFACTURER I

80 TAKEN ACTION

. ON PLANT METHOD HOURS ~-

SUBMITTED

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36 37 40 41 l!Ll@ uu0* l Bl o I 8 I ol@

42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS.@

I C~use - bent indicator pointer dragging across-face. plate prohibiting proper operation.~

cm:J 1PO:inter had been straightened after similar occurrence last month but apparent metal i

.I fa.'tique resulted in repetitive bending.

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Pointer replaced.

Sw reset to Dresden setpt. I QTI] I 110+/-2 psid and retested **sat. on 8/28/78 for verification of fix.

Monthly testing I

  • of MSL sw's will continue.

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i FACILFTY STATIJS 80 GE W@

METHOD OF

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DISCOVERY DIS_COVERY DESCRIPTION \\(31 l.J!JG2)1.__~S~u~r~v~e~i~l~l~a~n~c~e'--'T~e~s~t~i~n~g2--~~~--,~~~---'I

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M LOCATION OF RELEASE @

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80 so*

NA 80