ML17251A657
| ML17251A657 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 04/25/1986 |
| From: | Kober R ROCHESTER GAS & ELECTRIC CORP. |
| To: | Murley T NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| References | |
| RTR-REGGD-01.033, RTR-REGGD-1.033 NUDOCS 8605060294 | |
| Download: ML17251A657 (6) | |
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ROCHESTER GAS AND ELECTRIC CORPORATION KI Ptll LllCOalia I
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89 EAST AVENUE, ROCHESTER, N.K 14649-0001 ROGER W. KOBER VICE PIIESIDENT ELECTRIC S STEAM PROOVCTION TCCCPHI7NC AREA COOC 7la 546.2700 A
April 25, 1986 Dr. Thomas E. Murley, Regional Administrator U. S. Nuclear Regulatory Commission Region I 631 Park Avenue King of Prussia, Pennsylvania 19406
Subject:
I
& E Inspection Report 86-03 Notice of Violation Containment Integrity Technical Specification Requirements For Refueling Were Violated While Maintenance Was Being Performed, Concurrently, On Vital Bus 14 R. E..Ginna Nuclear Power Plant, Unit No.
1 Docket No. 50-244
Dear Dr. Murley:
In accordance with the above subject which stated:
"As a result of the inspection conducted on February 9
through February 28,
- 1986, one violation of NRC require-ments 'was identified.
The violation involved the failure to adhere to Station Technical Specifications.
Technical Specification 6.8 states that written proce-dures shall be established, implemented and maintained covering activities referenced in Appendix A of Regula-tory Guide 1.33, November 1972.
Appendix A, paragraph 1 discusses procedures for performing maintenance.
The Ginna Station Quality Assurance Manual program description requires implementation of Regulatory Guide 1.33, November
- 1972, which endorses American National Standards Institute (ANSI)'N18.7-1972.
ANSI N18.7-1972 states in paragraph 5.1.6.3, "planning (of maintenance) shall consider the possible safety consequences of concurrent or sequential maintenance,
- testing, or operating activities.
Equipment required to be operable for the mode in which the reactor exists shall be available."
Contrary to the above, maintenance procedures were not adequately established, implemented and maintained, in
- that, preventive maintenance performed on Vital Bus 14 and Motor Control Center 1C violated containment 8b050b0294 ab0425 PDR ADOCK 05000244 l0 8
f
',Or.
Thomas E. Murley I & E Znspection Report 86-03 Page 2
April 25, 1986 integrity requirements for refueling operations on February 15 and 16, 1986.
Containment isolation motor-operated valves 313 and 813 were deenergized and open for a period of approximately ten hours without their respective downstream isolation valves locked
- closed, as required by Technical Specification 3.8.l.a.
The following is submitted in response.
We believe the root cause of this event is due to not thoroughly reviewing the impact of the removal of MCC 1C relative to Technical Specification 3.1.8.l.a.
Our root cause analysis revealed the following:
o The error is not a result of a lack of knowledge.
o That procedure changes willnot prevent related generic problems.
o Means exist to ensure that proper conditions are established for each mode of plant operation - based on the self identifi-cation of event.
o That it is a shared staff responsibility to plan and schedule
.concurrent activities.
o That operations personnel should be cognizant of the status of plant systems and equipment under their control and should ensure that they are controlled in a manner that supports safe and reliable operation.
o That the ultimate responsibility for plant status controls lies with the Shift Supervisor.
Our actions to address this specific event are:
1.
The staff has discussed this violation and has concluded the most appropriate corrective action for us is to ensure that all sections thoroughly and independently review planned actions.
2.
The Operations Manger will present this violation to his Shift Supervisors at the next Shift Supervisors meeting.
The discussion will stress gob responsibilities and the need to ensure adherence to station policies, procedures, and Technical Specifications.
We concur that maintenance planning needs to be strengthened as identified in this violation and the violation in Xnspection Report 85-26.
To ensure that all station maintenance activities are reviewed and appropriately evaluated for their affect or potential impact on Technical Specification required and safety related r
C Ca
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Sr.
Thomas E. Murley I& E Inspection Report 86-03 Page 3
April 25, 1986 equipment the following short term actions will be completed by
- June, 1986.
1.
Plant managers will stress the requirement that all plant personnel maximize the use of the maintenance work request and trouble report (MWR) to initiate maintenance.
2.
Maintenance Manager will provide training session to all maintenance supervisors and foremen during weekly meeting.
The session will address A-1603 (Maintenance Work Request and Trouble Report) procedure on the establishment of conditions required to perform maintenance.
3.
Each maintenance shop foreman will provide his own training session to his assigned personnel.
4.
The Operations Manager will draft a memo to be attached to plan of day reinforcing operating personnel of their role in control of maintenance activities.
5.
Certain collateral duties currently assigned to the Mainten-ance Supervisor will be assigned to another employee.
This will increase the supervisor's availability to provide more time for planning and control of maintenance activities.
Long term action activities willcontinue Maintenance Information for full implementation to enhance the control of maintenance via the implementation of our computerized System.
The MIS target completion date is January, 1988.
Ve truly yours, Roger W. Kober Subscribed and Sworn to me on this 6 h day of April, 1986.
)
LYNNI. HAUCK Notary Public in the State of Nets Yotft h<ONROECOUNTY Comrisraon Expin.'s Nor. 30, lK-.P
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