ML17250B011

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Insp Rept 50-244/89-13 on 890807-0910.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maintenance,Surveillance,Security,Periodic & Special Repts & Recent SALP Mgt Meeting
ML17250B011
Person / Time
Site: Ginna 
Issue date: 10/03/1989
From: Mccabe E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17250B012 List:
References
50-244-89-13, NUDOCS 8910190070
Download: ML17250B011 (16)


See also: IR 05000244/1989013

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

Report

No.

50-244/89"13

Licensee

No.

DPR-18-

Licensee:

Rochester

Gas

and Electric Corporation

49 East

Avenue

Rochest'er,

New York

Facility:

Location:

R.

E. Ginna Nuclear. Power Plant

Ontario,

New York

Inspection

Conducted:

August

7 through September

10,

1989

Inspectors:

.Approved by:

N.'erry, Acting Senior Resident

Inspector,

Ginna

E. Yachimiak, Acting Resident

Inspector,

Ginna

8 c'4

E.

C.

McCabe, Chief, Reactor Projects

Section

38

I o/z/zy

Date

~Summar:

Areas Ins ected:

Routine inspection

by the resident

inspectors

of station ac-

tivities including plant operations,

radiological controls,

maintenance,

sur-

veillancee,

security, periodic

and special

reports,

and the recent

SALP manage-

ment meeting.

Inspection activities consisted of 93 hours0.00108 days <br />0.0258 hours <br />1.537698e-4 weeks <br />3.53865e-5 months <br /> of inspection,

and

included five hours of backshift inspection.

Results:

The plant operated

safely during this inspection period,

and the

licensee effectively dealt with plant occurrences.

'

TABLE OF CONTENTS

PAGE

1.

Persons Contacted................

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2.

Summary of Plant Operations...........................'...............

1

3.

Areas Inspected.

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a.

Plant Operations...

b.

Radi ol ogi ca 1 'ontrol s

c.

Maintenance..-

d.

Surveillance.

e.

Security.....

f.

Periodic

and Special

Reports

g.

Reports- of Nonroutine Events.

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5

4.

'ALP Management

Meeting.

5.

Exit Inter vice.

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6

6

DETAILS

Persons

Contacted

During this inspection period,

inspectors

held discussions

with and inter-

viewed operators,

technicians,

engineers

and supervisory level personnel.

The following people

were

among those contacted:

S

D

A

R.

T.

R;

A.

~).

I

~

~

  • S

J.

Adams,

Technical

Manager

Fi lkins, Manager of HP

8 Chemistry

Jones,

Corrective Action Coordinator

Narchionda,

Director of Outage

Planning

Marlow, Superintendent,

Support Services

Mecredy,

General

Manager,

Nuclear Production

Morris, Maintenance

Manager

St. Martin, Corrective Action Coordinator

Schuler,

Operations

Manager

Smith, Operations

Supervisor

Spector,

Superintendent,

Ginna Station

Widay, Superintendent,

Ginna Production

"Denotes

persons

present

at exit meeting

on September

14,

1989.

Summar

of Plant

0 erations

At the beginning of the inspection period,

the plant was in hot shutdown

with Microprocessor

Rod Position Indication (MRPI) System troubleshooting

activities ongoing.

On August 7,

1989, control rod position indication

coil stack

F-12 was determined to be shorted to ground; this caused

the

MRPI problems.

The plant was taken to cold shutdown

and the

F-12 coil

stack

was replaced with a qualified spare.

The reactor

was taken critical

on August ll, 1989.

With reactor

power at approximately

13 percent

on August 11,

1989, opera-

tors attempted

to manually withdraw control rods during the load increase.

Bank "D" was expected

to- move, but Bank "A" received

a withdraw demand

signal

instead.

No rods

moved,

as

Bank "A" was already fully withdrawn.

The rod control

bank overlap unit was found to be reset,

which caused

the

demand for Bank "A" to withdraw.

The bank overlap unit was set to the

correct position

and the load increase

was

resumed.

At the close of the

inspection period, the licensee

had not determined

the cause of the bank

overlap unit reset.

The annual

emergency

exercise

.was held

on August 16,

1989

and is addressed

in

NRC Inspection

Report 50-244/89-20.

On August 24,

1989 the "A" safety injection

pump recirculation'heck

valve

failed to check flow during monthly surveillance.

The valve was then re-

tested satisfactorily twice, once after running the "A" safety injection

pump to provide forward flow through the check valve.

No cause for the

malfunction was found.

The licensee

increased

the surveillance

frequency.

No additional malfuncti'on occurred,

and the prescribed

surveillance fre-

quency

was restored.

On August 28,

1989, during Periodic Test PT-1,

Rod Control System,

two

control

bank groups failed to move upon demand.

Operators initiated

a

plant shutdown in accordance

with technical

specifications,

and Instrumen-

tation

and Controls personnel

were called in.

Based

on discussion

with

Westinghouse

representatives

during troubleshooting,

two circuit cards in

the rod control

system were replaced.

The rod control

system

was retested

satisfactorily,

the power reduction

was halted at approximately

65 per-

cent,

and the plant was returned to full power.'he

two circuit cards

were sent to Westinghouse

for further testing.

At the close of the in-

spection period, that testing

was not completed.

During normal primary system chemistry

sampling

on September

1,

1989,

an

increase

in iodine indicated failed fuel cladding.

Control

room operators

noted

a small but steady

increase

in primary system radiation levels,

con-

firming the chemistry

sample results;

Iodine concentration

peaked

on Sep-

tember

3 and reached equilibrium during the following week.

The iodine

level

and total

system activity were below technical

specification

limits't

all times.

The licensee

implemented thei r action plan for failed fuel

and,

based

on communications

wi.th Westinghouse,

estimated that one or two

fuel rods caused

the activity increase.

On September

3,

1989,

the licensee

received

information from the Rochester

Police Department

concerning

a

bomb threat against

Ginna Nuclear

Power

Station.

The threat

was received

on the

911

number.

Rochester

police

stated that the caller was identified and picked up.

The

same

individual'as

reportedly threatened

Ginna and. government officials in the past.

The

threat

was assessed

as not credible.

During

a= periodic test of operability of heat trace circuits on September

7,

1989, electrici'ans

discovered

a blown fuse in the secondary

heat trace

circuit for the discharge

piping of the "B" boric acid

pump.

The heat

tracing

and fuse were replaced

and the

system

was returned to

an operable

status.

The primary heat trace circuitry remained

operable at all times.

On September

8,

1989, during

a periodic component cooling water

system

test,

the licensee

found the

low pressure

alarm setpoint

and the standby

pump auto-start

setpoint out of calibration.

The licensee

suspected

that

the primary cause

was setpoint drift caused

by pump stopping

and starting.

The setpoints

were recalibrated

and the test

was satisfactorily completed

(see section 3.d.).

The licensee

is evaluating corrective actions.

At the close of the inspection period,

the plant was operating at approxi-

mately full power.

e

'

3.

Functional or Pro

ram Areas Ins ected

a.

Plant

0 erations

(71707)

The inspectors

assessed

whether the Ginna Nuclear

Power Plant oper-

ated safely and in conformance with regulatory requirements.

Por-

tions of Rochester

Gas

and Electric Corporation's

management

control

systems

were evaluated

to ensure effective discharging of its re-

sponsibilitiess

for continued

safe operation.

Licensee actions during the inspection

period were found to be con-

servative.

For example,

the start-up

on August 11,

1989 was stopped

while rod control troubleshooting activities were performed;

the "A"

safety injection

pump, check valve was retested

twice on August 24,

1989;

and after the August 28,

1989 control rod failure, several

re-

tests

were performed.

No unsafe plant conditions were identified.

Radiolo ical Controls (71707)

C.

The resident"inspectors

periodically verified that

RWPs were imple-

mented properly, dosimetry was correctly worn in contr~lied areas

and

dosimeter

readings

were accurately

recorded,

access

control at en-

trances

to high radiation areas

was adequate,

personnel

used

con-

tamination monitors

as required

when exiting controlled areas,

and

postings

and labeling were in compliance with regulations

and proce-

dures.

No inadequacies

were i'dentified.

Maintenance

(62703)'

The inspectors

observed

safety-related

maintenance

to verify that

redundant

components

were operable; activities did not violate limit-

ing conditions for operation;

required administrative

approvals

and

tagouts

were obtained prior to initi'ating work; approved

procedures

were

used or the activity was within the "skills of the trade," ap-

propriate radiological controls were implemented; ignition/fire pre-.

vention controls were properly implemented;

and equipment

was pro-

. perly tested prior to its return to service.

Portions of the follow-

ing activity were observed:

Calibration Procedure

CP-210B, "Calibration and/or

Maintenance

of

RMS Channel

R-10B (Plant Vent Iodine)," Revision

1, effective

date January ll, 1989,

observed

September

6-7,

1989.

During

this activity,'he technicians

found

a minor procedure

problem.

The technicians

stopped

the activity and

had the procedure

cor-

rected before resuming.

The inspectors

concluded that this

.

maintenance activity was performed

correctly.'n

August 15,

1989,

"A" main steam line radiation monitor, R-31,

~ failed.. Technical

specifications

allow R-31 to be inoperable for

seven

days.

That limit was not exceeded,

as the monitor was returned

to service

on August 22.

However, the work was initiated late due to

improper prioritization and technicians

were unaware of the

seven

day

limit.

Plant maintenance

management

stated that, in the future,

maintenance

personnel will be cognizant of technical specification

limits.

The inspectors

had

no further questions.

Overall, maintenance

was assessed

as satisfactory.

d.

Survei l 1 ance

(61726)

The inspectors

observed

surveillances

to verify that the testing

demonstrated

operability, test instrumentation

was properly cali-

brated,

approved

procedures

were used,

work was performed

by quali-

fied personnel,

limiting conditions for operation

were met,

and sys-

, tems were correctly restored

following testing.

Portions of the fol-

lowing surveillances

were observed:

Periodi" Test PT-1, Revision 26,

"Rod Control System," effective

date

May 13,

1989,

observed

August 29,

1989.

PT-2.8,

Revision 21,

"Component Cooling Water

Pump System," ef-

fective date July 14,

1989,

observed

September

8,

1989.

During performance

of PT-2.8, miscommunication

between

two test per-

sonnel

resulted

in the opening of the "A" residual

heat

removal

heat

exchanger

Component Cooling Water

(CCW) outlet valve further than

required to achieve

the desired test flow for the "A" CCW pump.

This

resulted

in auto-start of the "B" (standby)

CCW pump

on low system

pressure.

The valve was repositioned to its correct setting

and the

"B" pump was

stopped

by a control

room operator.

The test

was then

completed with satisfactory results.

Subsequent

review revealed that

both the low pressure

alarm setpoint

and the standby

pump auto-start

setpoint

were out of calibration.

Instrumentation

and Control tech-

nicians recalibrated

both setpoints.

A station event report was ori-

ginated to notify the

NRC resident

inspector

and appropriate

Ginna

station personnel.

Although miscommunication

caused

the unanticipated start of the

standby

pump,

the inspectors

observed that subsequent

test personnel

actions demonstrated

clear understanding

of the system's

design

and

operation.

Their inquiries into the cause of the incident resulted

in correction of a deficient condition which could have otherwise

gone undetected.

Overall, surveillance activities were assessed

as satisfactory.

e.

~Securit

(71707)

During this inspection period, the resident

inspectors verified that

x-ray machines

and metal

and explosive detectors

were operational,

Protected

Area and Vital Area barriers

were maintained,

access

con-

trol during security tur'nover was adequate,

personnel

were properly

badged,

and compensatory

measures

were implemented

when necessary.

No inadequacies

were

identified'.

Periodic

and

S ecial

Re orts (90713)

Upon receipt, periodic

and special

licensee

reports

submitted pur-

'uant to Technical Specifications 6.9. 1 and 6.9.3 were reviewed.

This review included the following considerations:

reports contained

information required

by the

NRC; test results and/or supporting in-

formation were consistent with design predictions

and performance

specifications;

and reported

information was valid.

The following

report was reviewed:

Monthly Operating

Report for July,

1989.

No inadequacies

were identified.

g.

Written

Re orts of Nonroutine Events

(90712)

Written reports

submitted to the

NRC were reviewed to determine

whether details

were clearly reported,

causes

were properly identi-

fied,

and corrective actions

were appropriate.

The inspectors

also

determined

whether potential

safety consequences

had

been properly

evaluated,

generic implications were indicated,

the events warranted

onsite follow-up, and the reporting requi rements of 10 CFR 50.72

and

10 CFR 73 had

been

met.

The following LERs were reviewed (date in-

dicated is event date):

89-008, July 6,

1989,

"Dropped Control

Rod During Rod Control

System Exercises

Causes

Automatic Turbine Runback."89-009, July 29,

1989, "Failure of Control

Rod Position Indica-

tion System

Due to

a Grounded Coil Stack Causes

Plant Shutdown

per Technical Specifications."89-010, July 30,

1989,

"Safeguards

Bus Undervoltage

Relay Actu-

ation

Due to a Loose

Fuse

Connection

Causes

Automatic Start of

the "B" Emergency, Diesel G'enerator."

No inadequacies

were identified.

SALP Mana ement Meetin

On August 24,

1989, the Systematic

Assessment

of Licensee

Performance

(SALP) Report 50-244/87,-99

was discussed

at

a management

meeting in the

RG&E corporate offices in Rochester.

NRC management

summarized

licensee

strengths

and weaknesses

as described

in .the

SALP report.

RGEE indicated

general

agreement

with the report and stated that

a written response

would

be drafted within a month.

In addition,

RGhE committed to meet with NRC

management

to describe

programs

developed

to strengthen

performance.

Exit Interview (30703)

I

The inspectors

met with senior plant management

periodically and at the

end of the inspection period to discuss

inspection

scope

and

findings.'ased

on

NRC Region I review of this report

and discussion .held with lic-

ensee

representatives,

it was concluded that this report does

not contain

information subject to

10 CFR 2.790 restriction's.