ML17250A297
| ML17250A297 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 05/29/1980 |
| From: | White L ROCHESTER GAS & ELECTRIC CORP. |
| To: | Crutchfield D Office of Nuclear Reactor Regulation |
| References | |
| NUDOCS 8006030294 | |
| Download: ML17250A297 (5) | |
Text
pW REGULATORY ORMATION DISTRIBUTION SY M (RIDS)
ACCESSION NBR:8006030294 DOC ~ DATE: 80/05/29 NOTARIZED:
NO DOCKET FACIL:50 244 Robert Emmet Ginna Nuclear Planti Unit '1~ Rochester G
05000240 AUTH,NAME AUTHOR AFFILIATION WHITEpL,D Rochester Gas L Electric Corp.
REC IP ~ NARK REC IP IENT AFFILIATION CRUTCHFIKLDgD ~
Operating Reactors Branch 5
SUBJECT:
Responds to NRC 791023 request.Forwards revi'sed util 791210 commitments re containment purging.
DISTRIBUTION COOK:
A034S COPIES RECEIVED:LTR ENCL TITLE: Containment Purging NOTES'
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RECIPIENT ID CODE/NAME ACTION; 05 BC ~~~
INTERNAL:
0 12 IL 17 ENGR BR 19 PLANT SYS BR 21 EFLT TRT SYS 2Q E
REEVES EXTERNAL: 03 LPDR 25 ACRS COPlES LTTR ENCL a.
7 1
2 1
1 1
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RECIPIENT ID CODE/N A/1K 02 NRC PDR 15 CORE PERF BR 18 REAC SFTY BR 20 EKB 23 D
SHUN STS GROUP LKADR 04 NSIC COPIES LTTR KNCL 1
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TOTAL NUMBER OF COPIES REQUIRED; LTTR ~
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ROCHESTER GAS AND ELECTRIC CORPORATION L<4 ~ Oaf>I+Op. '0as i
o S9 EAST AVENUE, ROCHESTER, N.Y. 14649 LEON D. WHITE, JR.
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- RCA CDDC 7le 546.2700 Nay 29, 1980 Director of Nuclear Reactor Regulation Attention:
Nr. Dennis N. Crutchfield, Chief Operating Reactors Branch No.
5 U.S. Nuclear Regulatory Commission Washington, DC 20555
Subject:
Containment Purging During Normal Plant Operations R. E. Ginna Nuclear Power Plant Docket No. 50-244
Dear Nr. Crutchfield:
Your letter of October 23,'979 requested that Rochester Gas and Electric Corporation (RG&E) commit to an interim position on containment purging.
As a guideline, the Staff's interim position was enclosed.
Our letter of December 14, 1979 presented RG&E's com-mitments based on the Staff's guidelines.
Following Staff review of those commitments, we were requested to revise our commitments by members of the Staff.
Accordingly, the following commitments are provided using the paragraph numbering of the October 23, letter.
Whenever the containment integrity is required, emphasis will be placed on operating the containment in a passive mode as much as possible and on limiting all purging and venting times to as low as achievable.
To justify venting or purging, there must be an established need to improve working conditions to perform a safety related surveillance, safety related maintenance procedure, or inspections re-quired to facilitate design or installation of safety re-lated modifications.
(Examples of improving working con-ditions would include reducing temperature,
- humidity, and airborne activity sufficiently to permit efficient performance or to significantly reduce occupational radia-tion exposures.)
This commitment supersedes our prior 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year purge limit.
It should be noted that considerable judgment may be required in some instances to balance the goal of main-taining purging to as low as achievable and the goal of maintaining occupation radiation exposures as low as reasonably achievable.
- Further, judgment, may be re-quired in evaluating the need for purge while at hot shut-R006030~q P
ROCHESTER GAS AND ELECTRIC CORP.
DATE May 29, 1980 To Mr. Dennis M. Crutchfield SHEET NO.
down while performing cleanup following an outage when such cleanup is rectuired for safe operation of the plant.
2a.
Commitment number 2.a. is not revised.
The mechanical stops which limit purge valve opening were installed in December 1979.
2b.
Commitment number 2.b. is not revised.
As discussed with your Staff, our commitment 2.b.
meets your interim posi-tion.
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