ML17249A483

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Monthly Operating Rept for Dec 1979
ML17249A483
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/09/1980
From: Mcnamara A
ROCHESTER GAS & ELECTRIC CORP.
To:
Shared Package
ML17249A482 List:
References
NUDOCS 8001150485
Download: ML17249A483 (10)


Text

OPERAT)NG DATA REPORT DOCKET NO- 50 244 DATE J ua 9 1980 COMPLETED BY Andrew E. McNamara TELEPHONE 1-716-546-2700 OPERATING STATUS Ext. 291-205, at Ginna

l. Unit Name: GINNA STATION UNI The Reactor Power Level
2. Reporting period: December, 1979 averaged 100% in the 490 Report Month, exceptions
3. Licensed Thermal Power (MWt):

4i. Nameplate Rating (Gross MWe): were a Unit Shutdown S. 1)csign Electrical Rating (Net MWe):

490 from 12/2 - 12/19, detailed on Page 3.

6. Maximum Dependable Capacity (Gross MWe):
7. Maximum Dependable Capacity (Net MWe)t
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level to Which Restricted, If Any (Net MWe):

l0. Reasons For Restrictions, If Any:

This Month Yr.-to-Da te Cumulative I I. Ilours In Reporting Period 744 8 760 88 512 I 2. Number of Hours Reactor Was Critical 339.70 6,477.35 67,679,77 I < Reactor Rcscrvc Shutdown Hours 42.46 75. 06 1 621.57

  • 327.5 6,378 65,956.63 l4i. Ilours Generator On-Line
  • 0 0 8 5 IS. Ilnit Rcscrvc Shutdown Hours
16. Gross Thermal Energy Generated (MWH) 486 144 88 275 802 l 7. Gross Electrical Energy Generated (MWH) 159 810 28 685 791 l8. Nct Electrical Energy Gencratcd (MWH) 152 082 29 960 510 27 161 548 I'). Unit Service Factor 02 4.52%
20. Unit Availability Factor 02%%u ~%%u 4.5  %

.%%u 4 67. 74%

C%%u 0 2.$ . Unit Forced Outage Rate 2 I. Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):

Annual Refueli and Maintenance Overhau1 tentativel scheduled for March 15 1980.

2S.'f Shut Down At End Of Report. Period, Estimated Date of Startup:

26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION Cumulative total commencing January 1, 1975 ggg00 orb

AVERAGE DAILY UNIT POWER UNIT DOCKET NQ.. 50 244 UNIT tII pinna Statio Janaar 9, 1980 COMPLETED BY Andrew E. McNamara TELEPHONE 1-716-546-2700 Ex't 29 1 205 9 at Gonna MON TH DECEMBER 9 DAY AVERAGE DAILY POWER LEVEL DAY. AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 475 17 405 18 149 415 20 471 21 22 473 476 23 476 24 477 25

'77 10 26 477 27 476 12 28 476 13 29 475 14 30 476 31 INSTRUCTIOiVS On this format, list the average daily unit power'level in MWe-Net for each day in the reporting month.

Compute to the nearest whole megawatt.

tRKV I/78>

1 ~

A

l)O(:KET NO. ~o-244 IINIq NAhff: tt1 Ginna Station f)AT f Jant 9 1 980 UNIT SHUTDOWN AND POWER REDUCTIONS C:OhfPLETED BY r.>~a Andrew E. McNamara REPORT hfONTII D~E~~ Ti:LI:I>>IONI: 1-716-546-2700 Ext. 291-205, at Ginna 0 C C 0 Mj 0 sg C c v Licensee E~ C Cause L Corrective 0 ~

No. Date o 0 o Event vl 0

o Q t7 Action to o

O~ o CIA C Report ff EA 0

o go Prevent Recurrence 0

Cl 6~7 12-2-79 416.5 A 1 S/G Type (HT EXCH) "B" Steam Generator Tube Leak '-

Leak (79-22) Pressurizer Relief Line Nozzle Relief Line Repair - Boric Acid Tanks, Low Nozzle Boron Concentration.

(79-23) 3 F: Forced Reason: hfcthod: Fxhibit G - Instructions S: Schcdulcd A-Equipmcnt I ailurc (Explain) I-hfanual for Preparation of Data l3-hfa intcna ncc or Test 2-hfanual Scram. Entry Sheets for Liccnscc C-Rcfucling 3-Automatic Scram. Event Rcport (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) OI6I)

E-Operator Training 8: I.iccnsc Examination F-Administrative G-Operational Error (Explain) a9 89 (AEVI'/7SI II-Other (Explain) Exhibit I - Same Source Yearly Unit Shutdown Number.

a 1 1

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO. 0-2 UNIT Ginna Station Un't 0 DATE Januar 9 1980 COMPLETED BY Andxew E. McNamara TEI.EPHONE 1-716-546-2700 xt. - , at irma MONTH DECEMBER The Reactor Power Level averaged 100% until the Unit was shutdown on 12/2 for repair of a tube leak on the "B" Steam Genexator. The pressurizer relief line nozzle was also repaired during the shutdown. On 12/17 the Reactor was taken critical and shortly afterwards was placed in the hot shutdown condition when the Boric Acid Tanks were found.to be out of specifications due to low boron concentration. The Unit remained shut-down until startup on 12/19. The Reactor Power Level was gradually increased to 100% on 12/20 and remained there for the remainder of the Report Period.

C C A

(

GINNA STATION

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~ r MAIN ANCE REPORT FOR DECEiSER 1979 During December, normal inspections and minor maintenance was performed. Major safety related maintenance included:

1. Replacement of one source range (NV-32) and both intermediate ranges (N-35, N-36) of the nuclear instrumentation.
2. Plugging of two leaking tubes and 11 other tubes that were within the plugging criteria in the "B" steam generator.
3. Permanent repair of the south handhole on the "B" steam generator by welding the damaged area on the steam generator flanged area. This had previously been repaired using furmanite.
4. Replacing the body to bonnet gasket on pressurizer spray valve 431A.
5. Replacement of a spare primary loop RTD.
6. Weld repair of the corrosion cracking on the pressurizer relief valves safe'nd.

.7. , Replacement of reactor protection relay RT 10 on train "A" after a failed coil was found.

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