ML17229B515

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Insp Rept 50-331/96-04 on 960420-0605.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support
ML17229B515
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 07/05/1996
From: Kurth M, Christine Lipa, Kenneth Riemer
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17229B513 List:
References
50-331-96-04, 50-331-96-4, NUDOCS 9607310047
Download: ML17229B515 (22)


See also: IR 05000331/1996004

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

License

No:

50-331

DPR-49

Report

No:

50-331/96004

Licensee:

IES Utilities Incorporated

IE Towers,

P. 0.

Box 351

Cedar Rapids,

IA

52406

Facility:

Duane Arnold Energy Center

Dates:

April 20 June 5,

1996

Inspectors:

K. Riemer,

Senior Resident

Inspector

C. Lipa, Resident

Inspector

M. Kurth, Reactor

Engineer

G. Kelly, NRR Project Manager

Approved by:

R.

D. Lanksbury, Chief

Reactor Projects

Branch

2

96073i0047

960705

PDR

ADOCK'500033f

8

PDR

EXECUTIVE SUMMARY

Duane Arnold Energy Center

NRC Inspection

Report 50-331/96004

This integrated

inspection report included aspects

of licensee

operations,

engineering,

maintenance,

and plant support.

The report covers

a 6-week

period of 'resident

inspection;

in addition, it includes the results of

announced

inspections

by the

NRR project manager

and

a regional reactor

inspector.

~0evations

The inspectors

identified that Operation's

had not recognized,

prior to

authorizing

a maintenance activity,

a required entry into a limiting

condition for operation.

This was

a violation (Section Hl.3).

The inspectors

identified an increasing

trend in offgas pretreat

radiation release

rate that

had not been identified by the operators.

(Sections

01.3

and Rl.l)

Operator

response

to materiel condition problems

encountered

during the

period,

such

as

a reactor recirculation motor generator trip and

scoop

tube lockups,

continued to be appropriate

(Section H2).

Maintenance

One station activity undertaken

in response

to the Hay 16,

1996,

unexpected trip of the "B" reactor recirculation motor generator

(RRHG)

set

and control of monitoring equipment installed

because

of earlier

trips, were weak.

This resulted in the loss of potentially important

data necessary

to determine

the root cause of the trip (Section H1.4).

Chronic problems with the well water chlorination system continued to

challenge plant staff because

of resultant

higher than 'normal drywell

temperatures

due to fouling (Section

M2).

En ineerin

Engineering

support to plant operations

during this inspection period

was mixed.

Short term resolution of materiel condition issues

was

appropriate.

However, actions

taken to date in response

to long term

concerns

such

as the

RRHG trips and well water chlorination issues

have

not resolved

the items,

nor have they prevented further challenges

to

plant staff.

Engineering participation in the activities associated

with the "8" reactor recirculation motor generator

set

was weak and

contributed to the loss of potentially important data

(Section

M1.4 and

H2.1).

The inspector's

review of the containment

hardened

vent modification

identified only minor discrepancies,

which the licensee

properly

resolved

(Section El.l).

Several

UFSAR discrepancies

were identified during the Spent

Fuel

Pool

Licensing Basis

Review (Section E2.1).

Plant

Su

ort

A potentially negative trend in the off-gas radiation release

rate

was

not effectively communicated

by Chemistry through the site organization

until the inspectors

brought the matter to the licensee's

attention

(Section Rl).

Se f Assessment

and

ualit

Ve if'cation

Self-assessment

activities,

such

as Operations

Committee

and Action

Request

screening

meetings

were considered

effective (Section 07).

The

gA surveillance of the containment

hardened

pipe vent modification

was considered

thorough

and detailed

(Section El.l).

Re ort Detail s

Summar

of Plant Status

The plant began this inspection period at

100 percent

power.

There

was

a

routine downpower for turbine valve testing

on May 11.

From May 16 until

May 23, the plant was in single loop operations

and reactor

power was

approximately

45 percent following the trip of the "B" reactor recirculation

motor generator

(RRMG) set.

Following recovery of "B" RRMG on May 24," 1996,

the plant operated

near

100 percent

power for the remainder of the inspection

period.

I. 0 erations

01

Conduct of Operations

Ol.l

General

Comments

a.

Ins ect

o

Sco

e

71707

Using Inspection

Procedure

71707, the inspectors

conducted

frequent

reviews of ongoing plant, operations.

This included control

room

observations

and plant tours.

The inspectors

noted that, the conduct of

operations

was professional

and safety conscious.

Observations

indicated that the operations staff was knowledgeable of plant

conditions,

responded

promptly and properly to alarms,

adhered to

procedures

and applicable administrative controls,

performed through

turnovers,'nd that proper control

room staffing levels existed.

01.2

Failure To Reco nize

LCO Entr

b.

Observations

and Findin s

As discussed

in Section M1.3, the inspectors identified during

independent verification of operator actions for an ongoing maintenance

activity that the operators

had failed to recognize, prior to

authorizing maintenance

on

a drywell pressure

instrument, that entry

into a limiting condition for operation

(LCO) was necessary.

The

inspectors, were concerned that operation's

involvement in planning

and

review of this maintenance activity was weak.

01.3

0 erators

Unaware

o

Increasin

Trend in Off as Pretreat

Radiation

Release

Rate

b.

Observations

and F'in

s

As discussed

in Section Rl.l, control

room operators

were not aware of

an increasing

trend in the offgas pretreat radiation release

rate until

the inspectors

brought it to their attention'.

The increasing trend was

potentially an early indicator of fuel leakage

problems.

The operator's

il

I.

01.4

immediate

response

was to contact the chemistry department

to assist

in

resolution of this issue.

The inspectors

were concerned that

a

potential early indication of a fuel problem was not noted

by the

operators

in a timely manner.

A

ro riate

0 erator

Res

onse to Reactor Recirculation

Pum

Tri

a

~

Ins ection

Sco

e

71707

b.

On Hay 16,

1996, the "B" reactor recirculation motor generator

(RRHG)

set unexpectedly tripped

as discussed

in Sections

H1.4 and H2. lb.

The

inspectors

independently verified that appropriate

actions

were taken

by

reviewing strip charts,

surveillance

requirements,

and technical

specification requirements.

Observations

and Findin

s

01.5.

~

~

07

07.1

The operators

responded

appropriately to the event

and successfully

maintained

the plant in single loop operations.

The operators

also

correctly implemented the increased

surveillance

requirements

and

administrative controls necessary

to maintain the plant in single-loop

operation while trouble-shooting

and maintenance activities were

performed

on the "B" RRHG set.

On Hay 23,

1996, the inspectors

observed

the operators

place the "8" loop of RR back in service

and return the

unit to full power.

Conclusions

on Conduct of 0 erations

The inspectors

determined that, with the exception of the maintenance

activity on

a drywell pressure

instrument,

operator

cognizance

and

oversight of maintenance activities were appropriate for the tasks

performed.

The inspectors

also concluded that operators

performed well

in response

to the

RRHG set trip and during associated

troubleshooting

and maintenance activities,

and during recovery of the idle loop and

return of the unit to full power.

With the exception of the increasing

trend in offgas pre-treat radiation release

rate levels,

operator

panel

awareness

was thorough.

guality Assurance

in Operations

Licensee

Self-Assessment

Activities

40500

b.

Observations

and Findin

s

During the inspection period, the inspectors

reviewed multiple licensee

self-assessment

activities, including:

Routine Operations

Committee Meeting

Routine Action Request

Screening

Meetings

Special

Operations

Committee meeting

on Hay 17 to review

recommendation

to operate

at higher power level in single loop

operations,

as allowed

by TS.

Special

Operations

Committee meeting'n

Hay 22 to discuss

restoration of the "B" RRHG set

and return to full power

operations.

f

The inspectors

observed that there

was active participation at the

meetings.

c.

Conclusions

on License Self-Assessment

Activities

The inspectors

concluded that the self-assessment

activities observed

were effective.

08

Niscellaneous

Operations

Issues

(92700)

08.1

Closed

Licensee

Event

Re ort

LER

50-331

94003

Revision 0:

Failure

to Establish

Secondary

Containment

During Routine Maintenance.

The

licensee identified the cause to be incomplete

implementation of a TS

amendment.

The issue

was determined to be

a non-cited-violation

as

discussed

in inspection report (IR) 50-331/94002.

The inspectors

reviewed the completion of corrective actions listed in the

LER and

had

no concerns.

This item is closed.

08.2

Closed

LER 50-331

94006

Revisions

0 and

1:

Reactor

Water Cleanup

Isolation

Due to Incomplete Valve Closure

Caused

by Position Indicator

Obstruction.

This issue

was originally discussed

in IR 50-331/94008.

The inspectors

reviewed the completion of the four'orrective actions

discussed

in the

LER.

The corrective actions

were considered

appropriate

to prevent recurrence.

This item is closed.

II. Maintenance

Nl

Conduct of Naintenance

Ml. 1

General

Comments

a.

Ins ection

Sco

e

62703

61726

The inspectors

observed

and/or reviewed portions of the following work

and testing activities:

Drywell pressure

recorder maintenance

Deluge system for standby transformer

Turbine control valve

EOC

RPT logic and

RPS instrument functional

test

Daily instrument

checks

Functional/calibration of reactor water level instrumentation

Standby liquid control

system

boron concentration test

Standby diesel

generators

monthly operability test

"D" river water supply

pump motor replacement

Reactor recirculation motor generator

set troubleshooting

M1.2

Instrument

Used for TS Readin

not in Calibration

Pro

ram

b.

Observations

and Findin

s

On April 25,

1996, the inspectors

identified that level instrument

LI 3413,

used to verify fuel pool level

as required

by TS 4.9.C was not

in a calibration program.

Surveillance

Test Procedure

STP42A001,

"Daily

Instrument

Checks,"

Revision

113, required that fuel pool level

be

documented daily using LI 3413,

however,

the instrument

had not been

calibrated

since it was installed in 1990.

The licensee

was able to

show that the design of the instrument

was

such that periodic

calibration

was not necessary.

Upon further review, the inspectors

considered this to be

an isolated

case;

however,

the inspectors

were

concerned that nothing in the modification process specifically required

assigning

a calibration frequency to new instruments that would be used

for TS surveillances.

The licensee

promptly documented

the condition

on

AR 96-0759.

Pending

further review by the

NRC and the results of the licensee's

evaluation,

this is considered

an Unresolved

Item (URI 50-331/96004-01).

Failure to Enter

LCO Durin

Maintenance Activit

Observations

and Findin

s

Prior to the removal of drywell pressure

recorder

instrument

PR4398A for

maintenance

in accordance

with CHAR A26453

on Hay 15,

1996, the

Operations Shift Supervisor failed to realize that the channel

would be

inoperable,

which required entry into a 30-day limiting condition for

operation

(LCO) in accordance

with TS Table 3.2-H.

The inspectors

identified this discrepancy

on Hay

17 and brought it to the

OSS'ttention.

Technical Specifications

Table 3.2-H requires

a minimum of two channels

operable for the Drywell Pressure

Monitor (0-250 psig).

Technical

Specification Action Statement

93 required that if the number of

operable

channels

was reduced to one channel,

then entry into a 30-day

LCO was required provided

a redundant

channel,

specified in Table 3.2-F,

was operable.

The redundant

channel

was operable at the time.

Technical Specification 6.8. 1 specified that written procedures

covering

areas

such

as corrective maintenance

be implemented.

Maintenance

Directive

(HD) 020,

"Maintenance

Planning," Revision 25, specified that

the

OSS was responsible for determining the effect on the plant and

any

other

requirements"

or special

conditions that were required for the

maintenance

to occur.

Failure of the

OSS to identify that there

was

a

TS

LCO associated

with the maintenance

was

a violation (50-331/96004-02)

of TS 6.8. 1.

The inspectors

were concerned

that planning

and review

prior to maintenance

were not adequate,

which was due to personnel

error

and inadequate

attention to detail.

Poor Troubleshootin

Activities Followin

Tri

at "B" Reactor

Recirculation Motor Generator

RRMG

Set

Observations

and Findin

s

Following an earlier trip of the "B" RRMG set,

the licensee installed

monitoring equipment

on the unit in order.-to obtain data necessary

to

determine

the root cause

for, the repeat trips experienced

on the

machine.

Subsequent

to the Hay 16,

1996, trip of the "B" RRHG set,

engineering

and maintenance

personnel

attempted to retrieve data

received after the event.

Their attempts

were unsuccessful;

none of the

7

H1.5

monitored parameters

on the

"B",RRHG set

had

any data available.

The

parameters

measured

on the "A" RRHG set were all available

and indicated

normal,

expected

values.

Further investigation

by the licensee

determined that the data

was unavailable

on the'B" side

because

the

trigger points

had not been

armed

and turned

on following the trip of

the "B" RRHG set

on January

17,

1996.

Potentially important data

necessary

for root cause determination

was lost because

licensee

personnel

failed to correctly utilize the installed monitoring

equipment.

Additional licensee

troubleshooting efforts focused

on

a transformer in

the voltage regulator circuit which was noted to have

blown fuses'.

Engineering

and maintenance

personnel

removed the component

from the

plant and attempted to bench test it in the, shop.

Improper electrical

troubleshooting'methods

were applied

and the transformer

catastrophically failed.

Because of human error, the only piece of hard

physical

evidence

was destroyed;

again, potentially important data

necessary

for root cause determination

was lost.

The inspectors will continue to monitor the licensee's

investigation of

the above

personnel

errors

and subsequent

corrective actions.

This will,

be tracked

as

URI 50-331/96004-03.

Conclusions

on Conduct of Maintenance

H2

H2.1

The inspectors

noted that most maintenance

activities during the period

were completed thoroughly and professionally.

However, the inspectors

were concerned

with personnel

errors during troubleshooting of the trip

of the "B"'RHG set

and inadequate

attention to detail in planning for

the drywell pressure

monitor maintenance,

discussed

above.

Naintenance

and Nateriel Condition of Facilities and Equipment

Plant Material Condition

b.

Observations

and Findin

s

Plant materiel condition was acceptable.

The inspectors

noted that

a

number of materiel condition issues

arose during the 'inspection period

that required the plant personnel

to take prompt action and/or resulted

in TS

LCO entries.

The inspectors

considered

the licensee's

response

to

these materiel condition issues

to be appropriate.

While each

individual occurrence

was of minor consequence,

collectively the issues

represented

distractions for operators

and other plant staff.

In each

case,

the issue

was entered into the plant's maintenance

process

or

corrective action process

and corrected,

as appropriate.

The examples

are listed below:

From April 25,

1996, to Hay 14,

1996, the

"D" well water chlorination

system

was out of service for maintenance

due to system leaks

on one

train and

a

pump motor problem on the other train.

Without chlorination

of well water, drywell cooler fouling occurs

over time.

Between

April 25 and

Hay 14, drywell average

temperature

increased

from

approximately

118'F to 127'F.

Although this was below the

TS limit of

135'F, the inspectors

were concerned that chronic problems with the "D"

well water chlorination system continued to challenge

the plant.

A

similar concern with the well water chlorination system

was discussed

in

inspection report 50-331/96002.

~

On Hay 2,

1996, operators

received

a spurious

1/2 scram

on

Channel Al.

This was only the second

1/2 scram this year;

however,

the January

1996 1/2 scram also occurred

on Channel Al.

The licensee

was unable to determine

the cause,

and plans

were

being

made to connect

an event recorder to the channel for future

monitoring.

On May 16,

1996, the "B" reactor recirculation motor generator

(RRHG) set tripped.

This was the fifth trip of the unit in

2 years.

Operators

responded

well to the event

and successfully

maintained the plant in single-loop operations.

The licensee

was

unable to determine

the root cause of the trip.

Reference

Section

H1.4 for inspector

concerns

associated

with

troubleshooting of the event.

The inspectors will continue to

track and monitor this issue

under previously opened

IFI 50-

331/96002-01.

On May 23,

1996, while restoring the "B" RRHG set to service,

control

room operators

experienced

several

lock-ups of the "B"

RRHG set

scoop tubes.

Operators

were able to manually control the

unit and returned

the plant to full power.

Upon replacement

of

faulty deviation meters

in the circuitry, the

RRHG set functioned

properly.

~

On Hay 30,

1996, operators

declared

the rod worth minimizer

inoperable for the third time in the past

few months.

The

licensee initiated

an

AR to document evaluation

and resolution

and

was working with General

Electric to. understand

the cause.

c.

Conclusions

The inspectors

noted appropriate

operator

response

to the "B" RRHG set

trip and to the scoop tube lock-ups during restorations.

Engineering

support for short-term resolution of identified materiel condition items

was appropriate.

Engineering

and maintenance

activities for long-term

resolution of the

RRHG set trips and well water chlorination problems

were not effective in resolving the issues.

N8

Miscellaneous

Maintenance

Issues

(92902,

92700)

H8. 1

Closed

LER 50-331

96002

Revision 0:

Primary Containment Isolation

System

(PCIS) Half Group III Isolation

Due to Blown Fuse During

Maintenance.

The licensee

determined that the

PCIS isolation

was

a

normal

response

to the blown fuse in radiation monitor RM4116B.

The

fuse

was blown during

a maintenance activity in the

RH4104 cabinet

(located directly above

RH4116B)

when

a cable fell into the

RH4116B

cabinet.

Corrective actions,

which included inspection

and fuse

0

replacement

in RM4116B, reinforcing expectations

that loose cables shall

be secured,

and

a review for applicable training, were considered

appropriate.

This item is closed.

El

'a ~

Conduct of Engineering

Ins ection

Sco

e

37551

III En ineerin

El.l

Selected

engineering

problems or events

were evaluated to determine

their root cause(s).

,The effectiveness

of the licensee's

controls for

the identification, resolution,

and prevention of problems

was also

examined.

The inspection

included review of areas

such

as corrective

action systems,

root cause

analysis,

safety committees,

and self

assessment.

Verification of Mark I Hardened

Vent Modification

a ~

Ins ection

Sco

e

TI 2515

121

b.

The inspectors

used the guidance

in Temporary Instruction (TI) 2515/121

to review the licensee's

adherence

to commitments

made in response

to

Generic Letter (GL) 89-16, "Installation of Hardened

Wetwell Vent."

The

inspectors

reviewed

system diagrams,

Operating Instruction (OI),

UFSAR

description,

Emergency Operating

Procedures,

maintenance

history,

and

the Design

Change

Package

(DCP 1524),

and performed

a walkdown of

accessible

portions of the system.

Observations

and Findin

s

The inspectors verified that the as-built installation conformed to the

design criteria listed in TI 2515/121,

Appendix A, and that appropriate

plant procedures

and training were implemented.

The inspectors identified minor discrepancies

between the system valve

line-up in OI 573,

"Containment Atmosphere Control System," the system

diagram,

and valve labeling.

The discrepancies

were promptly corrected

when discussed

with the licensee.

The licensee

completed

a Quality Assurance

(QA) Surveillance of the

modification in September

1994

and identified one deficiency regarding

seismic qualification in the safety evaluation.

The inspectors verified

that the deficiency was promptly resolved.

The

QA Surveillance

was

considered

thorough

and detailed,

with appropriate

resources

assigned

to

the review.

10

c.

Conclusions

The inspectors

concluded that the licensee

met the commitments to

GL 89-16

and that the hardened

vent was installed

as designed.

This

review closes

TI 2515/121.

El.2

En ineerin

Su

ort to

RRMG Troubleshootin

Efforts

b.

Observations

and Findin

s

As documented

in Section Hl.4b, potentially valuable data

was lost

during troubleshooting efforts initiated in response

to the trip of the

"8"

RRHG set.

Engineering

support to data recovery

and trouble-shooting

efforts was weak.

c.

Conclusions

Engineering efforts to date

have

been ineffective with respect

to long-

term resolution of the

RRHG set trips.

E2

Engineering

Support of Facilities

and Equipment

E2. 1

S ent Fuel

Pool

SFP

Licensin

Basis

Review

a.

Ins ection

Sco

e

The staff identified in April 1996, that the Updated Final Safety

Analysis Report

(UFSAR) write up on spent fuel pool cooling did not

reflect the practices

at

DAEC as described

in a spent fuel pool rerack

submittal to the staff (Amendment

195 to the license).

There

appeared

to be areas of the

UFSAR description that should

be amplified to provide

design

bases

information to facilitate review of the current procedures

that assure

cooling for the spent fuel pool.

There also were areas

where the spent fuel pool rerack submittal

and the

UFSAR differed and

needed to be reconciled.

b.

Observations

and Findin

s

E2.1.1

In reviewing the licensing

bases of the spent fuel pool, the staff

determined that

DAEC had stated that under certain circumstances

it would use the

RHR system in the spent fuel pool cooling mode if

heat loads

were high enough to warrant it.

However,

DAEC did not

provide the equilibrium (i.e., bulk) temperature for when

RHR was

used to independently

provide cooling in lieu of the spent fuel

pool cooling

(SFPC)

system.

Based

on the rerack submittal,

the

temperature

should

be for the maximum heat load with one

RHR pump

and heat

exchanger

operating.

This inconsistency will be reviewed

further by the Office of Nuclear Reactor Regulation

(NRR)

as part

of the Spent

Fuel

Pool Licensing Basis

Review and is tracked

as

Inspection

Followup Item (IFI) 50-331/96004-04.

11

E2.1.3

E2.1.4

E2.1.5

In reviewing the licensing bases,

the staff noted that there are

a

number of values given for the

"maximum" temperature of the spent

fuel pool.

Section 5.4 (iii) of the rerack submittal states that

peak spent fuel pool temperature

is intended to be limited to

180

F assuming

two cooling trains,

which in turn is below the

212'F regulatory limit.

However in the

UFSAR, it appears

that the

SFP structural

design limit under normal

heat load conditions

(i.e.,

a temperature

to which it would be acceptable

to cycle

a

large

number of times) is analyzed to not exceed

150'F (the

temperature

found in the'merican

Concrete Institute Code).

In

addition, the calculated

maximum temperature for the full core

offload case

was 164.4'F,

which is above the 150'F in the

UFSAR,

but below the

180

F limit.

These inconsistencies will be reviewed

further by

NRR as part of the

SFP Licensing Basis

Review and are

tracked

as IFI 50-331/96004-05.

In reviewing the licensing bases,

the staff found that the heat

load stated

by DAEC in the rerack submittal for the

Case 3'ull

core offload (18.87 x 10'tu/hr) is not consistent with

Supplement

1 of the rerack submittal

(18.73 x 10'tu/hr).

This

inconsistency will be reviewed further by

NRR as part of the

SFP

Licensing Basis

Review and is tracked

as IFI 50-331/96004-06.

The

UFSAR states

that

a fuel shuffle will not begin prior to

160 hours0.00185 days <br />0.0444 hours <br />2.645503e-4 weeks <br />6.088e-5 months <br /> after shutdown or that

a full core offload will not

begin prior to 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> after shutdown.

However, the rerack

submittal states

that fuel would not be moved prior to 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />

after shutdown.

In addition, the Operating Instructions

(OIs) at

DAEC do not mention specific delay times that need to be honored

prior to moving fuel.

These inconsistencies will be reviewed

.

further by NRR as part of the

SFP Licensing Basis

Review and are

tracked

as IFI 05-331/96004-07.

The

DAEC spent fuel pool rerack submittal specifies

the maximum

number of fuel assemblies

moved out of the core,

put back in the

core, left in the spent fuel pool

(SFP),

and the number of new

assemblies

placed in the core during

a core reload.

However, the

applicable

procedures

do not specify maximum or minimum values of

,assemblies

to be moved.

This inconsistency will be reviewed

further

by NRR as part of the

SFP Licensing Basis

Review and is

tracked

as IFI 50-331/96004-08.

'ase

3: This scenario

corresponds

to the actual

discharge

practice

at

DAEC.

The calculations consider

a total of 3152 locations for the fuel storage

in the

pool

and

are carried

out at the point in time

when the stored

fuel

inventory is such that the addition of a normal batch to the pool will leave it

with insufficient capacity to accept

another

batch while maintaining the full

core discharge

reserve capability.

The transfer to the pool begins after

120

hours of in-core decay

and is conducted

at

144 assemblies

per

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Two

spent fuel pool cooling trains are

assumed

to be in operation.

12

E2.1.7

E2.1.8

In Section 9.1.3 of the

UFSAR,

DAEC uses

the terms

"maximum normal

heat load" and

"maximum possible

heat load."

"Maximum normal heat

load" appears

to refer to fuel shuffling with approximately

1/3 of

the core being unloaded into the SFP.

The

"maximum possible

heat

load" appears

to refer to a full core offload.

Both terms

appear

to involve some conservative

assumptions,

but the

UFSAR contains

few details of the underlying analyses.

The assumptions

in the

terms

"maximum normal heat load"

and

"maximum possible

heat load"

do not correspond

to any of the four scenarios

detailed in the

.

1993 rerack submittal.

In OI 149

(RHR system),

pg.

54, the

definition of maximum normal

heat load disagrees

with the current

practice at

DAEC (i.e., full core offloads).

These

inconsistencies

will be reviewed further by NRR as part of the

SFP

Licensing Basis

Review and are tracked

as IFI 50-331/96004-09.

The

UFSAR defines the

RHR system in the Spent

Fuel

Pool Cooling

mode

as the alternate

cooling path for the spent fuel pool.

This

. path

has

a very complicated

and potentially time consuming

procedure.

Use of the

RHR system in the Spent

Fuel

Pool Cooling

mode has not been tested

since plant pre-operational

testing in

the early 1970s.

This inconsistency will be reviewed further by

NRR as part of the

SFP Licensing Basis

Review and is tracked

as

IFI 50-331/96004-10.

In Section 1.8. 13 of the

UFSAR,

DAEC states

that

"The

RHR system

is used

as the source of makeup water [for the spent fuel pool]

and is classified

as Seismic Category I.

The Seismic Category I

piping is extended into the fuel pool cooling system

as far as

necessary

to ensure

the makeup water will get into the pool'."

This statement

is incorrect

and does not reflect other portions of

the

UFSAR (such

as Section 9.1).

No plant procedures

existed for

transferring water from RHR to the spent fuel pool.

These

inconsistencies

will be reviewed further by NRR as part of the

SFP

Licensing Basis

Review and are tracked as,IFI 50-331/96004-11.

E2.2

Standb

Li uid Control

Boron Solution 0 er atin

Conce tratio

b.

Observations

and Findi

s

On November

7,

1995, the licensee identified a discrepancy

between the

UFSAR and plant procedures for the standby liquid control

(SLC) system.

Section 9.3.4.2 of the

UFSAR specifies that maximum boron solution

operating concentration

is 14.6 weight percent,

however, this upper

concentration

limit was not in plant procedures.

For example,

monthly

surveillance

procedure

STP 44C001,

"SLC System

Boron Concentration

Test," Revision 3, which specified

a lower concentration limit, but not

an upper limit.

The inspectors

and licensee

reviewed past performance of STP 44C001

and

found only one instance

where the

UFSAR 14.6 weight percent requirement

was exceeded.

On January

10,

1992, test results

showed that the boron

solution concentration

was 14.93 weight percent;

however, there were no

13

E8

ES. 1

consequences

because

the temperature

at the time was

above the minimum

solution temperature

curve in TS.

The inspectors

were concerned that

there

were

no controls to prevent exceeding

the

maximum concentration

value because

the

SLC tank low temperature

alarm setpoint

was

based

on

a

maximum of 14.6 weight percent.

The licensee

revised the

STP

and other

procedures

to specify the maximum concentration

value.

The inspectors

considered

the corrective actions to be appropriate.

This issue will be

reviewed further as

an IFI 50-331/96004-12.

Hiscellaneous

Engineering

Issues

Closed

Violation 50-331

94017-01:

Failure to Revise

Procedures

Following Changes

to Radiation Honitor Setpoints.

The cause

was

determined to be inadequate

controls in the engineered

maintenance

action

(EHA) process.

The inspectors

reviewed the licensee's

corrective

actions

and commitments

documented

in a letter to the

NRC dated

December

5,

1994.

The corrective actions

were considered

narrow in

scope

when

an additional

example of inadequate

controls in the

EHA

process

was identified on January

25,

1996.

As discussed,

in inspection

report 50-331/96002,

this was

a violation of 10 CFR Part 50, Appendix B,

Criterion XVI.

The inspectors will review the controls in the

EHA

process

and the implementation of corrective actions specified in the

licensee's

response letter to the

NRC dated

Hay 9,

1996, during the

closure of NOV 50-331/96002-07.

This item is closed.

IV Plant

Su

ort

Radiological

Protection

and Chemistry Controls

a.

Ins ection

Sco

e

In accordance

with procedure

71750,

selected activities associated

with

radiological controls, radiological effluents,

and waste treatment

were

reviewed to ensure

conformance with facility procedures

and regulatory

requirements.

Rl. 1

Increased

Trend in Off as Pretreat

Radiation

Release

Rate

b.

Observations

and Findin

s

Following restoration of the "B" RRHG set

and return of the plant to

full power, the inspectors

identified that the off-gas pretreat

radiation release

rate

had approximately doubled from earlier values

(from approximately 4-5 mrem/hour before the trip to approximately

8-10 mrem/hour after).

Control

room operators

were not aware of the

trend

and could not explain the reason for the increase.

The lead

chemist

had noticed the change

and

was investigating the issue,

but had

not communicated

his observations

to others.

The inspectors

were

concerned

that

a potential early indicator of a fuel problem was not

effectively communicated to others in the organization.

Subsequent

to

the exit meeting

on June

5,

1996, the licensee

demonstrated

to the

inspectors,

via coolant- sample results,

that the increase

in the level

was not attributable to

a fuel leak problem.

R1.2

Conclusions

in Radiolo ical Protection

and Chemistr

Control

The inspectors

had

no substantive

concerns with the licensee's

subsequent

efforts to resolve the increase

in offgas pretreat

release

rate,

as discussed

above,

once

a fuel leak was ruled out.

No other

concerns

were identified in this area.

V. Mana ement Neetin

s

Xl

Exit Heeting

Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on June

5,

1996.

The licensee

acknowledged

the findings presented.

The inspectors

asked

the licensee

whether

any materials

examined during the

inspection

should

be considered

proprietary.

No proprietary information was

identified.

15

Licensee

PARTIAL LIST OF

PERSONS

CONTACTED

J.

Franz,

Vice President

Nuclear

G.

Van Hlddlesworth,

Plant Manager

R. Anderson,

Manager,

Outage

and Support

P. Bessette,

Manager,

Nuclear Licensing

J. Bjorseth,

Maintenance

Superintendent

J. Cantrell,

Manager,

Nuclear Training

D. Curtland, Operations

Supervisor

R. Hite, Manager,

Radiation Protection

M. McDermott, Manager,

Engineering

K. Peveler,

Manager,

Corporate guality Assurance

INSPECTION

PROCEDURES

USED

IP 37551:

Engineering

IP 61726:

Surveillance Observation

IP 62703:

Maintenance

Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support

IP 92700:

Onsite Followup of Written Reports of Non-routine Events at Power

Reactor Facilities

IP 92901:

Followup Operations

IP 92902:

Followup Engineering

IP 92903:

Followup Maintenance

TI2515/121: Verification of Hark I Hardened

Vent Modifications

(GL 89-16)

ITEMS OPENED,

CLOSED,

AND DISCUSSED

~0ened

50-331/96004-01

50-331/96004-02

50-331/96004-03

50-331/96004-04

50-331/96004-05

50-331/96004-06

50-331/96004-07

50-331/96004-08

50-331/96004-09

50-331/96004-10

50-331/96004-11

50-331/96004-12

Closed

URI

NOV

URI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

'FI

50-331/94003

LER

50-331/94006

LER

50-331/96002

LER

50-331/94017-01

VIO

16

LIST OF ACRONYHS USED

i

CFR

Code of Federal

Regulations

CHAR

Corrective maintenance

action request

DAEC

Duane Arnold Energy Center

DCP

Design

change

package

EHA

Engineered

maintenance

action

EOC

End of cycle

GL

Generic Letter

IFI

Inspection followup item

IR

Inspection report

LCO

Limiting Condition for Operation

LER

Licensee

Event'Report

HD

Haintenance

Directive

NOV

Notice of Violation

NRR

Office of Nuclear Reactor Regulation

OI

,

Operating Instruction

OSS

Operations Shift Supervisor

gA

guality Assurance

RHR

Residual

heat

removal

RPS

Reactor protection

system

RPT

Recirculation

pump trip

RRHG

Reactor recirculation motor generator

SFP

Spent fuel pool

SFPC

Spent fuel pool cooling

SLC

Standby liquid control

STP

Surveillance Test Procedure

TI

Temporary Instruction

TS

Technical Specification

UFSAR Updated Final Safety Analysis Report

URI

Unresolved

item

17