ML17215A775

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Insp Repts 50-335/85-03 & 50-389/85-03 on 850120-0216.No Violation or Deviation Noted.Major Areas Inspected:Plant Operation,Surveillance Observation,Maint Observation & Procedure/Drawing Review
ML17215A775
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 02/26/1985
From: Bibb H, Crlenjak R, Elrod S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17215A776 List:
References
50-335-85-03, 50-335-85-3, 50-389-85-03, 50-389-85-3, NUDOCS 8503190308
Download: ML17215A775 (6)


See also: IR 05000120/2002016

Text

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UNITEDSTATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/85-03

and 50-389/85-03

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami, FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St. Lucie

1 and

2

License Nos.:

DPR-67

and

NPF-16

Inspection

Conducted:

January

20 - February

16,

1985

Inspectors:

r

Ja

Aced 8

Date Signe

Approved by:

S.

.

ro

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ection

ie

Division of Reactor Projects

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SUMMARY

Scope:

This routine,

unannounced

inspection

entailed

179 resident

inspector-

hours

onsite

in the

areas

of plant operation,

surveillance

observation,

maintenance

observation,

and procedure/drawing

review.

8503190308

850226

PDR

ADOCK 05000335

8

REPORT DETAILS

Persons

Contacted

Licensee

Employees

  • C. M. Wethy, Plant Manager
  • J. H. Barrow, Operations

Superintendent

T. A. Dillard, Maintenance

Superintendent

L. W. Pearce,

Acting Operations

Supervisor

N.

G. Roos, guality Control Supervisor

C. F. Leppla, Instrument

& Control Supervisor

C. A. Pell, Acting Technical

Department Supervisor

H. F. Buchanan,

Health Physics

Supervisor

J.

G. West, Security Supervisor

J. Barrow, Fire Prevention

Coordinator

J. Scarola, Assistant Plant Superintendent-Electrical

  • J. Walls, guality Control Department
  • N. Weems, guality Assurance

Supervisor

Other

licensee

employees

contacted

included

construction

craftsmen,

technicians,

operators, shift technical

advisors,

security force members

and

office personnel.

Exit Interview

The resident

inspectors

attended

entrance

and exit interviews

conducted

during the inspection period by Region II inspector

B. R. Crowley.

The resident

inspectors

also

conducted

interim interviews with licensee

management

during the inspection

period

and held

an exit interview at the

conclusion of the inspection.

The inspector

discussed

the

scope of the

inspection

and his findings with the licensee.

Persons

indicated with an asterisk

(*) in paragraph

1 above attended

one or

more interviews.

The licensee

did not identify as proprietary

any of the materials

provided

to or reviewed by the inspector(s)

during this inspection.

Licensee Action on Previous

Enforcement Matters

Closed

- Unit 2

(Unresolved

Item 389/84-37-01)

- Apparent

disagreement

between

Safety

Injection

Tank

(SIT)

"Green

Band" Limits and Technical

Specification

Maximum Limits.

The inspector

reviewed the Shift Technical

Adviser's

response

submitted

on February

12,

1985 and agreed that the upper

edge of the

green

band

and

the

HI-HI alarm setpoint

correspond

to SIT

volumes less

than the technical specification upper limit.

0

Unresolved

Items

2

.Unresolved

Items were not identified during this inspection.

Operational

Safety Verification

The inspector

observed control <room operations,

reviewed applicable logs

and

conducted

discussions

with Control

room operators

during the report period.

The

inspector

verified the operability of selected

emergency

systems,

reviewed tagout

records

and verified proper return to service of affected

components.

Tours of the reactor,

auxiliary and turbine building were

conducted

to observe

plant equipment conditions,

including potential fire

hazards,

fluid leaks,

and

excessive

vibrations

and

to verify that

maintenance

requests

had

been

initiated for

equipment

in

need

to

maintenance.

The inspector,

by observation

and direct interview, verified

that the physical security plan was being implemented in accordance

with the

station security plan.

General

Status

6.

Both units

operated

at

100% output throughout

the period

except for

a

one-day

shutdown

(Saturday

5 Sunday,

February

9 - 10) of Unit 2 to repair

some minor oil leaks

on

a reactor coolant

pump.

A meeting

was held in Miami

at

the corporate

headquarters

to present

the

NRC's findings

from the

recently

conducted

Systematic

Assessment

of Licensee

Performance

(SALP)

(ref. Report Nos. 50-335/85-02

and 50-389/85-02).

Maintenance

Observation

Station

maintenance

activities

of selected

safety-related

systems

and

components

were observed/reviewed

to ascertain

that they were conducted

in

accordance

with requirements.

The following items were considered

during

this review:

the limiting conditions for operations

were met, activities

were

accomplished

using

approved

procedures,

functional

testing

and/or

calibrations

were

performed prior to returning

components

or systems

to

service; quality control

records

were maintained; activities were

accom-

plished

by qualified personnel;

parts

and materials

used

were properly

certified;

and radiological controls

were

implemented

as required.

Work

requests

were reviewed to determine status of outstanding

jobs and to assure

that priority is assigned

to safety-related

equipment maintenance

which may

affect system performance.

The inspector

personally

observed

work on the following components

and

subsequently

reviewed

the

completed

paperwork to assure

completeness

and

'ccuracy.

PWO-726

PWO-727

PW0<<736

IWV-08-13, Repair Valve Seat

IWV-08-12, Repair Valve Seat

IWV-08-12, Inspect Internals

7.

Surveillance Observation

During the inspection

period,

the inspector verified plant operations

in

compliance with at least

sixteen different technical

specifications

(TS)

requirements.

Typical of these

were confirmation of compliance with the

TS

for reactor

coolant chemistry, refueling water tank, containment

pressure,

control

room ventilation

and

IIIC and

DC electrical

sources.

The inspector

verified that testing

was performed in accordance

with adequate

procedures,

test instrumentation

was calibrated, limiting conditions for operations

were

met,

removal

and restoration of the affected

components

were accomplished,

test results

met requirements

and were reviewed

by personnel

other than the

individual directing the test,

and that any deficiencies identified during

the testing

were properly reviewed

and resolved

by appropriate

management

personnel.

8.

Procedure/Drawing

Review

The following procedures

were reviewed by the inspector:

EP 1-0120040,

Rev.

EP 1-0120034,

Rev.

EP 1-0030131,

Rev.

EP 1-0030132,

Rev.

EP 1-0030130,

Rev.

OP 2-1400063,

Rev.

15 - Natural Circulation/Cooldown

13 - Reactor Coolant

Pump - Off Normal Operation

21 - Plant Annunciator

Summary

1 - Anticipated Transient Without Scram

20 - Reactor

Trip/Turbine Trip

3 - Sequence

of Events

Recorder

Program Loading

Several

errors

were noted, mostly of an editorial nature,

and were reported

to

gC personnel

for correction

in subsequent

revisions.

The

number of

errors,

however,

points out the

need for continued diligence

and attention

to detail

when reviewing documents prior to issue.

The following drawings

were

reviewed

and it was noted that

some erroneous

valve positions

had

been corrected

as requested

by the inspector:

2998-G-088,

Rev.

14 - Containment

Spray

I% Refueling Water Systems

(Unit 2)

8770-G-088,

Rev.

15 - Containment

Spray

5 Refueling Water Systems

(Unit 1)

0