ML17202U984

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Safety Insp Repts 50-237/91-06 & 50-249/91-06 on 910123-28. Violation Noted.Major Areas Inspected:Containment Integrated Leak Rate Test Programs
ML17202U984
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 02/06/1991
From: Lougheed V, Maura F, Phillips M, Salehi K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17202U983 List:
References
50-237-91-06, 50-237-91-6, 50-249-91-06, 50-249-91-6, NUDOCS 9102130017
Download: ML17202U984 (12)


See also: IR 05000237/1991006

Text

U. S ~ .NUCLEAR REGULATORY* COMMISSION

  • REGION III

Reports No. 50-237 /91006 (DRS) ; 50...,249/91006. (DRS)

Docket Nos.56-237; 5b-2~9

Licenses No. DPR-19; .DPR-:-25

Licensee:

Commonwealth Ediso.n Company

Opus West III

1400 Opus Place

Downers Grove, IL * 6*0515* * *.

Facilit:y Name:.*. Dr'esden Nuclear Power station,. Units 2 and 3

  • Inspectio.n At:

Dresden Site, Morris, Illinois

  • In~pection Conducted:

January 23-28~ 1991

Inspectorl:j: .

  • _~lJ1

...... 1'-+-/.*._. ;J

......._~ _____ * .

K.~J:f

. y;J~ LJ

~ . . p. ~(]heed

F .. A .. Maura

Approved By:~

.

  • M:P:Phi1,....i---=-ip.,.... -s-, -c-h-=-i-ef
  • operations Br_anch * ..

Inspection summary

Date'

1

  • .

3/~lrr/

Date 1

_)~ /9/

Dat!e.'

Date

Inspection* on Januarv 23-28, 1991 * (Reports No.** 50-237 /91006(DRS);

No. 50-249/91006(DRS))

.

Areas Inspected:

Special annotinc~d safe~~ inspection by regional

based inspectors of .the licensee's coritainment integ~ated leak

rate test (CILRT) *and local leak*. rate test .(LLRT) programs,

including review of *the events surrounding the failure of the

flange on the Torus Ptirge Exhaust Containment Isolation

Valve 2-1601-20A, and *the data acquisition system failure

during the verification portion of the CILRT~

Results:

The inspection resulted in one apparent yiolation

against Technical Specification 3/4.7.A.2 which requires that

containment integrity be maintained at all times when the* reactor

is critical.

Leakage from the*fla.nge, at accident pressure, was

conservatively calculated to be 65 weight percent per day, which

. was 41 .. times the allowable *. This apparent violation is described

in section 6 of ~his* report.

9102130017 910207

PDR

ADOCK 05000237

Q

PDR

Dresden Unit 2 had been granted a waiver of compliance until the

end of the cycle 12 refueling outage in regard to testing of the

Reactor Building.Closed Cooling Water System (RBCCW).

LLRT

results during the'* refueling *outage *showed that this penetration

was acceptable during .the previous. ope_rating cycle.

The licensee is conside~ed to have failed the CILRT in the

as-found condition, due to leakage 'from the inboard* flange o*n

valve 2-1601-20A *

I

'

"

DETAILS

.1.

Persons Contacted-

Commonwealth Edison

  • E. -Eenigenburg, Station Manager
  • J~ Geiger, Technical Staff, CILRT Lead Test Engineer
    • J .. Glover, Nuclear "Engineering Divi.s.ion, Corporate

CILRT Lead *

.

.

  • *L. ' Gerner, Technical Superintendent
  • M. Horbaczewski, T~chnical Staff Group Leader
  • G. Kusnik, Quality Control
  • D. Lowenstein, Regulatory Assura~~e Analyst
  • K. Peterman, Regulatory Assurance Supervisor
  • R. Williams, Senior Quality Assurance Inspector
    • K. Yates, Onsite Nuclear Safety Administrator

Illinois. Department of safety .

  • R. Zuf.fa, .Resident Inspector

U.S .. NRC

  • P* Hills, $enior Resident Inspector
  • M .. Peck, Resident Inspector
  • J. Monninger, Re$ident Inspector,*NRR
  • Attended exit.on January 28, 1991.

The inspectors-also interviewed other licensee employees*

during the course of the inspection~ including members of

the maintenance,'. quality. *control, and technical staff.

2.

Licensee Action on Previously Id~ntified Findings

a.

(Closed) Violation 50-249/90005-01 "Failure to Include

Service 'Air and Demineralized Water in Valve *Lineups":

The licensee revised the CILRT procedure to include

the above systems in the valve lineups.

The inspectors

reviewed the revised.proced~re*_and the test results and

  • had no further concerns.

This item.is *considered

closed.

b. *:(Closed> Unresolved Item 50-249/90005-02 "Status of

Small Diameter Pneumatic Tubing-Penetrating Drywell":

The licensee has completed their. evaluation of all

- containment -isolation boundaries and is in the process

of performing a final review prior to submittal to.NRR.

The particular lines in question were handled by

cutting and cappi.ng them, under the licensee's minor

design change program.

The work was accomplished on

Unit 2 during*the Wir:it~r.1990 refueling outage, and

.. ,

  • Cl

will be performed on Unit *3 during the*spring 1991

refueling outage.

The inspectors. reviewed the packages

and.discussed the post-modific~tion testing

requirements for *unit 3 with the licensee *. * (Post-

modifi9ation testing for Unit 2 *was accomplished

through the CILRT.)

The -inspectors had no problems

with'the licensee's solution for*th~ pneumatic lines.

This item is consideied closed.

3 -~*

Revi*ew of co~taihment Integrat~d *Leak Rate Test

Proc*edure (70307)

The 'inspector~ reviewed .*surveillance instruction DTS 1600-7,

"Unit 2/3 Integrated Primary *Containment Leak Rate Test,"

Revision 11, dated December 13, 1990,.relative to the

.z:equirements of _10 CFR Part 50 Appendix *J,. ANSI N45.5-1972,

and th~ licensee** s Technical -Specif icatioris. . The valve

  • 1ineup problems and fa'ilure *to require venting of some

systems as desci;-ibed in .. Inspection 'Reports

No. 50-237/90006(DRS); ~o. 50-249/90005(DRS) had been

resolved in this revision.

~he inspectors dia not identify

any further probl~ms with the procedure.

4.

Test Re~tilts ~vaiuation (70323)

a.

Review of Data Acquisition Problems Encountered During

the CILRT

During the pressurizat.ion' phase the licensee

experier1ced *a failure of* their Data Acquisition System

(DAS) due to the loss of incoming data information.

.

  • .:The licensee attributed this to wetting of 1;he amphenol

, connector. to the DAS computer.

.This same failure also

occurred during the verification portion of the CILRT,

causing the l.icensee to terminate the supplemental

test.

The inspectors discussed the cause of the

failure ~ith the licensee~ .. The apparent root cause was

due to a soap-water soluti.ori used to identify leaks

wetting the connector and *causing it to* *short. out.

The

soap-water solution was used to. check the* fittings on

the CILRT instrumentation penetrations.

Th*ese

penetrations, which exit containment through the

.

personnel airlock, were a source of leakage during the'

last Unit 3 CILRT~

In order to- ensure that a similar

leak did not. occur durin*g. the Unit 2 test, the licensee

used a new Conax fitting, which provided a tighter

se~l, and t6en checked 'for leakage using the soap-water

mixture.

The licensee state~ that excess solution ran

down the cable from t.he fitting to the connector.*

Since the connector was not designed to be water-proof,

the accumulated moisture caused the connector to fail *

  • Although the licensee carefully.dried the cable and

connector when *the.failure first occurred during

containment pressurization, the licensee speculated

..

b.

. c.

that sufficient ~~isture ag~in 6ollecied to cause the

failure during the supplemental .test.

The inspectors

also discussed with the-licensee the .intended

preventative measures to ensure that similar problems

did not occur in the future .. The inspectors reviewed

the collected ,.data during both failures and verified*

that it was not isolated sensor* failures, but a

  • complete failure of al'i sensors during :that time

period.

The licensee stated that they were*considering

tighter.controls on the use of-soap~water solutions on

electrical.connections as well as providing a

water-proof connector. - The inspectors had no further

questions in this area.

CILRT Data Evaluation

A six hour and ten minute CILRT was performed on Unit 2

on December 17. and 18,. 1990_. at a test pressure of 64. 4

psia following satisf~ctory completion of the required

. temperature stabilization period.

During the

-pressurization phase, the licensee experienced

excessive leakage from the inboard flange of the Torus

Purge Exhaust Containment Isolation Valve, 2-1601-20A.

An evaluation of this l.eakage is described in section 6

of this report~

Data were collected every 1.0 minutes.

The inspectors independently evaluated leak rate data

using total time

(BN~ToP-'1) formulas to verify the

  • licensee's calculations of the leak rate and instrument

performance.

There was good agreement between *the

inspectors' and licensee's results as indicated by the

following summary (units are -in weight percent per

day).

Measurement

Measured leak rate during

CILRT (Lam)

Lam at 95 percent Upper

.

Conf iqence Level (95% UCL) *

Licensee

Inspector

0.500

0.500

0.743

0.746

.The 'Appendix J acceptance criterion is that Lam, at the

95% upper confidence -level (UCL), be less than 0.75 La

(i.2 wt%/day).

The test.met this crite~ion.

supplemental Test Data Evaluation

After satisfactory completion o.f . the CILRT, a known

),eakage rate of 13 scfm, equivalent to 1.53 wt%/day was

induce*d *. _The inspectors noted ~hat the licensee

corrected* the reakage rate for containment temperature

and volume changes at the time of the test.

These*

corrections were conservatiye in nature and resulted

'

_.

_, ..

.;,

in.a higher flowrate than the methodology used by the

inspectors.

Since both the inspectors' and the

licensee's calcui'ated induced leakage rates were within

the band specified by Appendix.J, the method was

  • . considered acceptable.

The Bechtel test method, described in BN-TOP-1,

requires a one hour stabilization perioc:l* b.etween the

time when *the known flowrate is induced and when the

supplementai'test*is started.* It also requires that

the supplemental test be at least half of the main test

in length.

The licensee commenced the supplemental

test following the one hour stabilization period

required by BN-TOP-L

Data were collected and analyzed

by the licensee every 10 minutes.

After approximately

two and a ha:J.f hours, the licensee's instrumentation

malfunction~d.

Th.e cause of this malfunction is

described in sectiori 4_.a above.

In order to obtain the

required* three hour verification period, the. 'licensee

requested from Region III that they be allowed to

include the one hour.stabilization period in the

supplemental test data.

The inspectors calculated 'the

supplemental test leakage rate, both with and without

the stabilization period data.

All data units are in

.weight pe~c~nt_ per day (wt%/day) *

Measurement

Measured leakage rate (Le)

during supplemental test,

stabilization data not

included*

Measured leakage rate'. (Le I°) _

during supple.mental test, .* ... :

stabilization data included

Induced Leakage Rate (Lo)

Results from main test _

(Lam)

.

Le*- (Lo+ Lam)

Le '

..:. (Lo + Lam)

Licensee

Inspector

1. 756

1. 754

1.814*.

1.812

1.556

1.533

0.500

0.500

-0.300

'.""'0.279

-0.242

-0.221

The.Appendix J acceptance criterion is that the value

of [Le -

(Lo+ Lam)) be within a band of+/- 25 % of La.

For Dresden, this results in an acc~ptance ~riterion of

.;..0.400 < [Le -

(Lo+ Lam)) < 0.400.

The supplemental

test results fell within the band, for both the cases

using the stabilization data ,and those without.

.

-,,

d.

.

The inspectors noted:that the last five data points

during the s_upplemental test* showed a decreasing trend.

Normaliy, *.the NRC expects the verification* results to

stabilize within the band before the test is .

terminated.

In this case,* since.the test was

terminated due to *equipment malfun*ction, the inspectors.

agreed, for this supplemental test only, to accept the

results as valid as long as all.of the points remained

.within tbe acceptance band ..

. CILRT Volume Change Corrections

'

At.the completion of the CILRT and the supplemental

test, the licensee was required to make corrections to

the calculated Lam at the 95% UCL due to changes in

volume of *various* water sources inside containment.

The following.corrections to Lam were recorded and

calculated by the licensee, with the calculations being

verified by* the ,inspectors:

-Water Source

Change in Volume

Equipment Drain Sump

.48 cubic feet

Floor Drain sump,

4*a cubic feet

prywell_ -. Floor

146 cubic feet

The' level at the beginning of the CILRT was 2.67 feet

in both sumps, and at the* end of the test both sumps

were full, with an additional inch of water on the

drywell'basement floor.

The* sumps are six-feet by six

'feet by four feet deep.

The drywell basement has a

radius of 23 .. 6 feet. *The licensee had not identified

the source of the water at.~he time of the inspection.

The total volume change due to water inleakage was

242 cubic feet which corresponds to o.*020 wt%/day.

This results in a total leakage, at the 95% UCL, of

o.766 wt%/day, which is under the maximum allowable of

1.2 wt%/day.

e.

CILRT Valve.Lineup Penalties

Due. to vaive:*configurat.j.ons which deviated from the

ide_al penetration v~l ve 1 ineups for the CILRT, the

  • I

I

~'

,: f

. '*

f .

res.ul ts of LLRTs for ~uch* penetrations must be added as

a penalty to Lam at the 95% UCL, per Appendix J *. The

licensee h~d the following penetrations in a

configuration which differed from that which would be

experienced post acciden*t:

X-101

  • X-107A,B

X-116A,B

X-119

x~l49AiB:

X-15bA

X-109A B

.

I

X-122

X-310A,B

X-lllA,B

X-138

X-JllA,B

X-113

X-:J..45A,B

  • Addition of the as-left minimum pathway LLRT result for

the non-vented penetrations added a penalty of 25.9

scfh to the 95%' UCL limit.* .This leakage was equivalent*

to 0.051 wt%/qay, resulting in a final as-left limit of

0.817 wt%/day."

This value was within the acceptance

'criterion (Lam< 1.2 wt%/day).

The licensee added an

add~tional 2 scfm penalty to its calculations~

~his

was-due*to the CILRT procedure listing service air as

-~*non-vented penetration.

Service air was properly:

vented during the CILRT, however the licensee failed

to remove it from th~ table,*~nd decided to take.the

"additional penalty as *<<;i conservative measure *. This

  • penalty* added approximately* o. !)04 wt%/day to the total

and was negligible.

As-Found Condition of Containment

The* as-found condition is* the co.ndition of the

containment at the beginning of the outage prior to any

repairs .or: adjustments to the containment boundary!

This is calculated by reviewing the summary of the

LLRTs and calculating:the amount of leakage rate

improvement dq.e to .r~pairs ;or adjustments using the

minimum pathway methodology.

The inspectors reviewed

the licensee's local leak rate re~ults to ensure that

the minimum pathway *repairs and adjustment calculations

were correctly performed. * The inspectors determined

that these corrections.were worth 140 scfh which

corre.sponds' *to O ;*275 *wt%/ day.

Adding this to the final

as-left tot:al would, have resulted in an as-fo.und leak

rate of 1.092 wt%/day, exclusive of the 2-1601-20A

flange leakage.

Howev:er, due* to the excessive leakage

  • from the flange, the CILRT ;was considered to have

failed in the as-found condition.

5.

Review of Local Leak Rate Test.Res~lts (61720)

a.

.R~v.:i..ew of* Proposed Dresden Primary.Containment Pathways

Document

      • *

The inspectors performed a cursory review of *the

licensee's -proposed DresdEm* primary contai,nment

0

pathways document issued by the corporate (Nuclear

Engineering Division) off.ice on November 19, 1990.

The

licensee stated that the current status of the document

was that it was being reviewed by the on-site technical

staff.

Following this* review, the document would be

reviewed.and* approved by the Onsite Review Group.

It

would then*be submitted to NRC -

NRR for review and

approval concurrently.with the .Quad Cities document.

The inspectors noted. that this document failed to

identify the requirement.to test the inboard flanges

of the purge . valves. _ No other problems were noted.

b.

Review of Local *Leak Rate Test Results

The* inspectors i::-eviewed* the licensee's LLRT procedure,

DTS 1600-1, "Local Leak* Rate Testing of Primary

Containment Isolation Valves," Revision 14 dated

September 24, 1990.

The inspectors noted that the

.licensee had completely revis.ed the d.ocument to resolve

the concerns discussed .. in Inspection Report 50-

237/90006 (DRS); 50-249/90005(DRS).

The inspectors also

reviewed the licensee's- LLRT data. *The licensee

performed the majority. of the LLRTs by using the flow.

makeup method.

This allowed *.for more accurate

representation of the* actual penetration leakage rates.

The inspectors noted that the licensee still tended to

p*ressurize the penetrations in excess of Pa ( 48 psig) .

This was especially true when the licensee had to

account*for a water head on one side of the penetration

and *was'using an increased test pressure to.overcome

the water pressure, which often resulted in a

differential pre~sure of- greater than Pa on the

penetration.

This was discussed with the licensee, and

the licensee agreed to keep future -tests closer to Pa.

The inspectois particularly revie~ed the results for

penetr~tions x~123 and X-124 for the Reactor Building

Closed Cooling Water '(RBCCW) system.

The licensee had

obtained a wa.iver of Compliance for the previous outage

from including these penetrations in calculating their

0.6 La total. *The inspectors noted that these

penetrations. ha*d acceptable LLRT results ( o. 4 and

14.6 scfh, respectively, in.the as-found condition.)

The inspectors had no further problems in this area.

'.

6.

Review of Ev.ents surrounding the Failure of Valve 2-1601-20A

(93702) .

On December 17, 1990, the* licensee began the pressurization

of containment in order to perform the CILRT.

A review of

the test log and discussions* with test personnel indicated

.. that at approximately 6: 30 on tbe morning of the 17th, with

the containment pressure at approximately 15 psig, a* loud

"pop" was heard, followed by a *~~siren-like sound".

Upon

  • '.

further inspection1* the licensee found the. leakage to be

.

occurring past the inboard.flange on the Torus Purge Exhaust*

'Containm~nt Isolation Valve 2-1601-20A.

The licensee

stopped-the air compressors, obtained approximately.ten data-

point~ prior.to tightening the flange bolts thereby *

eliminating the leak, and recommenced the CII,.RT

pressurization~ The licensee s.ubsequently *e:o:rnpleted the

CILRT with satisfactory results as discussed in section

  • ,4. o,

above~ :The inspectors had no concern . with these short-

.. term corrective actions.**

On December.18,* 1990, the*licens~e reviewed. the maintenance

history on the 2-1601:-20A v~lve and.determined that the

valve had not been w.orked on *since the last. refueling

outage, at which time the valve was replaced.

Upon making

this determination, the lic~nsee reported the event to the

NRC under. 10 CFR 50. 72 (b-) (2). (i).

This was subsequently

followed by.Licensee Event* Report LER-~0-018 which was

issued on January .i4, 199_1_.

The inspectors review*ed the work history of the valve and

flange.

The valve was replaced under nuclear work request 67528 in February 1.989.

Fol.lowing replacement of the valve,

a LLRT was performed by pressurizing between the 2-1601-20A

valve and check valve 2-1601-31A.

This test, which was the

licensee's normal LLRT method, tested the 2-l.601-20A valve

seat, p~cking,*and outboard flange as well as operation of

the check valve.

How~ver, it .failed to test the inboard

flange as required by paragraph IV.A of 10 CFR Part*50,

Appendix J.

This testing omission was no.t recognized by any

of the licensee personnel involved in development of the

work package, maintenance work_ activities, or conduct of the

post-maintenance t~st.

Following satisfactory completion of

the LLRT, as well as other required valve surveillances, the

valve was returned to operation. * On ,February 19, 1989,

Dresden.Unit 2 went critical following completion.of their

refueling out~ge.

The plant remained basical'ly in operation

until they shutdown for refueling in September 1990.

In order to obtain an estimate of *the leakage through the

flange, the inspectors calculated the leakage rate at

15 psig* using the ten data .points supplied by the licensee.

Using point to point test methodology, the*inspectors

calculated that the leakage rate through.the flange was

within the range of 23.8 to*_.24.6 wt%/day at a* test pressure

of 15 psig.

The inspectors then-corrected the leak rate

to the design pressure*(48.psig).

This involved both a

correction to the test mass and.pressure.

In regard to the

mass change, the calculation was base¢! on the ideal ga's law.

This result was then utilized in the pressure correction

calculation.

In.this.case, calculations were performed

using both a formula described in the licensee's local leak

rate procedures, which., yielded a result of 31 wt%/day; and a

formula developed by the Franklin Rese~rch Institu.te for the

.t

NRC, which yielded a result of 65 wt%/day.

~he later

formula assumes a capillary, or non-orifice, type leakage,

such* as would be the ~ase for leakage through a flange, ahd

the former Gase .~s based on flow through an orifice.

Neither calculation assumed that the size of the opening

  • would *enlarge due to increasing*pressure, although that

might be physically.realistic,* if the gasket material was

displaced due. to the, .increased air flow at higher pressures.

At the conclusion of the inspection, the licensee was in the

_process. of performing calculations to better quantify the

leakage at.design pressures.

Th~ inspectors noted that all.

of these values were considerably in excess of the design

allowable of 1.6 wt%/day and that either method of

extrapolating the leakage rate to design pressure resulted

in undesirable leakage rates.

At the time. of the inspection, the licensee had not

completed fts evaluation of the ef.fect of these leakage

rates upon 'the dose releases following a design basis loss

of coolarit accident~* Although direct *1inear interpolations

are not necessarily accurate, the inspectors noted that the

flange leakage rates were five to ten times greater than

tho~e utiiized in th~ dose calculations presented by the

licensee during an enforcement conference concerning opening

ot sampling valves held on October 12, 1990 (EA 96-168).

Those results .are contained as attachments to Dresden

Inspection Reports No. S0-237/90025(DRP);

No. 50-249/90024(DRP).

The inspectors*conducted numerous interviews to determine

  • the root cause of the failure.

This event :appeared to

originate in the maintenance program involving installation

of flanged valves.

The inspectors noted that there were no

acceptance criteria for tightening of the flange bolts as

they w,ere replaced.

The licensee had considered this

activity to be within the realm of "skill of the craft."

Discussions with the maintenance department indicated that.

the *bolts were tightened through use of a slugging wrench.

This involved tightening the bolts by hammering' the wrench

until the bolts'would not turn any further.

A.maintenance

worker also indicated th.at there was not a good fit between

the pipe and the valv~ at the time of installation that may

have contributed to the problem.

In addition, as discussed

above, the post-maintenance test did not challenge the

flange so that the. failure to completely tighten the flange .

. was not identified subsequent to* .,the valve installation and

prior to its being returned to service.

Although the

licensee installed eight similar valves with sixteen similar

flanges during the prior refueling outage, this was _the only

flange that leaked.

7.

. I

The inspectors noted_ that the iicensee, at the Quad Cities

N:uclea:r Station, had previously been notified that the

inside flanges of the purge* valves were part of the

containment boundary and that Type C testing* between the

containment .isolation :valves did.not challenge these

flanges. (See Inspection~eports No. 50-254/89024(DRS);

No. 50-2G5/89024(DRS) .issued on June 15, 1990).

Since Quad

cities was on an accelerated test program such that it

performed a CILRT every outage, no actiorr was required at

that site.

During the Dresden inspection, the inspectors*

~pecif ically discussed _with the licensee the. Appendix J

requirement to test the flanges was **similar to that for

other containment isolation valves and needed to be

performed every refueling outage rather than just following

maintenance. * The license~ acknowledged this requirement and

stated that the flanges would be properly tested. during *

. 'future* outages.

Te'chnical Specification 3.7.A.2 requires, in part, that

pi;-imary containment integrity be maintained whenever the

reactor is critical. Section 3.7.A.2.a.(3) defines the

maximum allowable leakage rate (La), at a. pressure o.f Pa,

as equal to 1.6 percent by weight of the containment air

per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at 4B psig.

Technical Specification section 3.7.A.2.b states, in part, that, when containment

integrity is required, primary leakage rates will-be limited

. to an overall integrated leakage rate of less than or equal

to 75 -percent of La.- Operation of Dresden Unit 2 over a

'complete operating cycle from February 1989 until

September 1990, with the inboard flange of containment

isolation valve 2-1601-20A having a calculated leakage of

approximately 65 wt%/day at 48 psig, is an apparent

.*violation of Technical Specification 3.7.A.2

( 50-237 /91006--01 (DRS)) * .

.

Exit Interviews

The inspectors met.~ith licerisee representa~ives (denoted in

section 1) throughout _the inspection.

An exit meeting was

held prior to leaving the.site on January 28, 1991.

The

inspectors summarized the scope of the inspection and the.

apparent findings.

The* licensee.acknowledged these

findings.

  • . The inspectors also discussed the likely

informational content of the insp~ction report with regards

to documents or processes reviewed by the inspectors during

the inspection .. The licensee did not identify any such

documents or processe~ a_s proprietary .