ML16342D247

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Insp Repts 50-275/96-04 & 50-323/96-04 on 960226-0301.No Violations Noted.Major Areas Inspected:Radioactive Effluent Mgt Program
ML16342D247
Person / Time
Site: Diablo Canyon  
Issue date: 03/19/1996
From: Murray B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D248 List:
References
50-275-96-04, 50-275-96-4, 50-323-96-04, 50-323-96-4, NUDOCS 9603260122
Download: ML16342D247 (16)


See also: IR 05000275/1996004

Text

ENCLOSURE

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-275/96-04

50-323/96-04

Licenses:

DPR-80

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Streets

Room 1451

P.O.

Box 770000

San Francisco,

California

Facility Name:

Diablo Canyon Nuclear

Power Plant, Units

1 and

2

Inspection At:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

February

26 through March 1,

1996

Inspector:

L. T. Ricketson,

P.E..

Senior Radiation Specialist

Plant Support

Branch

'

Approved:

a

e

urray,

ie

,

an

uppor

rane

Division of Reactor

Safety

Ins ection

Summar

Areas

Ins ected

Units

1 and 2:

Routine,

announced

inspection of the

radioactive effluent management

program including:

audits

and appraisals

~

program changes,

process

and effluent monitors,

dose commitment,

engineered

safety feature air cleaning systems.

training and qualifications,

effectiveness

of licensee controls,

followup on previous violations,

and

a

review of the Updated Final Safety Analysis Report was conducted.

Results

Units

1 and

2

~P1 tt

t

Adequate oversight of the radioactive effluent management

program was

implemented.

Thorough audits were performed

by the quality assurance

organization

on an annual

basis:

however, additional oversight

by means

of quality assurance

survei llances

was minimal (Section

1. 1).

A good program was in place to response test

and calibrate liquid and

gaseous

radioactive effluent monitors (Section 1.3).

9603260i22

960320

PDR

ADOCK 05000275

6

PDR

-2-

~

A good effluent management

program was implemented.

Sampling and

analyses

of effluent streams

were performed

as required,

and offsite

doses

were well below Technical Specification limits (Section 1.4).

~

A good program

had been established

concerning inplace and laboratory

testing of engineered

safety feature air cleaning

systems

and system

adsorbers.

The use of conservative

laboratory testing methodology

indicated

good management

support for the air clean

systems

program

(Section 1.5).

~

Chemistry personnel

participating in the effluent management

program

were appropriately trained

and qualified for the tasks

performed

(Section 1.6).

~

An effective corrective action program was in place to document

and

correct problems associated

with the areas

inspected

(Section 1.7).

Summar

of Ins ection Findin s:

~

Violations 323/9311-02,

323/9311-03,

and 323/9311-04

were closed

(Section 2).

Attachment:

~

Attachment

- Persons

Contacted

and Exit Meeting

-3-

DETAILS

RADIOACTIVE WASTE TREATMENT AND EFFLUENT MONITORING

(84750)

1.1

Audits and

A

raisals

The inspector

reviewed various assessment

activities to verify compliance with

Technical Specification 6.5.3.8

and agreement with the commitments in

Chapter

17 of. the Updated Final Safety Analysis Report.

The inspector

reviewed the 1994 and

1995 quality assurance

audits of the

radioactive effluent management

program

and noted that the audit team included

several

people with experience

related to area of review.

The inspector also

noted that the audit identified several

deficiencies in the effluent

management

program.

Audit findings were appropriately

addressed

by the

chemistry department.

The auditors

concluded that,

".

.

. while many areas of

the offsite dose calculation procedure

and radiological effluents programs

are

well run

~ increased

management

attention is warranted in the areas of

procedural

compliance,

commitment tracking and implementations

and attention

to detail."

Because of the conclusion

reached,

the inspector

asked if

subsequent

survei llances or observations

were performed

by the quality

assurance

organization to increase

management

oversight.

Quality assurance

representatives

stated that,

other

than for the purpose of verifying that

actions

were implemented to correct audit findings'o additional quality

assurance

reviews or assessments

were conducted in the area of radioactive

effluent management.

Quality assurance

personnel

indicated that the lack of

supplemental

assessments

during the remainder of the year was linked to the

quality assurance

staffing level.

The staff was fully utilized fulfilling

regulatory commitments.

The inspector also confirmed that there

had been

no

other independent

assessments

of the radioactive effluent management

program.

The inspector

concluded that the audits were thorough reviews.

Followup of

selected

items by the inspector

did not identify a recurrence of the problems

identified by the audit.

Based

on the strength of the annual audits,

the

inspector concluded that oversight of the effluent management

program was

adequate.

1.2

Pro

ram Chan

es

There were no major changes to the organization or program other than the

plant wide down-sizing.

The inspector noted

no problems attributable to the

reduction in staff.

In accordance

with Generic Letter 89-01. the licensee

removed

requirements'elating

to effluent management

and effluent monitoring from the Technical

Specifications.

However, the licensee's

license

amendment

deviated slightly

0

from the guidance

included with the gener ic letter.

Instead of relocating the

radiological effluent technical specifications to a single document

known as the Offsite Dose Calculation Manual, the licensee

relocated the

information into five documents

consisting of policy directives,

interdepartmental

administrative procedures,

departmental

administrative

procedures,

and implementing procedures.

These

documents

included:

CY2. ID1. "Radiological Monitoring and Controls Program"

CY2. IDl, "Radiological Environmental Monitoring Program"

CY2, "Radiological Effluent Control Program"

CAP A-8, "Offsite Dose Calculation Procedure"

TES A-7 ~ "Environmental Radiological Monitoring Procedure"

The inspector

reviewed these

documents

and commented to licensee

representatives

that identifying program requirements

appeared

cumbersome.

Licensee representatives

acknowledged this and stated that the licensee

planned to submit

a license

amendment

request,

by January

1,

1997. that would

allow it to use standard

Technical Specifications.

In doing so, the licensee

would adopt the use of a single document

known as the Offsite Dose Calculation

Manual

and simplify the process of identifying and following program

requirements.

The inspector stated that the change

would be reviewed during

a

future inspection.

Changes to the procedures

were included in the annual effluent reports,

as

required

by Technical Specification

6. 14.

The inspector

reviewed the changes

and determined that they did not merit further discussion.

1.3

Process

and Effluent Radiation Monitorin

The inspectors

reviewed the use,

response testing,

and calibration of effluent

monitors

and interviewed personnel

from the chemistry department

and the

engineering

services

group to determine

compliance with the requi rements in

Section

6 of CY2. IDl, "Radiological Monitoring and Controls Program,"

and

agreement with the commitments in Sections

11.2,

11.3

~

and 11.4 of the Updated

Final Safety Analysis Report.

The inspector

reviewed the licensee's

methodology for determining radiation

monitor setpoints

and verified that the proper setpoints

were installed for

selected effluent radiation monitors.

The inspector

reviewed calibration records of liquid and gaseous

effluent

radiation monitors

and confirmed that the calibrations

had been performed at

the requi red intervals.

Radioactive

sources of appropriate

geometry

and

energies

were used for the calibrations.

The inspector confirmed that the licensee

maintained

a program to correlate

radioactive effluent sample analyses

results to continuous monitors'eadings.

as described

in Regulatory Guide 1.21, Section C.5.

-5-

1.4

Dose Commitments

The inspector

reviewed the

1993 and

1994 annual effluent reports

and verified

that the licensee

complied with the dose

commitment limits of Section

6 of

CY2. 101, "Radiological Monitoring and Controls Program."

No observation of sampling

and analysis,

release

permit preparation,

or

operational effluerit releases

was performed

by the inspector during the

inspection period because

no releases

were conducted

by the licensee.

The

inspector

reviewed selected

examples of previous release

permits

and examined

post release

dose calculations

and identified no problems.

1.5

Air Filtration S stems

The inspector

reviewed records of surveillance testing,

performed walkdowns of

air cleaning systems,

and interviewed systems

engineering

personnel

to

determine compliance with the requirements of Unit 1 Technical Specifications 4.7.5, 4.7.6.

and 4.9. 12 and agreement with Updated Final

Safety Analysis Report Sections

9.4. 1, 9.4.2,

and 9.4.4.

With licensee

representatives.

the inspectors

performed walkdowns of air

cleaning

systems

in Units

1 and 2.

The units observed

included those for the

control

rooms,

the auxiliary building,

and the fuel handling areas.

No

problems involving the physical conditions of the air cleaning

systems

were

identified.

The inspectors

reviewed records of in-place testing of high efficiency

particulate air filters and charcoal

adsorbers

as .well as laboratory tests of

charcoal

samples

and found that those

systems

required

by Technical

Specifications

had been tested at the proper interval.

Testing

and charcoal

sampling were performed

by the licensee's

systems

engineer s.

Laboratory

testing of charcoal

samples

was performed

by a vendor.

The inspectors

reviewed air cleaning

system surveillance

procedures

and

determined that the procedures

incorporated

guidance

from ANSI 510-1980,

"Standard for Testing of Nuclear Air Cleaning Systems." to ensure that inplace

and laboratory testing of filters and adsorbers

were performed properly.

During the first half of 1994, the licensee

changed

laboratory charcoal

testing criteria from that of ASTM D3803-1979 to that of ASTM D3803-1989.

The

later criteria is more conservative

because it requires

charcoal to be tested

at 30 degrees

Celsius;

the 1979 criteria allowed testing of charcoal

at

80 degrees

Celsius.

The licensee initiated Licensee

Event Reports

2-94-003-01

and 2-94-005-00

when

it was determined that charcoal

samples

from the auxiliary building and the

fuel handling building, respectively,

did not meet the acceptance criteria of

ASTM D3803-1989

and, therefore,

they did not comply with Technical Specifications 4.7.6 and 4.9.12.

The licensee

had similar samples

tested to

the criteria in ASTN 03803-1979,

and the charcoal

samples

met the older

acceptance criteria.

It was determined,

that when the charcoal

was heated to

a higher temperature,

potential pollutants were driven off.

This allowed

a

greater

amount of the surface

area to become

exposed

again,

and the test

results indicated

a greater organic iodine adsorption

and

a lower penetration

level.

The licensee

replaced

the charcoal

in the auxiliary building and the E-5

absorber

bank in the Unit 2 fuel handling building and

made information

available to inform other sites of the licensee's

experience.

The inspector

determined that the licensee

acted conservatively in selecting to follow the

guidance in the latest testing standard

even though it resulted in the

accelerated

changeout of the charcoal

adsorber.

This indicated strong

management

support for this area of inspection.

1.6

Trainin

and

ualifications

The inspector determined that release

permits were prepared

by chemistry

foremen.

The inspector

reviewed selected

records of training and confi rmed

that all individuals reviewed

had successfully

completed

both formal and

on-the-job trai ning requirements

and were qualified to performed

such tasks.

1.7

Effectiveness of Licensee Controls

The inspectors

reviewed examples of action requests

related to radioactive

effluent and air cleaning

system activities.

The corrective actions

addressed

the identified causes.

Responses

to conditions

from the responsible

groups

were made in a timely manner.

2

FOLLOWUP

(92904)

2.1

Closed

Violation 323/9311-02:

No Pro

ram for Post Accident

Sam lin

S stem Reactor

Coolant

H dro en

The inspector

verified. through document

review, that the licensee

implemented

the corrective actions listed in the June

22,

1993, reply to the Notice of

Violation.

2.2

Closed

Violation 323/9311-03:

Failure to Perform 50.59 Evaluation for

Post Accident

Sam lin

S stem

The inspector verified that the licensee

implemented the corrective actions

listed in the June

22,

1993, reply to the Notice of Violation.

2.3

Closed

Violation 323/9311-04:

No Pro ram for Post Accident

Sam lin

S stem Plant Vent Iodines

and Particulates

The inspector verified that the licensee

implemented the corrective actions

listed in the June

22,

1993, reply to the Notice of Violation.

3

REVIEW OF UPDATED FINAL SAFETY ANALYSIS REPORT COMHITHENTS

A recent discovery of a licensee

operating their facility in a manner contrary

to the Updated Final Safety Analysis Report description highlighted the need

for a special

focused

review that compares

plant practices,

procedures

and/or

parameters

to the Updated Final Safety Analysis Report description.

While

performing the inspections

discussed

in this report, the inspector

reviewed

the applicable portions of the Updated Final Safety Analysis Report that

related to the areas

inspected.

The inspector verified that the Updated Final

Safety Analysis Report wording was consistent with the observed plant

practices,

procedures

and/or parameters.

ATTACHMENT

PERSONS

CONTACTED

1. 1

Licensee

Personnel

R. Allen, Engineer,

Engineering Services/Balance

of Plant

K. Brieze, Auditor, Quality Assurance

D. Chen,

Chemist,

Chemistry and Environmental

Operations

J. Gardner,

Senior Chemical

Engineer,

Chemistry and Environmental

Operations

  • C. Harbor,

NRC Interface,

Regulatory Services

~J.

Hays.

Oi rector',

Chemistry and Environment

Operations

  • J. Knemeyer,

Chemical

Engineer,

Chemistry

and Environmental

Operations

  • F. Ling, Engineer,

Engineering Services/Balance

of Plant

  • K. O'eil, Engineer,

Engineering Services/Instruments

and Controls

  • R. Powers,

Acting Plant Manager

  • R. Waltos, Director, Engineering Services/Balance

of Plant

  • J. Young, Director, Quality Assurance

1.2

NRC Personnel

  • M. Tschi ltz, Senior Resident

Inspector

S.

Boynton, Resident

Inspector

  • Denotes personnel

that attended

the exit meeting.

In addition to the

personnel

listed, the inspector contacted other personnel

during this

inspection period.

2

EXIT MEETING

An exit meeting

was conducted

on March 1,

1996.

During this meeting,

the

inspector

reviewed the scope

and findings of the report.

The licensee did not

express

a position on the inspection findings documented

in this report.

The

licensee did not identify as proprietary,

any information provided to, or

reviewed

by the inspector.

/j