Letter Sequence Response to RAI |
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MONTHYEARDCL-14-018, License Amendment Request 14-01, Revision to Technical Specification 3.8.1, AC Sources - Operating.2014-03-27027 March 2014 License Amendment Request 14-01, Revision to Technical Specification 3.8.1, AC Sources - Operating. Project stage: Request ML14122A3622014-05-0202 May 2014 Acceptance Review of LAR Regarding Revision to Technical Specification 3.8.1 Project stage: Acceptance Review ML14303A2572014-10-27027 October 2014 ISFSI - Response to Requests for Clarification of October 6, 2014 RAI Responses Concerning Emergency Planning Exemption Request Project stage: Other ML15029A6642015-01-29029 January 2015 NRR E-mail Capture - Diablo Canyon Power Station, Units 1 and 2 - Requests for Additional Information (Rais) for License Amendment Request 14-01 Associated with Revision to TS 3.8.1, AC Sources - Operating Project stage: RAI DCL-15-022, Response to NRC Request for Additional Information Regarding License Amendment Request 14-01 Revision to Technical Specification 3.8.1 'Ac Sources - Operating2015-02-19019 February 2015 Response to NRC Request for Additional Information Regarding License Amendment Request 14-01 Revision to Technical Specification 3.8.1 'Ac Sources - Operating Project stage: Response to RAI ML15089A1552015-03-25025 March 2015 NRR E-mail Capture - Diablo Units 1 and 2 - (Round 2) Requests for Additional Information (Rais) for License Amendment Request 14-01 Associated with Revision to TS 3.8.1, AC Sources - Operating Project stage: RAI DCL-15-052, Response to NRC Request for Additional Information Regarding License Amendment Request 14-01, Revision to Technical Specification 3.8.1, AC Sources - Operating.2015-04-29029 April 2015 Response to NRC Request for Additional Information Regarding License Amendment Request 14-01, Revision to Technical Specification 3.8.1, AC Sources - Operating. Project stage: Response to RAI ML15162A8822015-07-0101 July 2015 Issuance of Amendment Nos. 218 and 220, Revise Surveillance Requirements in TS 3.8.1, AC Sources, Related to Diesel Generator Testing Project stage: Approval 2015-01-29
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Category:Letter type:DCL
MONTHYEARDCL-24-010, Nuclear Material Transaction Report for New Fuel2024-01-29029 January 2024 Nuclear Material Transaction Report for New Fuel DCL-24-009, Nuclear Material Transaction Report for New Fuel2024-01-17017 January 2024 Nuclear Material Transaction Report for New Fuel DCL-24-008, Schedule Considerations for Review of the DCPP License Renewal Application2024-01-17017 January 2024 Schedule Considerations for Review of the DCPP License Renewal Application DCL-24-004, Supplement to License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2024-01-15015 January 2024 Supplement to License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b DCL-23-129, Nuclear Material Transaction Report for New Fuel2023-12-27027 December 2023 Nuclear Material Transaction Report for New Fuel DCL-23-122, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-12-14014 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation DCL-23-128, Emergency Plan Update2023-12-13013 December 2023 Emergency Plan Update DCL-23-125, Core Operating Limits Report for Unit 1 Cycle 252023-12-0606 December 2023 Core Operating Limits Report for Unit 1 Cycle 25 DCL-23-121, Supplement to License Amendment Request 23-03, Revision to Technical Specification3.7.8, Auxiliary Saltwater System2023-11-16016 November 2023 Supplement to License Amendment Request 23-03, Revision to Technical Specification3.7.8, Auxiliary Saltwater System DCL-23-120, License Amendment Request 23-03 Revision to Technical Specification 3.7.8, Auxiliary Saltwater (Asw) System2023-11-14014 November 2023 License Amendment Request 23-03 Revision to Technical Specification 3.7.8, Auxiliary Saltwater (Asw) System DCL-23-118, License Renewal Application2023-11-0707 November 2023 License Renewal Application DCL-2023-520, Discharge Self-Monitoring at Diablo Canyon Power Plant (DCPP)2023-10-19019 October 2023 Discharge Self-Monitoring at Diablo Canyon Power Plant (DCPP) DCL-23-103, Independent Spent Fuel Storage Installation - Withdrawal of License Amendment Request 22-01, Request for Approval of Alternative Security Measures for Early Warning System2023-10-13013 October 2023 Independent Spent Fuel Storage Installation - Withdrawal of License Amendment Request 22-01, Request for Approval of Alternative Security Measures for Early Warning System DCL-23-092, Material Status Report for the Period Ending August 31, 20232023-09-28028 September 2023 Material Status Report for the Period Ending August 31, 2023 DCL-23-077, License Amendment Request 23-02 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors2023-09-27027 September 2023 License Amendment Request 23-02 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors DCL-23-083, Upcoming Meeting with Nuclear Security and Incident Response Staff2023-09-13013 September 2023 Upcoming Meeting with Nuclear Security and Incident Response Staff DCL-23-078, Nuclear Material Transaction Report for New Fuel2023-09-0606 September 2023 Nuclear Material Transaction Report for New Fuel DCL-23-070, Withdrawal of Request Regarding Senior Reactor Operator License Application2023-08-16016 August 2023 Withdrawal of Request Regarding Senior Reactor Operator License Application DCL-23-068, Nuclear Material Transaction Report for New Fuel2023-08-0909 August 2023 Nuclear Material Transaction Report for New Fuel DCL-23-066, Nuclear Material Transaction Report for New Fuel2023-08-0303 August 2023 Nuclear Material Transaction Report for New Fuel DCL-23-065, Letter DCL-23-065 Request That Exam Material Be Withheld from Public Disclosure2023-07-27027 July 2023 Letter DCL-23-065 Request That Exam Material Be Withheld from Public Disclosure DCL-23-064, Nuclear Material Transaction Report for New Fuel2023-07-26026 July 2023 Nuclear Material Transaction Report for New Fuel DCL-23-054, License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2023-07-13013 July 2023 License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b DCL-23-055, Nuclear Material Transaction Report for New Fuel2023-07-0606 July 2023 Nuclear Material Transaction Report for New Fuel DCL-23-042, Independent Spent Fuel Storage Installation, Submittal of Quality Assurance Program Description, Revision 02023-05-24024 May 2023 Independent Spent Fuel Storage Installation, Submittal of Quality Assurance Program Description, Revision 0 DCL-23-032, Independent Spent Fuel Storage Installation Docket No. 72-27, Materials License Number SNM-2514 Humboldt Bay Independent Spent Fuel Storage Installation - NRC Requested Notification of Withdrawal from Voluntary Program2023-05-22022 May 2023 Independent Spent Fuel Storage Installation Docket No. 72-27, Materials License Number SNM-2514 Humboldt Bay Independent Spent Fuel Storage Installation - NRC Requested Notification of Withdrawal from Voluntary Program DCL-23-041, 10 CFR 50.46 Annual Report of Emergency Core Cooling System Evaluation Model Changes for Peak Cladding Temperature for 20222023-05-22022 May 2023 10 CFR 50.46 Annual Report of Emergency Core Cooling System Evaluation Model Changes for Peak Cladding Temperature for 2022 DCL-23-038, Revision to the Unit 1 Reactor Vessel Material Surveillance Program Withdrawal Schedule2023-05-15015 May 2023 Revision to the Unit 1 Reactor Vessel Material Surveillance Program Withdrawal Schedule DCL-23-034, 2022 Annual Nonradiological Environmental Operating Report2023-05-0101 May 2023 2022 Annual Nonradiological Environmental Operating Report DCL-23-036, 2022 Annual Radiological Environmental Operating Report2023-05-0101 May 2023 2022 Annual Radiological Environmental Operating Report DCL-23-025, 2022 Annual Radioactive Effluent Release Report2023-05-0101 May 2023 2022 Annual Radioactive Effluent Release Report DCL-2023-512, Submittal of Receiving Water Monitoring Program 2022 Annual Report2023-04-27027 April 2023 Submittal of Receiving Water Monitoring Program 2022 Annual Report DCL-23-035, Response to Request for Additional Information on Request Regarding Senior Reactor Operator License Application2023-04-24024 April 2023 Response to Request for Additional Information on Request Regarding Senior Reactor Operator License Application DCL-23-028, Technical Specification Bases, Revision 142023-04-24024 April 2023 Technical Specification Bases, Revision 14 DCL-2023-511, Report on Discharge Monitoring for the First Quarter of 20232023-04-20020 April 2023 Report on Discharge Monitoring for the First Quarter of 2023 DCL-23-031, Submittal of Annual Report of Occupational Radiation Exposure for 20222023-04-19019 April 2023 Submittal of Annual Report of Occupational Radiation Exposure for 2022 DCL-23-024, Independent Spent Fuel Storage Installation, Response to Nrg Request for Additional Information for Revision to License Amendment Request 22-01 Request for Approval of Alternative Security Measures for Early Warning System2023-04-0404 April 2023 Independent Spent Fuel Storage Installation, Response to Nrg Request for Additional Information for Revision to License Amendment Request 22-01 Request for Approval of Alternative Security Measures for Early Warning System DCL-23-022, 2023 Annual Statement of Insurance for Pacific Gas and Electric Companys Diablo Canyon Power Plant2023-03-29029 March 2023 2023 Annual Statement of Insurance for Pacific Gas and Electric Companys Diablo Canyon Power Plant DCL-23-023, Decommissioning Funding Report for Diablo Canyon Power Plant, Units 1 and 22023-03-28028 March 2023 Decommissioning Funding Report for Diablo Canyon Power Plant, Units 1 and 2 DCL-23-021, Independent Spent Fuel Storage Installation, Emergency Plan Update2023-03-23023 March 2023 Independent Spent Fuel Storage Installation, Emergency Plan Update DCL-23-020, Responses to NRC Questions Regarding License Renewal Efforts2023-03-17017 March 2023 Responses to NRC Questions Regarding License Renewal Efforts DCL-23-009, Owner'S Activity Report for Unit 2 Twenty-Third Refueling Outage2023-02-22022 February 2023 Owner'S Activity Report for Unit 2 Twenty-Third Refueling Outage DCL-23-008, Request Regarding Senior Reactor Operator License Application2023-02-22022 February 2023 Request Regarding Senior Reactor Operator License Application DCL-2023-503, Annual Sea Turtle Report2023-01-26026 January 2023 Annual Sea Turtle Report DCL-2023-502, (DCPP) 4th Quarter 2022 Report on Discharge Self-Monitoring2023-01-18018 January 2023 (DCPP) 4th Quarter 2022 Report on Discharge Self-Monitoring DCL-22-091, Revised Steam Generator Tube Inspection Report for Twenty-First Refueling Outage2022-12-20020 December 2022 Revised Steam Generator Tube Inspection Report for Twenty-First Refueling Outage DCL-22-089, Core Operating Limits Report for Unit 2 Cycle 242022-12-20020 December 2022 Core Operating Limits Report for Unit 2 Cycle 24 DCL-22-085, Request to Resume Review of the License Renewal Application or, Alternatively, for an Exemption from 10 CFR 2.109(b), Concerning a Timely Renewal Application2022-10-31031 October 2022 Request to Resume Review of the License Renewal Application or, Alternatively, for an Exemption from 10 CFR 2.109(b), Concerning a Timely Renewal Application DCL-22-041, Site-Specific Decommissioning Cost Estimate, Revision 12022-10-12012 October 2022 Site-Specific Decommissioning Cost Estimate, Revision 1 DCL-22-042, Post-Shutdown Decommissioning Activities Report, Revision 12022-10-12012 October 2022 Post-Shutdown Decommissioning Activities Report, Revision 1 2024-01-29
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Pacific Gas and Electric Company James M. Welsch Diablo Canyon Power Plant Site Vice President Mail Code 104/6 P. 0. Box 56 Avila Beach, CA 93424 February 19, 2015 805.545.3242 Internal: 691.3242 Fax: 805.545.4884 PG&E Letter DCL-15-022 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Docket No. 50-275, OL-DPR-80 Docket No. 50-323, OL-DPR-82 Diablo Canyon Units 1 and 2 Response to NRC Request for Additional Information Regarding License Amendment Request 14-01 "Revision to Technical Specification 3.8.1 'AC Sources I I
- Operating"'
References:
- 1. PG&E Letter DCL-14-018, License Amendment Request 14-01, "Revision to Technical Specifications 3.8.1, 'AC Sources-Operating,"' dated March 27, 2014 (ADAMS Accession No. ML14086A426)
- 2. NRC Letter, "Diablo Canyon Power Station, Units 1 and 2-Requests for Additional Information (RAis) for License Amendment Request 14-01 Associated with Revision toTS 3.8.1, 'AC Sources
-Operating' (TAC Nos. MF3826 and MF3827)," dated January 29, 2015
Dear Commissioners and Staff:
PG&E Letter DCL-14-018, dated March 27, 2014, submitted License Amendment Request (LAR) 14-01, "Revision to Technical Specification 3.8.1, 'AC Sources-Operating.'" LAR 14-01 proposed to:
(1) revise Surveillance Requirements (SRs) 3.8.1.2, 3.8.1.7, 3.8.1.11, 3.8.1.12, 3.8.1.15, 3.8.1.19, and 3.8.1.20 to change the allowable steady state diesel generator (DG) operating voltage and frequency bands; (2) revise SR 3.8.1.3 to change the DG test loading criterion; (3) add verification of DG cooling system function for SRs 3.8.1.3 and 3.8.1.14, respectively; (4) revise SR 3.8.1.4 to change the DG day tank surveillance requirement minimum volume; (5) revise SR 3.8.1.9 to revise the voltage and frequency recovery timing requirement; (6) revise SR 3.8.1.1 0 to change the DG full-load rejection test loading criterion and voltage limit; A member of the STARS (Strategic Teaming and Resource Sharing) Alliance Callaway
Document Control Desk PG&E Letter DCL-15-022 February 19, 2015 Page2 (7) revise SR 3.8.1.14 to change the DG 24-hour test loading criteria; (8) revise SR 3.8.1.15 to change the DG test prerequisite loading criterion; and (9) add a new note to SRs 3.8.1.1 0 and 3.8.1.14 to reduce the SR minimum DG operating power factor (PF) with the stipulation that PF limit requirements are not required if grid conditions do not permit.
On January 29, 2015, the NRC staff requested additional information required to complete the review of LAR 14-01 (Reference 2). PG&E's responses to the staff's questions are provided in the Enclosure.
This information does not affect the results of the technical evaluation or the no significant hazards consideration determination previously transmitted in PG&E Letter DCL-14-018.
PG&E makes no regulatory commitments (as defined by NEI 99-04) in this letter.
This letter includes no revisions to existing regulatory commitments.
If you have any questions, or require additional information, please contact Philippe Soenen at (805) 545-6984.
I state under penalty of perjury that the foregoing is true and correct.
Executed on February 19, 2015.
Sincerely,
~~e~
Site Vice President e1 d?/4418/503071 01 Enclosure cc: Diablo Distribution cc/enc: Marc L. Dapas, NRC Region IV Administrator Thomas R. Hipschman, NRC Senior Resident Inspector Siva P. Lingam, NRR Project Manager Gonzalo L. Perez, Branch Chief, California Dept of Public Health A member of the STARS (Strategic Teaming and Resource Sharing) Alliance Callaway
Enclosure PG&E Letter DCL-15-022 PG&E Response to NRC Request for Additional Information Regarding License Amendment Request 14-01, "Revision to Technical Specification 3.8.1, 'AC Sources - Operating"'
NRC RAI EPNB-1 Section 3. 4 of the license amendment request states that, for each day tank, "The minimum volume is obtained by considering: DG operation at full load for 60 minutes plus margin ... " ANSI N195-1976 states that the day tank capacity shall be based on the fuel consumption at a load of 100% of the continuous rating of the diesel plus a minimum margin of 10%. Please confirm that the margin that you used is at least 10%.
PG&E Response:
The proposed Diablo Canyon Power Plant (DCPP) diesel generator (DG) day tank usable minimum volume is conservatively based on the fuel consumption at a load of 2750 kilowatt (kW) plus 10 percent margin. The continuous rating of the DCPP DGs is 2600 kW.
NRC RAI EEEB-1:
In PG&E's submittal dated March 27, 2014, the licensee provided a summary of assumptions and results of the DG load study analysis. This DG load study analysis was performed to address the NRC resident inspector observations related to the implementation of NRC Temporary Instruction 25151176, "Emergency Diesel Generator Technical Specification Surveillance Requirements Regarding Endurance and Margin Testing," to evaluate Class 1E 4160 V Engineered Safety Features bus loading under various Design Basis Accident scenarios. The OG load study analysis appears to only consider kilowatt (kW) losses. Since the kilovolt (kV) ampere reactive (kVAR) losses will increase the current that the switchgear has to manage, please describe how the kVAR losses were considered when analyzing the DG loading.
PG&E Response:
The DG loading analysis considers both equipment kVAR loading demand and system losses. The kVAR demand of motors is adjusted in conjunction with the kW demand resulting from operation at 60.8 hertz (Hz) to achieve the appropriate motor power factor. Both kW and kVAR losses associated with the electrical distribution system (e.g. 4.16 kV I 480 volt (V) transformer and cables) are computed and included as a "load constituent" in determining the maximum steady state DG loading.
In addition to DG loading, the kVAR demand on equipment within the electrical distribution system is also considered when evaluating the ampacity rating of the equipment.
Enclosure PG&E Letter DCL-15-022 NRC RAI EEEB-2:
The LAR proposes a new voltage range of 2:: 39BO V and s; 4340 V for SRs 3. B. 1. 2,
- 3. 8. 1. 7, 3. 8. 1. 9, 3. 8. 1. 11, 3. B. 1. 12, 3. B. 1. 19, and 3. B. 1. 20. The current requirements of induction motors and other voltage sensitive equipment vary according to available voltage and frequency. Please provide excerpts from calculations with a summary that validate DG loading when operating at extremes of the proposed voltage range.
PG&E Response:
A sensitivity analysis study was performed with the DG frequency at 60.8 Hz. This study analyzes the DG peak output load in conjunction with the DG maximum and minimum output voltage. The total peak steady-state load on the DG consists of three components: constant power (kVA) loads (e.g. motors, inverters, and battery chargers),
constant impedance loads (i.e., heating and lighting), and equipment (i.e., cable and transformer) losses. The variations of the three components as a function of voltage are different: motors are constant power loads, where power is independent of voltage within the normal range of voltage variation; constant impedance loads vary as the square of the ratio of operating voltage to rated voltage; cable and transformer losses associated with constant kVA components increase when voltage is decreased; and cable and transformer losses associated with constant impedance loads decrease when voltage is decreased. As shown in the table below, the sensitivity analysis study results indicate that the increase in constant impedance loads due to the increase in operating voltage outweighs the increase in cable and transformer losses when voltage is reduced. Therefore, the maximum continuous peaks loads were determined at the maximum operating voltage of 4340 V.
var1a1ons1n
.f . DG Pea k Stea dIY-Sta te Loa ds DG @ Max Voltage DG @Min Voltage Peak Peak Output Output DG Bus Continuous Continuous Voltage (V) Voltage (V)
Load (kW) Load (kW) 13 F 4340 2652 3980 2645 NOTE: This sensitivity analysis study was performed as an alternative analysis to the DG load analysis calculation to demonstrate that DG operation at maximum voltage provides a bounding condition for maximum DG loading. The resultant peak load at maximum voltage from the study differs from the resultant loads of the final DG load analysis calculation due to the different computational tools and input parameters utilized by each analysis. For example, the DG load analysis calculation conservatively considers a high voltage condition to maximize load demand and maximized system losses from a low voltage condition.
2