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Category:Letter
MONTHYEARML24022A2262024-01-22022 January 2024 (PBAPS) Unit 3 - Submittal of the Inservice Inspection (ISI) Owner'S Activity Report (OAR) for the 24th Refueling Outage for Unit 3 ML23346A2412024-01-17017 January 2024 Staff Assessment of Updated Seismic Hazards Following the NRC Process for the Ongoing Assessment of Natural Hazards Information (EPID L-2019-PMP-0061) - Letter IR 05000277/20234022024-01-11011 January 2024 Security Baseline Inspection Report 05000277/2023402 and 05000278/2023402 and Independent Spent Fuel Storage Installation Security Inspection 07200029/2023401 ML23354A1922024-01-0505 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) ML23355A0622023-12-18018 December 2023 Independent Spent Fuel Storage Installation (Isfsi), Security Plan, Training and Qualification Plan, and Safeguards Contingency Plan ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML23305A1402023-12-13013 December 2023 Units 1 & 2; Nine Mile Point, Unit 2; Peach Bottom, Units 2 & 3; and Quad Cities, Units 1 and 2 - Issuance of Amendments to Adopt Traveler TSTF-580 ML23334A2502023-11-30030 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23270C0072023-11-29029 November 2023 Notice of Proposed Amendment to Decommissioning Trust Agreement ML23317A1192023-11-10010 November 2023 Constellation Energy Generation, LLC - 2023 Annual Report - Guarantees of Payment of Deferred Premiums ML23305A3472023-11-0101 November 2023 Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) IR 05000277/20230032023-10-30030 October 2023 Integrated Inspection Report 05000277/2023003 and 05000278/2023003 and Exercise of Enforcement Discretion ML23286A0012023-10-13013 October 2023 Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2023010-01 RS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans ML23271A1342023-10-11011 October 2023 Dtf Analysis Letter IR 05000277/20244012023-10-0505 October 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000277/2024401 and 05000278/2024401 ML23265A1502023-09-22022 September 2023 License Amendment Request Revise a License Condition and Certain Technical Specifications to Remove Restrictions in Support of Decommissioning Activities ML23264A8682023-09-21021 September 2023 Independent Spent Fuel Storage Installation Registration of Dry Storage Canister WC-EOS-37PTH-008-B4L, WC-EOS-37PTH-007-B4L, and WC-EOS-37PTH-002-B4L IR 05000277/20230102023-09-15015 September 2023 Biennial Problem Identification and Resolution Inspection Report 05000277/2023010 and 05000278/2023010 and Notice of Violation ML23251A2022023-09-11011 September 2023 Cover Letter W/Report LR-N23-0045, and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement2023-09-0808 September 2023 and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement IR 05000277/20230052023-08-31031 August 2023 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2023005 and 05000278/2023005) ML23158A1952023-08-30030 August 2023 R. E. Ginna - Issuance of Amendments to Adopt TSTF-273-A, Revision 2, Safety Function Determination Program Clarifications ML23232A0012023-08-19019 August 2023 Revision of One Procedure That Implements the Radiological Emergency Response Plan (Rerp). Includes EPP 06-009, Rev. 13 IR 05000277/20230112023-08-15015 August 2023 Comprehensive Engineering Team Inspection Report 05000277/2023011 and 05000278/2023011 ML23226A1112023-08-14014 August 2023 10 CFR 50.46 Annual Report IR 05000277/20230022023-08-0808 August 2023 Integrated Inspection Report 05000277/2023002 and 05000278/2023002 RS-23-087, Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor2023-08-0404 August 2023 Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor IR 05000277/20230402023-07-17017 July 2023 95001 Inspection Supplemental Report 05000277/2023040 and Follow-Up Assessment Letter ML23188A0532023-07-0707 July 2023 Registration of Use of Independent Spent Fuel Storage Installation (ISFSI) Casks ML23186A1272023-07-0606 July 2023 Response to Disputed Non-Cited Violation Documented in Peach Bottom Atomic Power Station, Units 2 and 3, Inspection Report 05000277/2022004 and 05000278/2022004 ML23178A0352023-06-27027 June 2023 Senior Reactor and Reactor Operator Initial License Examinations RS-23-077, Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations2023-06-16016 June 2023 Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations ML23151A4162023-05-31031 May 2023 Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) ML23150A2052023-05-30030 May 2023 Independent Spent Fuel Storage Installation (Isfsi), Annual Radiological Environmental Operating Report 80 January 1, 2022 Through December 31, 2022 RS-23-042, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-25025 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling ML23142A1602023-05-23023 May 2023 Summary of April 11, 2023, Public Observation Meeting with Constellation Energy Generation, LLC Re Proposed Exemption Request from Work Hour Requirements ML23132A1582023-05-18018 May 2023 Correction to Technical Specification 3.4.7 (Page 3.4-16) Issued in Amendment No. 337 ML23132A1532023-05-12012 May 2023 Transmittal of 2022 Annual Financial Reports WM 23-0009, Financial Assurance Requirements for Decommissioning Nuclear Power Reactors 10 CFR 50.75(f)(1)2023-05-10010 May 2023 Financial Assurance Requirements for Decommissioning Nuclear Power Reactors 10 CFR 50.75(f)(1) IR 05000277/20230012023-05-0808 May 2023 Integrated Inspection Report 05000277/2023001 and 05000278/2023001 ML23114A2522023-04-28028 April 2023 Request to Use a Provision of a Later Edition of the ASME Boiler & Pressure Vessel Code, Section XI 2024-01-05
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December 17, 2013 Mr. Patrick R. Simpson, Manager-Licensing Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555
SUBJECT:
PEACH BOTTOM EXEMPTION REQUEST (TAC NO. L24749)
Dear Mr. Simpson:
As discussed during our telephone call on December 11, 2013, the NRC has concluded that issuance of the requested exemption to Exelon Generation Company, LLC (EGC) regarding Transnuclear, Inc. (TN) TN-68 casks loaded with fuel bundles with incorrect cooling times at the Peach Bottom Power Station (PBAPS), Units 2 and 3 Independent Spent Fuel Storage Installation (ISFSI) in June and July 2001 is not appropriate at this time.
By letter dated May 23, 2013, EGC submitted an exemption request for the four PBAPS Unit 3 fuel assemblies that were loaded into four TN - 68 casks (i.e., one assembly per cask) with cooling times less than the minimum cooling time specified in the Certificate of Compliance (CoC) No. 1027, Amendment No. 0, Appendix A, Technical Specification (TS) 2.1.1, Table 2.1.1-1, "Minimum Acceptable Cooling Time as a Function of Max. Burnup and Min. Initial Enrichment". The non-compliance was identified during a January 2013 internal review of historical ISFSI fuel characterization for PBAPS.
Specifically, the four spent fuel assemblies had been cooled for approximately 9.8 years instead of the required 10 years that is specified in TS Table 2.1.1-1. Upon discovery of the TS non-compliance, EGC verified that the actual heat load of each fuel bundle, at the time of loading, was less than the limit specified in TS 2.1.1.E.ii. The decay heat of the assemblies has continued to decrease since their initial loading in June and July 2001. As of September 14, 2001, the four assemblies fully complied with the TS 2.2.1, Table 2.1.1-1 cooling time requirement.
As required by TS 2.2.2, EGC notified the NRC Operations Center within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of discovery of the TS non-compliance (ENS notification 48698). Similarly, as required by TS 2.2.3, EGC provided a 30-day special report to the NRC on February 22, 2013. This special report described the cause of the TS non-compliance and the actions taken to restore compliance and prevent recurrence. Specifically, the four spent fuel assemblies were non-compliant, at the time of loading, for durations ranging from 58 to 86 days. Subsequently, EGC requested NRC approval of a one-time exemption for the PBAPS, Units 2 and 3 ISFSI from the requirements of 10 CFR 72.212, due to a non-compliance with the terms and conditions of CoC No. 1027. Section 72.212 requires, among other things, compliance with all of the terms and conditions of an NRC approved cask by a general Part 72 licensee.
P. Simpson The NRC staff has reviewed your exemption request and concluded that the exemption request is not appropriate at this time. As of September 14, 2001, all four spent nuclear fuel assemblies were within the terms and conditions of CoC No. 1027 with respect to fuel age due to the subsequent aging of the fuel after their loading. EGCs erroneous loading of the subject assemblies was a violation of the terms of the CoC, but is not a continuing one. NRC completed an integrated inspection and documented the inspection results in the Peach Bottom Resident Inspector Report 2013003 (ML13213A239). The report concluded the loading of the four fuel assemblies did not impact the shielding, confinement, and thermal design functions of the loaded TN-68 casks and there was no safety consequences associated with the event. The NRC dispositioned the event as a minor violation of the TS.
If you have any questions, please contact me at (301) 287-9202.
Sincerely,
/RA/
John-Chau Nguyen, Sr. Project Manager Licensing Branch Division of Spent Fuel Storage and Transportation Office of Nuclear Material Safety and Safeguards Docket No.: 72-29, 50-277, 50-278, 72-1027 TAC No.: L24749 cc: See attached list
P. Simpson The NRC staff has reviewed your exemption request and concluded that the exemption request is not appropriate at this time. As of September 14, 2001, all four spent nuclear fuel assemblies were within the terms and conditions of CoC No. 1027 with respect to fuel age due to the subsequent aging of the fuel after their loading. EGCs erroneous loading of the subject assemblies was a violation of the terms of the CoC, but is not a continuing one. NRC completed an integrated inspection and documented the inspection results in the Peach Bottom Resident Inspector Report 2013003 (ML13213A239). The report concluded the loading of the four fuel assemblies did not impact the shielding, confinement, and thermal design functions of the loaded TN-68 casks and there was no safety consequences associated with the event. The NRC dispositioned the event as a minor violation of the TS.
If you have any questions, please contact me at (301) 287-9202.
Sincerely,
/RA/
John-Chau Nguyen, Sr. Project Manager Licensing Branch Division of Spent Fuel Storage and Transportation Office of Nuclear Material Safety and Safeguards Docket No.: 72-29, 50-277, 50-278, 72-1027 TAC No.: L24749 cc: See attached list Distribution:
SFST r/f MLombard SCoffin DMarcano AGendelman JDavis (SFST)
BDean/RI MFerdas/RI JNicholson/RI REnnis/NRR SHansell/RI RRolph/RI RMcCullum/NEI JBorowsky DForsyth CAraguas MRahimi ADAMS: ML13351A255 File location: G:\SFST\Nguyen\Peach Bottom TN68\Peach Bottom Exemption Request.docx DIVISION SFST SFST SFST SFST SFST WWheatley (via NAME: JCNguyen MSampson email)
DATE: 12/16/2013 12/16/2013 12/17/13 OFFICIAL RECORD COPY
LETTER FOR PEACH BOTTOM EXEMPTION Mr. Donis Shaw Transnuclear, Inc.
7135 Minstrel Way Columbia, MD 21045 Mr. John Schrage Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555