ML12335A602

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Official Exhibit - RIV000078-00-BD01 - IPEC Site Management Manual, IP-SMM, CY-110, Rev. 1, 8.6 RGWMP Quarterly Integrated Review Checklist (Quater 1, 2009), IPEC00225217
ML12335A602
Person / Time
Site: Indian Point  
Issue date: 12/22/2011
From:
Entergy Corp
To:
Atomic Safety and Licensing Board Panel
SECY RAS
References
RAS 21642, 50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01
Download: ML12335A602 (2)


Text

United States Nuclear Regulatory Commission Official Hearing Exhibit In the Matter of:

Entergy Nuclear Operations, Inc.

(Indian Point Nuclear Generating Units 2 and 3)

ASLBP #: 07-858-03-LR-BD01 Docket #: 05000247 l 05000286 Exhibit #:

Identified:

Admitted:

Withdrawn:

Rejected:

Stricken:

Other:

RIV000078-00-BD01 10/15/2012 10/15/2012 RIV000078 Submitted: December 22, 2011 IPEC SITE MANAGEMENT MANUAL QUALITY RELATED ADMINISTRATIVE PROCEDURE INFORMATIONAL USE IP-SMM CY-110 Page Revision 1 of 2

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8.6

""IVYIQIII Monitoring Well Sample Data Storm Drain Sample Data IE Bulletin No. 80-10 Facility Operations Spills & Leaks IPEC00225217 Item MW Sample Results MW Result Trends Storm Drain Activities Storm Drain Trends New 80-10 File Reports Refueling Activities Spent Fuel Moves Construction Activities Spill Reports Condition Reports 10CFR50.75(g)

EN-RP-113 Reports RGWMP QUARTERLY INTEGRATED REVIEW CHECKLIST

_" II" 11t:11 ~~

In general there is an elevated concentration of Sr-90, Ni-63, H3, & Cs-137 in some of the Unit 1 wells.

Additional samples were captured on 3/16-3/18.

This event was documented in CR-IP2-2009-0883.

This was discussed with the NRC and a press release made to the stakeholders.

The following condition reports were written to document MW IL exceedences in 4th QTR 2008:

CR-IP2-2009-00073, CR-IP2-2009-00232, The following condition reports were written to document MW IL exceedences in 1 st QTR 2009:

CR-IP2-2009-01110, CR-IP2-2009-01111, CR-IP2-2009-01113, CR-IP2-2009-01114, CR-IP2-2009-01369.

No anomalies were noted with the storm drain samples collected this quarter.

No anomalies were noted with samples collected in support 80-10 program for this quarter.

Per ANI audit 4 key sample points were sent to Teledyne and were found to be below effluent LLD.

A refueling outage of Unit 3 began on March 11 and was continuing at the end of this quarter.

On 02/04/2009, Operations overflowed 31 WHUT resulting in the spilling of approximately 2,000 gallons of waste water to the WHUT cell.

A CST Return Line was found to be leaking at -17 GPM on 2/15/09. This was documented in CR-IP2-2009-00666. This line was excavated and the affected area replaced. Tritium determined to be -1700 pCilL.

A press release was made to the stakeholders.

On 02/04/09 CR-IP2-2009-00476 documents that LW-

Entergy System Chemistry

& Activity Other IPEC00225218 IPEC SITE MANAGEMENT MANUAL SFP Chemistry RWST Chemistry RCS Activity QUALITY RELATED ADMINISTRATIVE PROCEDURE INFORMATIONAL USE IP-SMM CY-110 Page Revision 1 2

of 2

672 was leaking on the upstream side of the valve.

On 02/04/09 CR-IP3-2009-00306 documented a spill of approximately 2,000 gallons for waste water during a transfer from 32 Monitor Tank to 31 WHUT.

On 03/01/09 CR-IP2-2009-00807 documents a through wall leak downstream of LW-1134 @ 6 drops/minute.

On 03/07/09 CR-IP2-2009-00888 documents a leak from 14 WDST at valve CT-979 at 1 gallon/minute.

No unusual system chemistry was noted during this quarter.

REMP was revised to add LAF-002 as a REMP well.