ML12335A602
| ML12335A602 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 12/22/2011 |
| From: | Entergy Corp |
| To: | Atomic Safety and Licensing Board Panel |
| SECY RAS | |
| References | |
| RAS 21642, 50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01 | |
| Download: ML12335A602 (2) | |
Text
United States Nuclear Regulatory Commission Official Hearing Exhibit In the Matter of:
Entergy Nuclear Operations, Inc.
(Indian Point Nuclear Generating Units 2 and 3)
ASLBP #: 07-858-03-LR-BD01 Docket #: 05000247 l 05000286 Exhibit #:
Identified:
Admitted:
Withdrawn:
Rejected:
Stricken:
Other:
RIV000078-00-BD01 10/15/2012 10/15/2012 RIV000078 Submitted: December 22, 2011 IPEC SITE MANAGEMENT MANUAL QUALITY RELATED ADMINISTRATIVE PROCEDURE INFORMATIONAL USE IP-SMM CY-110 Page Revision 1 of 2
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8.6
""IVYIQIII Monitoring Well Sample Data Storm Drain Sample Data IE Bulletin No. 80-10 Facility Operations Spills & Leaks IPEC00225217 Item MW Sample Results MW Result Trends Storm Drain Activities Storm Drain Trends New 80-10 File Reports Refueling Activities Spent Fuel Moves Construction Activities Spill Reports Condition Reports 10CFR50.75(g)
EN-RP-113 Reports RGWMP QUARTERLY INTEGRATED REVIEW CHECKLIST
_" II" 11t:11 ~~
In general there is an elevated concentration of Sr-90, Ni-63, H3, & Cs-137 in some of the Unit 1 wells.
Additional samples were captured on 3/16-3/18.
This event was documented in CR-IP2-2009-0883.
This was discussed with the NRC and a press release made to the stakeholders.
The following condition reports were written to document MW IL exceedences in 4th QTR 2008:
CR-IP2-2009-00073, CR-IP2-2009-00232, The following condition reports were written to document MW IL exceedences in 1 st QTR 2009:
CR-IP2-2009-01110, CR-IP2-2009-01111, CR-IP2-2009-01113, CR-IP2-2009-01114, CR-IP2-2009-01369.
No anomalies were noted with the storm drain samples collected this quarter.
No anomalies were noted with samples collected in support 80-10 program for this quarter.
Per ANI audit 4 key sample points were sent to Teledyne and were found to be below effluent LLD.
A refueling outage of Unit 3 began on March 11 and was continuing at the end of this quarter.
On 02/04/2009, Operations overflowed 31 WHUT resulting in the spilling of approximately 2,000 gallons of waste water to the WHUT cell.
A CST Return Line was found to be leaking at -17 GPM on 2/15/09. This was documented in CR-IP2-2009-00666. This line was excavated and the affected area replaced. Tritium determined to be -1700 pCilL.
A press release was made to the stakeholders.
On 02/04/09 CR-IP2-2009-00476 documents that LW-
Entergy System Chemistry
& Activity Other IPEC00225218 IPEC SITE MANAGEMENT MANUAL SFP Chemistry RWST Chemistry RCS Activity QUALITY RELATED ADMINISTRATIVE PROCEDURE INFORMATIONAL USE IP-SMM CY-110 Page Revision 1 2
of 2
672 was leaking on the upstream side of the valve.
On 02/04/09 CR-IP3-2009-00306 documented a spill of approximately 2,000 gallons for waste water during a transfer from 32 Monitor Tank to 31 WHUT.
On 03/01/09 CR-IP2-2009-00807 documents a through wall leak downstream of LW-1134 @ 6 drops/minute.
On 03/07/09 CR-IP2-2009-00888 documents a leak from 14 WDST at valve CT-979 at 1 gallon/minute.
No unusual system chemistry was noted during this quarter.