ML12333A307

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Update: PNO-I-12-008A-Update Fitzpatrick NOEU for Fire in Main Transformer
ML12333A307
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 11/28/2012
From: Mel Gray
Division Reactor Projects I
To:
Gray M
References
PNO-I-12-008A
Download: ML12333A307 (2)


Text

Date: November 28, 2012 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-I-12-008A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information received may not yet be fully verified or evaluated by the Region Staff.

Facility Licensee Emergency Classification Entergy Nuclear Operations, Inc X Notification of Unusual Event James A. FitzPatrick Nuclear Power Plant _____ Alert Lycoming, NY _____ Site Area Emergency Docket: 50-333 _____ General Emergency

_____ Not Applicable

Subject:

UPDATE: JAMES A. FITZPATRICK NUCLEAR POWER PLANT NOTIFICATION OF UNUSUAL EVENT DUE TO FIRE IN MAIN TRANSFORMER This preliminary notification supplements information in PNO-1-12-008, which documented the declaration of an Unusual Event at the Fitzpatrick plant on November 11, 2012, following a fire in the T1-A main transformer. On-site fire brigade personnel, with assistance from a local fire department, extinguished the transformer fire. Operators declared an Unusual Event (UE) at 5:45 a.m. EST and exited the UE at 8:01 a.m. the same day. The plant includes two main transformers T1-A and T1-B. These transformers are located on-site, outside and adjacent to the turbine building.

On November 12, 2012, while the FitzPatrick plant was shut down, Entergy staff began maintenance activities that included inspection of the T1-A and T1-B main transformers.

Entergys investigation determined that the problem initiated in the B Phase winding of the T1-A main transformer that subsequently resulted in the fire. Entergy personnel replaced the T1-A main transformer and determined the T1-B was not damaged. FitzPatrick operators re-started the plant after completing replacement and testing of the replacement T1-A main transformer, and testing of other similar transformers. The plant reached full power on November 27, 2012.

The NRC staff continues to closely follow Entergys causal evaluations of the transformer failure and corrective actions. NRC oversight is being conducted through the NRCs baseline inspection program.

Entergy issued two news releases on November 11, 2012, related to the Unusual Event declaration, transformer fire, and termination. The information presented herein has been discussed with Entergy and is current as of November 28, 2010, at 10:00 a.m. Region I Public Affairs has responded to media inquiries.

This preliminary notification is issued for information only and no further notification by the staff is anticipated.

ADAMS Accession Number: ML12333A307 Contacts: Mel Gray (610) 337-5209 mel.gray@nrc.gov

ML12333A307 Non-Sensitive Publicly Available SUNSI Review Sensitive Non-Publicly Available OFFICE RI/DRP RI/PAO RI/SLO RI/DRP RI/ORA NAME MGray/ar for DScrenci DTifft DRobert /prw for WDean DATE 11/28/2012 11/28/2012 11/28/2012 11/28/2012 11/28/2012