ML110730779

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Lr - Draft Telecon Summary
ML110730779
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 03/14/2011
From:
Office of Nuclear Reactor Regulation
To:
Division of License Renewal
References
Download: ML110730779 (7)


Text

DiabloCanyonNPEm Resource From: Ferrer, Nathaniel Sent: Monday, March 14, 2011 4:14 PM To: Grebel, Terence Cc: DiabloCanyonNPEm Resource

Subject:

Draft Telecon Summary Attachments: Telecon Summary 2-4-11.doc

Terry, Attached is a draft of the Teleconference Summary for February 2 and 4, 2011. Please review and let me know if there are any corrections/changes needed.

Please let me know if you have any questions.

Nathaniel Ferrer Project Manager Division of License Renewal Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission (301)4151045 1

Hearing Identifier: DiabloCanyon_LicenseRenewal_NonPublic Email Number: 2687 Mail Envelope Properties (26E42474DB238C408C94990815A02F094C09C6B5E9)

Subject:

Draft Telecon Summary Sent Date: 3/14/2011 4:13:47 PM Received Date: 3/14/2011 4:13:46 PM From: Ferrer, Nathaniel Created By: Nathaniel.Ferrer@nrc.gov Recipients:

"DiabloCanyonNPEm Resource" <DiabloCanyonNPEm.Resource@nrc.gov>

Tracking Status: None "Grebel, Terence" <TLG1@pge.com>

Tracking Status: None Post Office: HQCLSTR01.nrc.gov Files Size Date & Time MESSAGE 399 3/14/2011 4:13:46 PM Telecon Summary 2-4-11.doc 65018 Options Priority: Standard Return Notification: No Reply Requested: No Sensitivity: Normal Expiration Date:

Recipients Received:

LICENSEE: Pacific Gas and Electric Company FACILITY: Diablo Canyon Nuclear Power Plant, Units 1 and 2

SUBJECT:

SUMMARY

OF TELEPHONE CONFERENCE CALLS HELD ON FEBRUARY 2 AND 4, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PACIFIC GAS AND ELECTRIC COMPANY CONCERNING REQUESTS FOR ADDITIONAL INFORMATION RELATED TO THE DIABLO CANYON NUCLEAR POWER PLANT, UNITS 1 AND 2, LICENSE RENEWAL APPLICATION (TAC NOS. ME2896 AND ME2897)

The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of Pacific Gas and Electric Company (PG&E or the applicant) held telephone conference calls on February 2 and 4, 2011, to obtain clarification on the applicants response to requests for additional information (RAIs) regarding the Diablo Canyon Nuclear Power Plant license renewal application.

By letter dated December 20, 2010, the staff issued follow up RAIs regarding the Flux Thimble Tube Program. Due to the timing of the request and the issuance of the safety evaluation report with open items, the staff identified issues related to this aging management program as an open item. The staff requested a telephone conference call to express its concerns regarding the open item. The telephone conference call was useful in clarifying the staffs concerns. provides a listing of the participants. Enclosure 2 provides discussions on the RAI and related open item.

The applicant had an opportunity to comment on this summary.

Nathaniel B. Ferrer, Project Manager Projects Branch 2 Division of License Renewal Office of Nuclear Reactor Regulation Docket Nos. 50-275 and 50-323

Enclosures:

As stated cc w/encls: Distribution via Listserv

LICENSEE: Pacific Gas and Electric Company FACILITY: Diablo Canyon Nuclear Power Plant, Units 1 and 2

SUBJECT:

SUMMARY

OF TELEPHONE CONFERENCE CALLS HELD ON FEBRUARY 2 AND 4, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PACIFIC GAS AND ELECTRIC COMPANY CONCERNING REQUESTS FOR ADDITIONAL INFORMATION RELATED TO THE DIABLO CANYON NUCLEAR POWER PLANT, UNITS 1 AND 2, LICENSE RENEWAL APPLICATION (TAC NOS. ME2896 AND ME2897)

The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of Pacific Gas and Electric Company (PG&E or the applicant) held telephone conference calls on February 2 and 4, 2011, to obtain clarification on the applicants response to requests for additional information (RAIs) regarding the Diablo Canyon Nuclear Power Plant license renewal application.

By letter dated December 20, 2010, the staff issued follow up RAIs regarding the Flux Thimble Tube Program. Due to the timing of the request and the issuance of the safety evaluation report with open items, the staff identified issues related to this aging management program as an open item. The staff requested a telephone conference call to express its concerns regarding the open item. The telephone conference call was useful in clarifying the staffs concerns. provides a listing of the participants. Enclosure 2 provides discussions on the RAI and related open item.

The applicant had an opportunity to comment on this summary.

Nathaniel B. Ferrer, Project Manager Projects Branch 2 Division of License Renewal Office of Nuclear Reactor Regulation Docket Nos. 50-275 and 50-323

Enclosures:

As stated cc w/encls: Distribution via Listserv DISTRIBUTION:

See next page ADAMS Accession Number:

OFFICE LA:DLR PM:DLR:RPB2 BC:DLR:RPB2 PM:DLR:RPB2 NAME DATE OFFICIAL RECORD COPY

TELEPHONE CONFERENCE CALL DIABLO CANYON NUCLEAR POWER PLANT, UNITS 1 AND 2 LICENSE RENEWAL APPLICATION LIST OF PARTICIPANTS FEBRUARY 2 AND 4, 2011 PARTICIPANTS: AFFILIATIONS:

Nate Ferrer U.S. Nuclear Regulatory Commission (NRC)

Kim Green NRC Allen Hiser NRC Jim Medoff NRC Yogen Garud Argonne National Laboratory (contractor)

Terry Grebel Pacific Gas and Electric Company (PG&E)

Mike Wright PG&E Kyle Duke PG&E Dan Hardesty PG&E Joon Kang PG&E ENCLOSURE 1

DIABLO CANYON NUCLEAR POWER PLANT, UNITS 1 AND 2 LICENSE RENEWAL APPLICATION REQUEST FOR ADDITIONAL INFORMATION FLUX THIMBLE TUBE INSPECTION PROGRAM By letter dated December 20, 2010, the staff issued a request for additional information (RAI) regarding certain aspects of the Pacific Gas and Electrics (PG&E or the applicant) Flux Thimble Tube Inspection Program. Because the applicant did not have time to respond to the RAI prior to issuance of the safety evaluation report (SER), the staff identified the issues as an open item in the SER. By letter dated January 12, 2011, the applicant responded to the staffs RAIs. The RAIs and response of interest are provided below along with a discussion of the issue.

Response to RAI B2.1.21-1 (follow up)

In its response, the applicant stated that it performed eddy current tests on thimble tubes from 1R3 RFO and sent the results to Westinghouse as part of the WCAP-12866 program. PG&E stated that based on the WCAP, it is not necessary to add any uncertainty to the eddy current indications, and that [f]or conservatism, a wall loss of 80% should now be used to determine when a thimble action is required (i.e. repositioned, replaced, etc.). PG&E considers that its acceptance criteria of 68 percent includes 17.5 percent margin compared to the 80 percent limit recommended in WCAP-12866.

Discussion:

During the calls, the staff explained that the applicants current procedure for projecting wear rates does not currently reflect an uncertainty term for measurement uncertainty. However, the Westinghouse calculation referenced in the procedure suggests that a factor be included for measurement uncertainty. The staff asked that the applicant revise its procedure to clearly identify whether measurement uncertainty is included. The applicant stated that it will revise the procedure as requested.

Response to RAI B2.1.21-2 (follow up)

2. Describe how the trending of thimble tube wear rates accounts for the possibility of a non-linear or accelerating wear rate.

In its response, PG&E stated that the possibility of non-linear or accelerating wear rates was addressed by STP R-22 FTT enhanced acceptance criteria which it listed in the response. PG&E previously committed to limiting repositioning of any tube to one time, and stated that there are currently no tubes in either unit that have been repositioned more than once.

3. Identify all aging effects and mechanisms that contributed to the degradation in Unit 2 flux thimble tube L13 over time (i.e., as detected during ROs 2R11, 2R12, and 2R13) and discuss the failure analysis activities that were performed at the site or were contracted out to confirm the apparent cause of the degradation that had occurred in the tube and the rapid progression of the degradation mechanism that lead to the relative rapid leak in 2006 (i.e., the leak occurred within four months of returning to power).

ENCLOSURE 2

In its response, PG&E stated that it sent a portion of the Unit 2 L-13 tube to Westinghouse for destructive analysis. It further stated that [t]he piece had several wear scars on it but none were through wall. The wear scars conformed to the scars Westinghouse had seen during development of the WCAP-12866. Their determination was that the event was caused by flow induced vibration of the thimble tube against the lower internals, core plate, or bottom nozzle. This was similar to other failures they had previously analyzed.

Discussion:

With regard to request 2, the staffs concern is that the applicants current procedure may not be conservative in predicting accelerated wear rates that may occur non-linearly. The staff asked the applicant to make wear rate data (predicted and actual) available for audit to confirm if the wear rates are occurring in a linear or non-linear fashion. The applicant agreed to make its wear rate data available to the staff for audit.

With regard to request 3, the staff explained that it could not determine the root cause of the flux thimble tube failure based on the information presented in the January 12th response provided by the applicant. During the call, PG&E explained that it sent a portion of the flux thimble tube to Westinghouse for analysis, and PG&E performed eddy current testing on the portion of the flux thimble tube that failed. Based on the information from Westinghouse and the results of the eddy current test, PG&E determined that the root cause of the failure of the tube was wear, and that no cracks were detected. The staff asked the applicant to amend its previous response to explain this. The applicant agreed to amend its response and explain how it arrived at the conclusion that no cracks occurred.