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Category:Letter
MONTHYEARIR 05000338/20244202024-09-23023 September 2024 Security Baseline Inspection Report 05000338/2024420 and 05000339/2024420, Cover Letter IR 05000338/20244022024-09-17017 September 2024 Security Baseline Inspection Report 05000338/2024402 and 05000339/2024402 ML24215A2622024-08-28028 August 2024 Transmittal Letter for Subsequent Renewed License IR 05000338/20240052024-08-27027 August 2024 Updated Inspection Plan for North Anna Power Station, Units 1 and 2 (Report 05000338/2024005 and 05000339/2024005) 05000339/LER-2024-001, Loss of Generator Field for 2J Eog During 2-PT-82.282024-08-20020 August 2024 Loss of Generator Field for 2J Eog During 2-PT-82.28 ML24234A0742024-08-15015 August 2024 Notification of Deviation from Pressurized Water Reactor Owners Group (PWROG) Letter OG-23-63, NEI 03-08 Needed Guidance: PWR Thermal Shield Flexure Inspection Requirements ML24163A3002024-08-0808 August 2024 Request for Relief Request N1-I5-NDE-007 Inservice Inspection Alternative ML24206A0062024-08-0808 August 2024 Notice of Availability of the Final Environmental Impact Statement for the North Anna Nuclear Power Station Unit Numbers 1 and 2 Subsequent License Renewal (Docket Numbers: 50-338 and 50-339) ML24221A1832024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Chickahominy Indian Tribe-Eastern Division ML24221A1852024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Delaware Tribe of Indians ML24221A1942024-08-0808 August 2024 Tribal Section 106 Letters-North Anna-United Keetoowah Band of Cherokee Indians in Oklahoma ML24221A1912024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Rappahannock Tribe, Inc ML24221A1902024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Pamunkey Indian Tribe ML24221A1892024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Nansemond Indian Nation ML24221A1822024-08-0808 August 2024 Tribal Section 106 Letters - North Anna - Chickahominy Indian Tribe ML24221A1882024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Monacan Indian Nation ML24221A1812024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Catawba Indian Nation ML24221A1862024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Eastern Band of Cherokee Indians ML24221A1932024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Upper Mattaponi Tribe ML24221A1872024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Eastern Shawnee Tribe of Oklahoma ML24208A0142024-08-0808 August 2024 Tribal Section 106 Letters-North Anna-Absentee-Shawnee Tribe of Indians of Oklahoma ML24206A0052024-08-0808 August 2024 SLR Final EIS Letter to Achp ML24221A1842024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Delaware Nation, Oklahoma ML24221A1922024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Tuscarora Nation of New York ML24241A0692024-08-0606 August 2024 ISFSI, Submittal of Cask Registration for Spent Fuel Storage IR 05000338/20240022024-08-0202 August 2024 Integrated Inspection Report 05000338/2024002 and 05000339/2024002 ML24206A0432024-07-26026 July 2024 Feis - Letter to the Applicant 05000338/LER-2024-001, Automatic Reactor Trip Due to Prni High Negative Rate2024-07-25025 July 2024 Automatic Reactor Trip Due to Prni High Negative Rate ML24206A0902024-07-24024 July 2024 Owners Activity Report ML24178A2422024-06-25025 June 2024 2023 Annual Report of Emergency Core Cooling System (ECCS) Model, Changes Pursuant to the Requirements of 10 CFR 50.46 ML24177A2792024-06-20020 June 2024 Preparation and Scheduling of Operator Licensing Examinations ML24143A1622024-06-12012 June 2024 – Correction to Issuance of Amendment Nos. 297 and 280 and Surry Units 1 and 2, Correction to Issuance of Amendment Nos. 317 and 317, to Change Emergency Plan Staff Augmentation Times ML24170B0532024-06-10010 June 2024 DOM-NAF-2-P/NP-A, Revision 0.5, Reactor Core Thermal-Hydraulics Using the VIPRE-D Computer Code ML24165A1462024-06-0505 June 2024 Loss of Generator Field for 2J EDG During 2-PT-82.28 IR 05000338/20240102024-05-24024 May 2024 NRC Fire Protection Team Inspection (FPTI) Report 05000338/2024010 and 05000339/2024010 IR 05000338/20240012024-05-10010 May 2024 Integrated Inspection Report 05000338/2024001 and 05000339/2024001 IR 05000338/20244032024-04-30030 April 2024 – Security Baseline Inspection Report 05000338-2024403 and 05000339-2024403 ML24054A0142024-04-22022 April 2024 Issuance of Amendment Nos. 297 and 280, and Surry Power Station Unit Nos. 1 and 2, Issuance of Amendment Nos. 317 and 317, to Change Emergency Plan Staff Augmentation Times ML24110A1502024-04-18018 April 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24110A1462024-04-18018 April 2024 Independent Spent Fuel Storage Installation (Sfsi) - Annual Radiological Environmental Operating Report ML24110A1392024-04-18018 April 2024 Annual Environmental Operating Report ML24087A0572024-04-16016 April 2024 Correction to Issuance of Amendment Nos. 296 and 279 ML24088A2692024-03-27027 March 2024 Core Operating Limits Report Cycle 31 Pattern Sos Revision 0 ML24086A4292024-03-25025 March 2024 Response to Request for Additional Information Associated with Alternative Request N1-I5-NDE-007 Request to Deter Additional Required Reactor Coolant Pump Casing Inspection ML24082A2742024-03-22022 March 2024 Request for Approval of Alternative Request N1-I5-NDE-007 to Deter Additional Required Reactor Coolant Pump Casing Inspection ML24086A4682024-03-21021 March 2024 Summary of Facility Changes, Tests and Experiments ML24005A0042024-03-18018 March 2024 Issuance of Amendment Nos. 296 and 279, Regarding Revised Emergency Plan for Relocation of the Technical Support Center ML24074A3012024-03-14014 March 2024 Notification of Target Set Inspection and Request for Information (NRC Inspection Report 05000338-2024403 and 05000339-2024403) IR 05000338/20244012024-03-0808 March 2024 Security Baseline Inspection Report 05000338/2024401, 05000339/2024401 and 07200016/2024401 IR 05000338/20230062024-02-28028 February 2024 Annual Assessment Letter for North Anna Power Station, Units 1 and 2 - NRC Inspection Reports 05000338/2023006 and 05000339/2023006 2024-09-23
[Table view] Category:Licensee 30-Day Written Event Report
MONTHYEARML16134A0712016-05-0606 May 2016 Day Report of Emergency Core Cooling System (ECCS) Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML13281A8032013-10-0202 October 2013 30-Day Report of Emergency Core Cooling System Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML12334A3802012-11-14014 November 2012 Post Accident Monitoring Report ML11123A1912011-04-25025 April 2011 Independent Spent Fuel Storage Installation, Special Report on Nuhoms Dry Shielded Canisters Loaded to Incorrect Heat Load Limits ML1021401952010-07-29029 July 2010 Day Report of Emergency Core Cooling System Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML0917402312009-06-17017 June 2009 Post Accident Monitoring (Pam) Report ML0708200742007-03-22022 March 2007 Day Report of Emergency Core Cooling System (ECCS) Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML0526602322005-09-15015 September 2005 Post Accident Monitoring Instrumentation Report 2016-05-06
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VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 June 17, 2009 U.S. Nuclear Regulatory Commission Serial No.09-359 Attention: Document Control Desk NAPS: MPW Washington, D.C. 20555 Docket Nos. 50-338 License Nos. NPF-4 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY (DOMINION)
NORTH ANNA POWER STATION UNIT 1 POST ACCIDENT MONITORING (PAM) REPORT On May 11, 2009, with Unit 1 in Mode 1 at 100 percent power, the open red indication light for the Phase B containment isolation valve (CIV) 1-CC-TV-102C ("B" RCP CC Return Outside Isolation) was determined to be inoperable. This Regulatory Guide 1.97 CIV is located outside of containment in the component cooling (CC) water return line from the "B" Reactor Coolant Pump (RCP). The closed green light indication is operable. The cause of the inoperable red open light is a missing rubber insulating ring in the socket. Technical Specification (TS) 3.3.3 Condition "A" requires restoration of the CIV indication to operable within thirty days. If CIV indication is not returned to service within thirty days, a Post Accident Monitoring Report is required in accordance with TS 5.6.6. This letter provides the required report and includes our plan and schedule for restoring the CIV indication to service.
Other indicators are available that provide verification of the CIV in the closed position if a containment isolation signal is received. There has been no change in CC system flow from the "B" RCP to indicate any mechanical problem from the valve. The CIV cycled properly during its last valve position indication test completed on March 30, 2009. The CIV located inside containment (1-CC-TV-102D) was also cycled properly during the last valve position indicator test completed on March 29, 2009. If a containment depressurization actuation (CDA) were to occur, both the inside and outside CIVs would receive a signal to close. The outside CIV would be verified closed using alternate indication.
This is a valve position open indication operability issue only. The replacement of the bulb with the rubber insulating ring missing in the bulb socket on-line can lead to grounding of the circuit, and possibly result in the associated trip valve closing which would be detrimental to Unit 1 operation. Therefore, due to the inherent risks involved with performaing maintenance on-line and our safety standards requiring the missing rubber insulating ring to be installed in the socket to prevent grounding, repairs are scheduled to be performed at the first entry into a unit condition of sufficient duration to allow the repair. The risks associated with performing repairs on-line include maintenance in a sensitive area (i.e., Control Room Safeguards Equipment Panel) and
Serial No.09-359 Docket No. 338 PAM Report Page 2 of 3 by-passing the air supply to the CIV to prevent the CIV from inadvertently closing, which may require manually tripping the reactor and shutting down the running "B" RCP.
Initial conditions for the valve testing and the position indication periodic test require the unit to be in Modes 5 or 6 or defueled with the RCP secured.
Continued operation of this valve is permitted because there are several levels of alternate indication. The Plant Computer System (PCS) provides an alternate reliable indication (PCS computer point S1CCO17D, "B" RCP Return Header Valve") to determine valve position. Flow indicators will also indicate zero flow in the CC return line when 1-CC-TV-102C is closed.
This report has been reviewed and approved by the Facility Safety Review Committee.
If you have any questions or require additional information, please contact Mr. Page Kemp at (540) 894-2295.
Sincerely, Daniel G. Stoddard, P.E.
Site Vice President Commitments made in this letter: None
Serial No.09-359 Docket No. 338 PAM Report Page 3 of 3 cc: U.S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW Suite 23T85 Atlanta, Georgia 30303 NRC Senior Resident Inspector North Anna Power Station Mr. J. F. Stang, Jr.
NRC Project Manager U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 0-8 G9A Rockville, Maryland 20852-2738 Ms. D. N. Wright NRC Project Manager U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 0-8 H4A Rockville, Maryland 20852-2738