SCH09-068, Quarterly Remedial Action Progress Report, Fourth Quarter 2008 PSEG Nuclear, LLC, Salem Generating Station
ML091690304 | |
Person / Time | |
---|---|
Site: | Salem |
Issue date: | 03/26/2009 |
From: | Bernard R ARCADIS G&M, Public Service Enterprise Group |
To: | Tuccillo K Office of Nuclear Reactor Regulation, State of NJ, Dept of Environmental Protection |
References | |
SCH09-068 | |
Download: ML091690304 (106) | |
Text
e,ARCADIS Infrastructure,environment, buildings Imagine the result Quarterly Remedial Action Progress Report, Fourth Quarter 2008 PSEG Nuclear, LLC, Salem Generating Station
PSEG Nuclear LLC P.O. Box 236, Hancock Bridge, NJ 08038-0236 May 26, 20090 NuclearLLC SCH09-068 CERTIFIED MAIL RETURN RECEIPT REQUESTED ARTICLE NUMBER: 7005 1160 0003 4381 7039 Karen Tuccillo Radiation Protection Programs Bureau of Nuclear Engineering New Jersey Department of Environmental Protection 33 Arctic Parkway Trenton, New Jersey 08625 QUARTERLY REMEDIAL ACTION PROGRESS REPORT, FOURTH QUARTER 2008 PSEG NUCLEAR, LLC, SALEM GENERATING STATION
Dear Ms. Tuccillo:
PSEG Nuclear LLC (PSEG) has prepared this Quarterly Remedial Action Progress Report (RAPR) summarizing groundwater remediation activities performed during 2008 at the PSEG Nuclear, LLC, Salem Generating Station (Station). The Station is located on Artificial Island in Hancock's Bridge, Salem County, New Jersey. Groundwater remediation activities are being conducted to address tritium detected in shallow groundwater adjacent to and south of the Salem Unit 1 Reactor Containment and Fuel Handling Building. The Station site plan is depicted on Figure 1 and Figure 2 presents a detailed view of the area undergoing active remediation.
The release of tritium contaminated water to the environment ceased in February 2003 when the Salem Unit 1 telltale drains were cleared and the Spent Fuel Pool (SFP) water that had accumulated behind the liner was drained. Routine maintenance of the spent fuel, pool (SFP) telltale drains has precluded further flow restrictions in those drains.
The installed seismic gap drains continue to provide a hydraulic gradient into the building and to the waste treatment systems, and away from the environment. The Groundwater Recovery System continues to control the flow of shallow groundwater in the shallow unconsolidated zone maintaining the plume to the on-site area while removing the remaining tritiated groundwater.
The monitoring program provides data to support the adaptive management program and analyze the efficiency of the program. Short-lived gamma-emitting radioisotopes have not been detected and tritium concentrations have continued to decline in groundwater samples, indicating that current activities meets the objectives of the program as provided in the RAWP.
W1 The annual recalculation of the mass ot tritium remaining in the plume produced an estimate of less than 1 Curie of tritium remaining in the plume where it exists above the NJDEP Ground Water Quality Criteria (NJGWQC). The mass is estimated based upon a number of factors including: the amount of tritium drawn back through the seismic gap by gap draining activities, the actual degree of variability in the tritium concentrations of the groundwater, and the amount of mass held in dead end pore space. Additionally, the existing monitoring network was designed to monitor a much more extensive plume; therefore the great reductions in plume mass achieved to date has resulted in the present situation where only a few wells indicate concentrations above the NJGWQC.
The following sections present the background of environmental investigation and remedial action at the site, the details and results of activities conducted since the recent submittal of the 3 rd Quarter 2008 RAPR, and provide a discussion of upcoming activities projected for the next reporting period.
1 Project Background In April 2004, a Remedial Investigation Report (RIR) was submitted to the New Jersey Department of Environmental Protection Bureau of Nuclear Engineering (NJDEP-BNE) presenting the details and results of a groundwater investigation conducted following the discovery of tritium in groundwater adjacent to Salem Unit 1. The results of the
- remedial investigation indicated that the source of tritium detected in groundwater was the Spent Fuel Pool, the tritium release to the environment had been stopped, and that tritium had not migrated to the property boundary above the New Jersey GWQC.
Based on the results of the remedial investigation a remedial action strategy was developed to hydraulically limit further migration and reduce the concentration of tritium remaining in groundwater adjacent to Salem Unit 1. In April 2004, PSEG initiated a pilot study designed to demonstrate the effectiveness of groundwater extraction for achieving remedial objectives. The pilot study proved to be effective, and in July 2004, a Remedial Action Work Plan (RAWP) proposing the operation of a full-scale groundwater extraction system was prepared and submitted to the NJDEP-BNE. The RAWP was approved by the NJDEP-BNE in November 2004 and a full-scale groundwater extraction system was subsequently installed.
In April 2005, weekly draining of the Unit 1 seismic gap was initiated to ensure that the flow of water entering the seismic gap was directed toward the interior of the building for treatment rather than outward toward the environment. Continuous draining of the Unit 1 seismic gap was initiated in February 2007 and the program has been continued to date.
2 Continued Groundwater Monitoring
- Groundwater monitoring activities continued through this reporting period in accordance with the schedule provided to NJDEP-BNE. The sampling program is- designed to 2
provide the representative data necessary to evaluate plume containment. Monitoring activities include the periodic collection of groundwater samples from the 36 Station monitoring wells. A summary of monitoring well construction details is presented in Table 1. Results for Plume area monitoring well locations are depicted on Figure 2 and wells beyond the area of active remediation are shown on Figure 3.
Groundwater samples are initially submitted to Salem Chemistry for analysis for tritium and gamma-emitting radioisotopes. Samples indicating tritium concentrations less than 50,000 picocuries per liter (pCi/L) are sent to Maplewood Testing Services for more refined analysis yielding lower detection limits.
Historical and current analytical data indicate that plant related gamma-emitting radioisotopes have not been detected in groundwater from any monitoring well since monitoring was initiated in 2003.
Historical analytical tritium results for groundwater collected from the Station monitoring wells are presented on Figure 2 and Table 2. Included on Figure 2 are: panel 1) the extent of tritium in groundwater at the completion of the remedial investigation (Baseline Plume); panel 2) the extent of tritium in groundwater one year prior to the reporting period, December 2007; and, panel 3) the extent of tritium in groundwater in September 2008. Based on a review of Figure 2, it is apparent that the mass of tritium in groundwater has been significantly reduced by the remedial efforts conducted to date.
Details regarding these activities are discussed below.
The analytical results for groundwater samples collected from the monitoring wells were evaluated based on the water-bearing zone in which they are screened. The three primary water-bearing units investigated beneath the Station are: 1) the Vincentown Formation; 2) the shallow water-bearing unit within the limits of the cofferdam surrounding Salem Unit 1; and, 3) the shallow, water-bearing unit outside the limits of the cofferdam.
2.1 Tritium Analytical Results for the Vincentown Formation The following wells are screened in the Vincentown Formation: Well V, Well K, Well L, Well P, Well Q, and Well CB. Groundwater quality for Well K, Well L, Well P, and Well Q is currently monitored on a semi-annual basis. Groundwater quality for Well V and Well CB is currently monitored on a quarterly and monthly basis, respectively.
Tritium has consistently not been detected above laboratory detection limits or detected at relatively low levels in groundwater at all monitoring wells screened within the Vincentown formation since the initiation of monitoring at these locations with the recent exception of Well CB. As discussed in the Q3, 2008 RAPR concentrations of tritium increased slightly at well CB following the March/April 2008 outage, during which the
- steam generators in Unit 2 were replaced. The activities involved in the spring 2008 outage applied significant but temporary vibration and compressive stresses to the Kirkwood clay and overlying units as the steam generators were removed and replaced.
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- The resulting vibration and compression of the Kirkwood Clay likely remobilized some tritiated water present in and above the immobile porosity fraction of the Kirkwood and overlying units as a result of historic above ground steam releases in this area. The tritium concentrations which may have been present within the Kirkwood are a result of concentration gradient driven diffusion into the immobile pore water of the clay.
Following the removal and replacement of the turbines, tritium concentrations in groundwater exhibited a slight increase and subsequent decrease. Tritium levels in Well CB are trending toward levels historically observed in other wells completed in the Vincentown formation with some variability in routine analytical results. At no time did tritium concentrations rise to a level approaching the New Jersey Groundwater Quality Criteria. Thus, the groundwater monitoring results continue to indicate that the previous release of tritium impacted water from the SFP has not significantly migrated below the shallow water-bearing unit.
2.2 Tritium Analytical Results for Wells Installed Within the Limits of the Cofferdam The following wells are screened in the shallow, water-bearing unit within the limits of the cofferdam: Well M, Well N, Well 0, Well R, Well AC, Well AE, Well Al, Well AM, Well AN, and Well AO. Groundwater quality for these wells is currently monitored on a monthly basis. However, Well AO has been inaccessible due to site constraints and
- has not been sampled since January 2007. During 2008 Well AW was only sampled in the months of March through September, although this well is typically sampled every month. Based on the results of groundwater analysis, the potential for reducing the frequency of sampling for these wells will be evaluated.
Groundwater collected from Well AC, Well AD, Well AM, and Well AN exhibit some of the highest concentrations of tritium remaining at the Site, likely due to their location relative to the original release. Tritium concentrations in groundwater at these wells exhibits general decreasing trends since the initiation of monitoring in 2003. Well AC, for example, the location of the historic highest concentrations, has exhibited steadily decreasing concentrations (from a maximum of 15,000,000 pCi/L in April 2003 to 26,934 pCi/L during the sampling event in December 2008). The decrease in tritium concentrations - observed at Well AC provides confirmation that tritium impacted groundwater is no longer being released to the- environment and that the remedial groundwater recovery system (GRS) is effectively reducing concentrations of previously released tritium.
The mobile extraction unit was moved from Well AM to Well 0 and then to Well AR during the second quarter of 2008 to address seasonal fluctuations. The mobile system is only typically used during the period between March and November in order to avoid potential freeze damage.
Tritium concentrations at Well N, Well R, and Well Al are below GWQC and generally show consistent declining temporal trends. Tritium concentrations at all well locations 4
' within the cofferdam the initiation have generally of monitoring, decreased indicating by oneactivities that remedial order of magnitude or more are effectively since removing mass from the areas of greatest concentration. Variations in concentration occur primarily due to the complex flow patterns and limited flushing within the limits of the cofferdam.
2.3 Tritium Analytical Results for Wells Installed Outside the Limits of the Cofferdam The wells installed in the shallow, water-bearing unit beyond the limits of the cofferdam are Well S, Well T, Well U, Well W, Well Y, Well Z, Well AA, Well AB, Well AD, Well AF, Well AG (Shallow and Deep), Well AH (Shallow and Deep), Well AJ, Well AL, Well AP, Well AQ, Well AR, Well AS, Well AT, and Well CA. These wells are screened either just above the clay confining unit that separates the shallow water-bearing unit from the Vincentown Formation, or in the interval indicating the highest tritium concentrations found in the shallow water-bearing unit at each boring location at the time of the Supplemental Investigation completed in August 2003.
By 2007, tritium concentrations at Well AR had been reduced to approximately 80,000 pCi/L. In the spring of 2008, recovery Wells AS and AT began to lose efficiency as the pumps degraded. As a result, slight increases in tritium concentration were observed at
- Well AS and Well AT during the summer of 2008. These increases were later determined to be an artifact of reduced functionality of the pumps coupled with the location of the sampling ports. Subsequent servicing of the GRS (October 2008) revealed that by October these two wells were wholly non-functional and although the installed check valves prevented backflow into the well, the sampling ports were producing samples more representative of total system effluent than of the concentrations in Wells AR, AS and AT. Grab samples collected at the wells indicated that the concentrations in Well AS and AT were below GWQC which was inconsistent with some of the second and third quarter analytical results obtained from the samples collected at the sampling ports in the control shed.
Tritium concentration trends for wells screened in the shallow, water-bearing unit indicate that the operation of the groundwater extraction system is achieving the remedial action objectives (i.e., reduce the mass of tritium in groundwater and maintain hydraulic control). The distribution of tritium in groundwater in December 2008 is presented on Figure 2, along with the distribution of tritium prior to the initiation of the pilot study in March 2004, and in December 2007. As shown on Figure 2, the mass of tritium in groundwater has continued to decrease through the operation of the groundwater extraction pilot study system and operation of the full-scale system.
3 Groundwater Extraction
- Groundwater extraction as a remedial strategy at the site was initiated with the operation of a pilot test from April 2004 to February 2005. In accordance with the 5
RAWP, groundwater extraction activities completed to date consisted of the operation of the pilot-study from April 26, 2004 to February 11, 2005 and operation of the full scale GRS from February 16, 2005 to the present. As discussed above, system service was scheduled and performed in October 2008 to address valve and pump difficulties.
3.1 Full-Scale System The objectives of the full-scale GRS consist of:
, maintaining hydraulic containment of the tritium plume; and
" reducing tritium concentrations in groundwater.
The present operation of the GRS consists of groundwater extraction from Wells AB, AD, AJ, AN, AS, and AT. Pumping at Well S has not occurred since 2006 as a result of low yield and resulting pump failures. The system was inactive for several weeks during the first quarter of 2008 for system servicing and again at the end of the third quarter of 2008. A regular system service schedule will be planned and implemented to maximize system operation and efficiency. Groundwater extracted from the wells is processed in accordance with the Station's United States Nuclear Regulatory Commission (USNRC) license and plant procedures. Details of the extracted effluent are discussed below.
3.2 Mobile Groundwater Recovery Unit The mobile groundwater recovery unit was designed and built to target specific areas of the groundwater plume exhibiting greater tritium concentrations. The mobile unit typically operates between March and November (weather permitting). The mobile unit collects water in nominal 1,000 gallon batches for handling in accordance with the station's permits. The mobile unit has historically been used successfully at Wells 0, AP, AM, and AR. In 2008 it was operated at Wells 0 and AR where relatively elevated concentrations were present during the early part of the year.
3.3 Total System Effluent Data and Evaluation GRS operations were initiated on February 16, 2005. The system operated in various configurations as part of the optimization process for approximately the first month. The GRS discharges continuously in accordance with the Station's USNRC permit allowing the GRS to be more effective and efficient than the pilot-scale system. As of December 2008, the GRS has recovered greater than 23 million gallons of groundwater. This is equivalent to an average recovery rate of approximately 10.8 gallons per minute or greater than 15 times the recharge rate for the extraction area (calculated to be 0.7 gallons per minute, based upon an assumed percentage of annual precipitation).
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3.4 Water-Level Data and Evaluation Water level measurements from the extraction and select observation wells have been monitored to confirm hydraulic containment of the tritium groundwater plume. Water levels are periodically collected and evaluated according to the schedule described in the Q4 2006 RAPR submitted in March 2007. " Groundwater elevation contours developed from water level measurements collected in January, April, August and December of 2008 are presented in Figures 4, 5, 6, and 7, respectively. Because some operational issues arose in 2008 water levels were not as consistent as they have been in past years. The system was serviced in October with a second service event scheduled for spring 2009. The pump service performed in October restored the declining performance of several of the components of the GRS system. An additional servicing event was scheduled for the spring of 2009 and will be established on a regular schedule going forward. The partially rehabilitated system continues to control the flow of groundwater in the Salem Unit 1 yard area and therefore controls the distribution of the remnants of the tritium groundwater plume.
3.5 Cumulative Curies Removed The various groundwater recovery activities conducted to date have been successful in controlling the plume and recovering tritium from groundwater at and downgradient of the Salem Unit 1 seismic gap.
Figure 8 summarizes the results of groundwater remediation, activities conducted using the well field including both the pilot study and the permanent system. As Shown on Figure 8, greater than 2.8 curies of tritium have been recovered from the operation of the GRS through December 2008. Approximately 0.93 curies of tritium were removed by the pilot system. As the mass remaining in the plume continues to decrease so will the rate of tritium recovery by the GRS. The effectiveness of the GRS is emphasized by the decrease and stabilization of system effluent concentrations since the activation of the full scale system in February 2005. System effluent concentrations averaged 35,250 pCi/L during the fourth quarter 2008 (data available from October and December). This indicates that the GRS has been successful at significantly decreasing tritium concentrations in groundwater as discharge concentrations are roughly 30 percent of the peak concentration (109,000 pCi/L) observed in March 2005.
The average effluent concentration during 2008 was 48,626 pCi/L, indicating that the GRS continues to reduce the mass present in the subsurface of the Salem Unit 1 yard area. The mass of tritium in the plume was recalculated in late 2008 in order to provide an annual update of the remedial progress. The annual recalculation interval was selected based upon the adaptively managed sampling program such that the most complete data set is used to calculate the mass remaining in the plume. At the end of 2008 the mass was estimated to be less than one curie. This calculation is based upon the concentration of tritium shown in the plume and the pore volume for that area. The endpoint for the mass calculation is the 20,000 pCi/L concentration isocontour.
Therefore it is expected that GRS operations will achieve end criteria for tritium removal 7
ahead of the previously communicated schedule although the system will likely remain in some form as a fail safe for the release mechanism.
4.0 Operation of the Seismic Gap Drain In addition to the operation of the GRS and mobile groundwater recovery unit, the seismic gap drains in Salem Unit 1 and Unit 2 are being used to continuously drain the water from these gaps, resulting in the recovery of residual tritium concentrations from the seismic gap. The operation of these permanent gap drains creates an inward gradient towards the gaps facilitating the recovery of water from low accessibility areas and minimizing the potential for this water to enter the environment.
Water samples from the seismic gap drains are periodically collected for tritium analysis. Table 3 and Figure 9 summarize the results of periodic tritium analysis from the seismic gap. A comparison of Figure 1 and Figure 9 indicates that concentrations of tritium in water recovered in the Unit 1 seismic gap have been consistently significantly higher than those detected in groundwater samples collected from Well AC and Well AM located to the southeast and southwest of the seismic gap, respectively.
Thus, continuous operation of the Unit 1 seismic gap drain is effectively removing residual SFP water in the seismic gap, resulting in the reduction of tritium concentrations in groundwater adjacent to the seismic gap. Tritium concentrations in water presently being removed from the gap are close to the concentrations present in the pool indicating that the continuous draining program has been successful in establishing a more direct flow path between the seismic gap drain and any SFP water.
Continuous or nearly continuous draining (resulting in a hydraulic head less than that which is present in the geologic materials present outside the seismic gap) provides positive assurance that the engineering control established by the seismic gap drain is effective at capturing any SFP water that enters the seismic gap. The gap drain creates an inward gradient such that groundwater flows into the seismic gap assuring that no further potential exists for a discharge to the environment from the gap. This is further supported by the reversal in the concentration relationship between Wells AC and AM suggesting that the plume is detaching from the location of the original release.
Concentrations of tritium from the Unit 1 seismic gap (summarized by week) are shown on Figure 9.
Monitoring of water drained from the Unit 2 seismic gap acts as a screen for a potential release from the Unit 2 SFP. Water collected in the Unit 2 seismic gap drain indicate tritium levels several orders of magnitude below the Unit 1 seismic gap drain concentration, and consistent with the trends in the Unit I seismic gap drain.
Water samples will continue to be periodically obtained from the Unit 1 and Unit 2 seismic gap drain to evaluate the potential for the release of radioisotopes to the environment.
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Upcoming Activities Activities projected for the first half of 2009 (January through June) include the following:
, Continue to monitor continuous draining of seismic gap drains;
- Ongoing evaluation of the data to refine the procedures and protocols as necessary to adaptively manage the operation and sampling of the GRS;
" Continue to measure groundwater levels and evaluate flow and plume containment;
- Perform calculations of the residual tritium remaining in the plume and estimate the time remaining to completing the remediation;
, Continued groundwater sampling and analysis; and, Continued operation and evaluation of the GRS performance.
Based on the decreasing trends in most wells, PSEG recommends modifying the minimum sampling frequency of wells that are routinely below the NJGWQC. It is recommended that wells W, AA, AF, Al, AL, and AP have the sampling frequency reduced by one step, i.e, monthly to quarterly, or quarterly to semi-annually. It is also recommended that operating wells connected to the GRS system be sampled on a monthly basis to aid in the adaptive management of the GRS system.
If you have any questions or comments regarding the contents of this report, please do not hesitate to contact me at (856) 339-1636.
Since 7 Robert N. Bernard Manager - Salem Chemistry, Environmental, and Radwaste C Ron Nimitz- NRC NRC - Salem Resident Inspector NRC - Document Room 9
BC:
George Gellrich S05 Edward Keating N21 Jeffrey Pantazes T1I7A John Valeri Jr. T5C Christine Neely N21 Helen Gregory N21 File#Groundwater EXTERNAL Peter Milionis, ARCADIS Bradley Pierce, ARCADIS' Scott Potter, PhD., ARCADIS Christopher Sharpe, ARCADIS 10
1 of2 Table 01. Well Construction Details, PSEG Nuclear, LLC, Salem Generating Station, Hancock's Bridge, New Jersey.
Construction Diameter Total Depth Monitoring Monitored MP MP Northing Easting Installation Details (inches) (feet bgs) Interval Hydrogeologic Elevation Elevation (NAD 83) (NAD 83)
Well ID Date (feet bgs) Unit (feet RPD) (feet amsl) 1 231,435. 199,697 Well K Feb-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown 102.00 12.08 1 230,933 199,263 Well L Jan-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown 101.46 11.54 2 230,843 199,546 Well M May-03 Sch-40 PVC 1 20.0 10.0-20.0 Cofferdam 102.17 12.25 2 230,777 199,661 Well N Jan-03 Sch-40 PVC 2 20.0 10.0-20.0 Cofferdam 101.65 11.73 2 230,804 199,839 Well 0 Jan-03 Sch-40 PVC 2 20.0 10.0 - 20.0 Cofferdam 101.33 11.41 1 230,336 200,000 Well P Mar-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown 101.13 11.21
' 230,645 201,196 Well Q Mar-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown 106.59 16.67 2 230,906 199,640 Well R Jun-03 Sch-40 PVC 1 19.0 9.0- 19.0 Cofferdam 102.35 12.43 3 230,711 199,613 4
May-03 Sch-40 PVC 2 34.7 24.7- 34.7 Shallow 99.04 9.12 Well S 3 Sch-40 PVC 2 31.2 21.2-31.2. Shallow 104.13 14.21 231,575 199,575 Well T Jun-03 3 231,370 199,618 May-03 Sch-40 PVC 2 32.2 27.2-32.2 Shallow 98.57 8.65 Well U4 2 79.5 69.5-79.5 Vincentown' 98.74 8.82 231,355 199,548 Well V4 Jun-03 Sch-40 PVC 3 230,777 199,450 4
Jun-03 Sch-40 PVC 2 35.0 25.0-35.0 Shallow 98.26 8.34 Well W 3 Sch-40 PVC 2 37.0 27.0-35.0 Shallow 101.81 11.89 230,771 199,343 Well Y Sep-03 3 230,681 199,399 Well Z Sep-03 Sch-40 PVC 2 37.5 27.5-37.5 Shallow 101.86 11.94 3 230,603 199,541 Sep-03 Sch-40 PVC 2 36.0 26.0-36.0 Shallow 99.07 9.15 Well AA4 3 230,623 199,677 4
Oct-03 Sch-40 PVC 2 42.0 32.0- 42.0 Shallow 98.93 9.01 Well AB 2 230,724 199,725 4
Sep-03 Sch-40 PVC 2 24.0 14.0-24.0 Cofferdam 98.77 8.85 Well AC 3 230,684 199,607 AD 4
Oct-03 Sch-40 PVC 6 43.0 33.0-43.0 Shallow 98.99 9.07 Well 2 Sch-40 PVC 2 37.5 27.5-37.5 Cofferdam 101.54 11.62 230,829 199,845 Well AE Oct-03 Notes:
MP Measuring Point bgs Below ground surface RPD Relative to plant datum amsl Relative to mean sea level (NAVD 1988) 1 Monitoring well is screened in the Vincentown Formation.
2 Monitoring well is screened in the shallow, water-bearing unit at a location within the limits of the cofferdam.
3 Monitoring well is screened in the shallow, water-bearing unit at a location outside the limits of the cofferdam.
4 The surface completions of Monitoring Wells S, U, V, W, AA, AB, AC,'and AD were converted from above-grade to flush-grade in February 2004.
0 2 of 2 Table 01. Well Construction Details, PSEG Nuclear, LLC, Salem Generating Station, Hancock's Bridge, New Jersey.
Installation Construction Diameter Total Depth. Monitoring Monitored MP MP Northing Easting WellID Date Details (inches) (feet bgs) Interval Hydrogeologic Elevation Elevation (NAD 83) (NAD 83)
(feet bgs) Unit (feet RPD). (feet amsl) 3 Well AF Oct-03 Sch-40 PVC 2 45.0 35.0-45.0 Shallow 101.61 11.69 230,491 199,702 3
Well AGrShallow . Feb-04 Sch-40 PVC 1 24.2 14.2-24.2 Shallow 99.29 9.37 230,496 199,508 3
WellAG-Deep Feb-04 Sch-40 PVC 1 40.0 30.0-40.0 Shallow 99.20 9.28 230,496 199,508 3
Well AH-Shallow Feb-04 Sch-40 PVC 1 24.5 14.5 -24.5 Shallow 102.58 12.66 230,450 199,596 3
Well AH-Deep Feb-04 Sch-40 PVC 1 40.0 30.0 -40.0 Shallow 102.70 12.78 230,450 199,596 2
Well Al Jan-04 Sch-40 PVC 4 22.0 12.0-22.0 Cofferdam 98.79 8.87 230,798 199,521 3
Well AJ Jan-04 Sch-40 PVC 4 35.3 15.3-35.3 Shallow 98.85 8.93 230,670 199,665 3
Well AL Jan-04 Scl1-40 PVC 2 25.3 15.3-25.3 Shallow 99.13 9.21 230,594 199,806 2
Well AM Jan-04 Sch-40 PVC 4 20.9 10.9-20.9 Cofferdam 98.55 8.63 230,762 199,680 Well AN Jun-04 Sch-40 PVC 4 25.0 10.0-25.0 Cofferdam2 98.76 8.84 230,727 199,735 Well AO Jun-04 Sch-40 PVC 4 21.0 11.0- 21.0 Cofferdam2 98.82 8.90 230,765 199,556 Well AP Jun-04 Sch-40 PVC' 4 40.0 15.0-40.0 Shallow3 98.65 8.73 230,694 199,464 Well AQ Jun-04 Sch-40 PVC 4 45.0 20.0-45.0 Shallow3 99.05 9.13 230,526 199,540 Well AR Jun-04 Sch-40 PVC 4 43.0 18.0-43.0 Shallow3 99.22 9.30 230,622 199,626 Well AS Jun-04 Sch-40 PVC 4 41.5 16.5-41.5 Shallow3 99.44 9.52 230,566 199,604 Well AT Jun-04 Sch-40 PVC 4 44.0 19.0-44.0 Shallow3 99.25 9.33 230,546 199,566 Well BW Dec-06 Sch-40 PVC 1 10 5-10 Shallow1 98.72 8.80 231563.00 199,864 Well BX Dec-06 Sch-40 PVC 1 10 5-10 Shallowi 98.72 8.80 231582.00 199,876 Well CA Dec-06 Sch-40 PVC 4 38 28.0- 38.0 Shallow' 98.87 8.95 231318.00 199,791 3
Well CB Dec-06 Sch-40 PVC 2 80 70.0-80.0 Vincentown 98.98 9.06 231328.00 199,787 Notes:
MP Measuring Point bgs Below ground surface RPD Relative to plant datum amsl Relative to mean sea level (NAVD 1988) 1 Monitoring well is screened in the Vincentown Formation.
2 Monitoring well is screened in the shallow, water-bearing unit at a location within-the limits of the cofferdam.
3 Monitoring well is screened in the shallow, water-bearing unit at a location outside the limits of the cofferdam.
4 The surface completions of Monitoring Wells S, U, V, W, AA, AB, AC, and AD were converted from above-grade to flush-grade in February 2004.
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Ainion Identification Date Note lResult (pCiIL) I'LLD IDeviation Boron(mg/L) ISodium(mg/L Well- K 01/29/03 -153 153 90 Well- K 02/03/03 <153 153 91 0.74 1,060 Well- K 02/05/03 1,120 147 104 Well- K 02/12/03 506 148 96 Well- K 02/27/03 1,170 145 104 0.8 1,210 Well- K 03/14/03 937 144 100 1.38 1,200 Well- K 03/18/03 875 144 99 1.19 1,060 Well- K 03/26/03 822 140 97 Well- K 03/31/03 677 155 103 Well- K 04/09/03 1,010 140 99 Well- K 04/17/03 1,170 141 102 Well- K 04/21/03 911 140 98 Well- K 04/29/03 833 142 97 Well- K 05/05/03 948 135 96 Well- K 05/20/03 878 145 100 Well- K 05/28/03 859 141 97 Well- K 06/04/03 921 141 98 Well- K 06/10/03 897 138 97 Well- K 06/17/03 894 141 98 Well- K 06/24/03 783 141 96 Well- K 06/30/03 914 142 99 Well- K 07/16/03 870 140 97 Well- K 07/29/03 950 140 98 Well- K 08/12/03 845 142 98 1.13 1,190 Well- K 08/27/03 852 141 97 1.02 1,220 Well- K 09/09/03 653 147 98 1.16 1,170 Well- K 09/25/03 713 139 94 0.82 1,280 Well- K 10/06/03 880 143 99 1.15 1,250 Well- K 11/09/03 891 141 98 0.92 1,330 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
L Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page I of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- K 02/04/04 762 139 95 ....
Well- K 06/10/04 777 143 97 ....
Well- K 08/02/04 720 144 97 0.67 1,160 Well- K 10/04/04 485 156 100 ....
Well- K 11/03/04 598 148 98 1.60 1,270 Well- K 12/06/04 1 -4,520 4,520 1,370 ....
Well- K 01/10/05 480 152 98 2.12 1,200 Well- K 02/01/05 602 139 93 ....
Well- K 03/03/05 711 146 98 ....
Well- K 04/05/05 740 143 97 ....
Well- K 05/09/05 473 155 100 ....
Well- K 07/05/05 721 150 101 ....
Well- K 01/09/06 511 155 100 ....
Well- K 07/10/06 404 153 97 ....
Well- K 01/23/07 468 152 98 ....
Well- K 07/12/07 294 144 90 ....
Well- K 01/16/08 358 138 88 ....
Well- K 07/16/08 200 129 80 -- .2 Well- L 01/22/03 - 147 147 87 0.76 1,020 Well- L 01/23/03 '146 146 86 0.67 1,890 Well- L 01/24/03 '147 147 87 0.59 2,000 Well- L 01/27/03 '151 151 89 0.53 1,900 Well- L 03/14/03 '143 143 85 ....
Well- L 03/18/03 -143 143 86 -- --
Well- L 04/02/03 -153 153 91 ....
Well- L 04/08/03 '142 142 86 ....
Well- L 04/15/03 '141 141 84 ....
Well- L 04/24/03 *139" 139 82 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
ooo Constituent was detected above its New Jersey Groundwater Quality Criteria. r N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 2 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Idniiaio Dae INtResult (pCiIL) ILLD IDeviation IBoron(mg/L) TSodium(mg/L)1 Well- L 04/29/03 .- 141 141 83 Well- L 05/05/03 '134 134 82 Well- L 05/15/03 -144 144 85 Well- L 05/20/03 -144 144 86 Well- L 05/28/03 -141 141 84 Well- L 06/04/03 '140 140 84 Well- L 06/10/03 -137 137 82 Well- L 06/17/03 -141 141 84 Well- L 06/24/03 '141 141 84 Well- L 06/30/03 '140 140 83 Well- L 07/29/03 '141 141 86 Well- L 08/27/03 '142 142 84 1.95 2,330 Well- L 09/25/03 '140 140 84 1.62 2,490 Well- L 12/16/03 '146 146 86 Well- L 03/23/04 3,870 147 137 Well- L 05/04/04 -138 138 82 Well- L 05/10/04 -138 138 84 Well- L 05/19/04 '148 148 88 Well- L 05/24/04 '147 147 88 Well- L 06/10/04 140 140 85 1.56 2,180 Well- L 07/07/04 753 140 96 0.81 1,140 Well- L 08/02/04 '147 147 88 Well- L 10/04/04 -159 159 92 Well- L 11/03/04 '142 142 84 Well- L 12/06/04 I '4,520 4,520 1,280 Well- L 01/10/05 -158 158 93 Well- L 02/01/05 -148 148 87 Well- L 03/07/05 -158 158 94 0.832 2,400 Well- L 04/06/05 <152 152 90 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
IA00 !Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 3 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Major Cations and Anin Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- L 05/17/05 -150 150 88 ....
Well- L 07/06/05 -152 152 90 ....
Well- L 01/09/06 -160 160 95 ....
Well- L 07/10/06 '156 156 92 ....
Well- L 01/22/07 -154 154 92 ....
Well- L 07/19/07 -145 145 87 ....
Well- L 01/17/08 '137 137 81 ....
Well- L 07/16/08 -129 129 78 ....
Well- M 02/12/03 18,700 170 270 0.25 23 Well- M 02/28/03 14,400 146 219 0.17 28 Well- M 03/03/03 9,420 140 181 0.16 27 Well- M 03/10/03 15,000 144 223 0.21 22 Well- M 03/17/03 10,600 142 192 ....
Well- M 03/24/03 10,100 144 189 ....
Well- M 03/31/03 11,000 154 203 ....
Well- M 04/07/03 9,260 136 181 ....
Well- M 04/14/03 9,600 135 183 ....
Well- M 04/21/03 8,880 140 - 180 ....
Well- M 04/30/03 8,800 143 180 ....
Well- M 07/09/03 126,000 138 602 ....
Well- M 07/23/03 *11 1.09 141 573 Well- M 08/06/03 73.;00 141 466 Well- M 08/06/03 30 144 462 0.24 22 Well- M 08/20/03 62,000 141 430 0.27 23 Well- M 09/04/03 37 143 346 0.22 23 Well- M 09/16/03 3 141 320 0.32 25 Well- M 10/03/03 449ý 146 289 0.27 25 Well- M 10/20/03 1 16,380 NA NA ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F !Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 4 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ItTritium I Major Cations and Anions Identification Date INote [Result (pCiIL) ILLD Deviation IBoron(mg/L) ISodium(mg-/L)
Well- M 10/30/03 NA NA Well- M 12/04/03 11,200 146 198 Well- M 01/06/04 8,900 145 183 Well- M 01/22/04 7,340 140 164 Well- M 02/17/04 11,300 NA NA Well- M 03/05/04 7,170 146 168 0.15 22 Well- M 04/29/04 6,510 141 159 0.12 21 Well- M 05/11/04 2,350 141 117 Well- M 06/10/04 3,610 141 133 Well- M 07/08/04 5,090 144 150 Well- M 08/17/04 3,857 143 136 Well- M 09/08/04 3,745 146 137 Well- M 10/04/04 3,036 144 126 Well- M 11/03/04 2,818 143 125 Well- M 12/06/04 '4,520 4,520 1,390 Well- M 01/19/05 3,950 2,890 Well- M 01/19/05 2,650 2,830 Well- M 02/09/05 4,660 3,240 Well- M 03/02/05 3,360 3,400 3.33 24 Well- M 04/11/05 4,220 2,550 Well- M 05/03/05 10,031 147 192 Well- M 06/06/05 15,169 146 225 Well- M 07/12/05 3,750 4,070 Well- M 08/15/05 -18900. 3,905 4,114 Well- M 09/06/05 4,940 4,037 Well- M 10/10/05 17,049 148 240 Well- M 11/14/05 12,528 158 219 Well- M 12/13/05 8,257 148 178 Well- M 01/17/06 6,932 152 170 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
I 'Constituent was detected above its New Jersey Groundwater Quality Criteria.
'Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10137 AM Page 5 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Io Major Cations and Anions Identification Date INote ýResýult (pCi/L) ILLD Deviation IBoron(mg/L) ISodium(mg/L)
Well- M 02/21/06 7,371 153 174 Well- M 02/22/06 1 7,510 3,550 1,750 1
Well- M 03/20/06 4,200 3,730 1,530 Well- M 04/11/06 4,067 155 144 Well- M 05/16/06 4,592 152 148 Well- M" 06/19/06 4,712 155 150 Well- M 07/18/06 5,553 157 161 Well- M 08/08/06 4,912 161 157 Well- M 09/18/06 4,132 161 148 Well- M 10/10/06 3,565 157 139 Well- M 11/01/06 4,077 170 154 Well- M 12/18/06 3,887 162 147 Well- M 01/13/07 4,517 150 148 Well- M 02/23/07 4,796 168 161 Well- M 03/08/07 5,085 158 160 Well- M 04/20/07 11,617 170 225 Well- M 05/15/07 10,479 181 219 Well- M 06/18/07 8,426 147 177 Well- M 07/18/07 7,443 146 168 Well- M 08/15/07 6,066 140 154 Well- M 09/20/07 5,271 150 153 Well- M 10/03/07 5,612 160 164 Well- M 11/14/07 4,505 124 133 Well- M 12/12/07 4,617 151 146 Well- M 01/17/08 4,713 140 141 Well- M 02/06/08 4,733 139 141 Well- M 03/18/08 4,946 145 147 Well- M 04/02/08 4,755 142 142 Well- M 05/08/08 4,893 147 146 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 6 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and An s Identification Date Note Result (pCi/L) LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well- M 06/19/08 4,969 135 140 ....
Well- M 07/07/08 4,980 129 137 ....
Well- M 08/06/08 4,755 140 140 ....
Well- M 09/02/08 4,523 134 135 ....
Well- M 11/19/08 4,000 135 131 ....
Well- M 12/15/08 4,347 149 142 ..
Well-N 01/30/03 L90 187 505 0.34 14 Well-N 01/30/03 58,400 141 412 0.37 14 Well- N 02/10/03 15,600 149 229 0.28 11 Well- N 03/04/03 2,770 144 123 0.2 34 Well- N 03/14/03 2,670 143 121 0.41 24 Well- N 03/17/03 3,830 142 134 0.36 21 Well- N 03/25/03 3,480 139 129 ....
Well- N 04/04/03 3,560 152 137 ....
Well- N 04/11/03 3,730 137 131 ....
Well- N 04/16/03 3,910 142 134 ....
Well- N 04/25/03 4,600 138 140 ....
Well- N 04/30/03 9,370 144 185 ....
Well- N 05/06/03 9,830 137 186 ....
Well- N 05/21/03 7,480 144 169 ....
Well- N 05/27/03 7,130 141 165 ....
Well- N 06/04/03 5,480 141 150 ....
Well- N 06/11/03 4,990 137 144 ....
Well- N 06/19/03 5,680 142 153 ....
Well- N 06/25/03 5,060 142 146 ....
Well- N 07/10/03 5,020 137 144 ....
Well- N 07/25/03 5,220 141 148 ....
Well- N 08/07/03 5,110 145 148 0.21 24 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
'Constituent was detected above its New Jersey Groundwater Quality Criteria.
-Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 7 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I tritium Major Catios and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well- N 08/20/03 5,850 140 153 0.25 20 Well- N 09/04/03 5,660 145 154 0.33 23 Well- N 09/17/03 6,160 141 157 0.27 22 Well- N 10/03/03 6,460 NA NA Well- N 10/03/03 5,740 145 157 0.24 24 Well- N 11/03/03 5,560 NA NA Well- N 12/12/03 6,010 NA NA Well- N 01/20/04 6,050 143 155 Well- N 02/11/04 5,950 139 154 Well- N 02/11/04 7,360 NA NA Well- N 03/18/04 6,550 145 162 Well- N 04/08/04 7,180 137 164 2.30E-01 17 Well- N 05/12/04 8,210 147 178 Well- N 06/03/04 9,890 152 196 Well- N 07/20/04 5,220 141 148 Well- N 08/17/04 14,303 161 235 Wkell- N 09/14/04 11,642 148 207 Well- N 10/25/04 10,619 157 206 Well- N 11/23/04 9,150 149 187 Well- N 12/27/04 7,660 4,060 1,720 Well- N 01/12/05 9,550 154 195 Well- N 02/22/05 9,442 146 186 Well- N 03/15/05 9,712 153 195 0.11 18 Well- N 04/19/05 9,781 147 193 Well- N 05/17/05 9,060 147 185 Well- N 06/21/05 9,302 145 183 Well- N 07/12/05 8,147 147 177 Well- N 08/15/05 8,152 157 184 Well- N 09/20/05 7,502 151 174 Notes: -
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
q Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 8 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I I p Tritium Ia Major Cations and Anions Identification Date INote IResult (pCi/L) ILLD IDeviation IBoron(mg/L) I Sodium(mL Well- N 10/10/05 8,280 149 180 Well- N 11/14/05 8,210 151 180 Well- N 12/20/05 5,896 157 162 Well- N 01/23/06 7,400 149 171 Well- N 02/23/06 1 8,410 3,920 1,810 1
Well- N 03/21/06 13,500 3,730 2,130 Well- N 04/11/06 8,393 164 189 Well- N 05/16/06 8,588 152 185 Well- N 06/20/06 15,289 150 232 Well- N 07/18/06 6,660 159 170 Well- N 08/21/06 13,776 154 224 Well- N 09/07/06 <22,714 155 277 Well- N 09/19/06 14,486 160 232 Well- N 10/09/06 159 310 Well- N 11/01/06 11,023 165 213 Well- N 11/15/06 10,407 197- 232 Well- N 12/07/06 9,280 211 233 Well- N 12/18/06 10,163 154 199 Well- N 01/13/07 6,325 148 165 Well- N 01/22/07 6,812 157 173 Well- N 02/06/07 11,587 189 234 Well- N 02/23/07 12,517 167 227 Well- N 03/08/07 13,252 146 218 Well- N 04/20/07 6,332 160 172 Well- N 05/15/07 8,139 150 177 Well- N 06/19/07 7,554 145 169 Well- N 07/18/07 8,865 99 168 Well- N 08/15/07 9,045 148 182 Well- N 09/21/07 9,711 147 188 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
O Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 9 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
)
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCiL) TLLD Deviation Boron(mg/L) Sodium(mg/L)
Well-N 10/03/07 2.39 145 267 Well- N 10/17/07 2-1.01 153 279 ....
Well- N 11/14/07 18,607 124 237 ....
Well- N 12/12/07 12,763 145 207 ....
Well- N 01/17/08 8,049 139 170 ....
Well- N 01/28/08 7,780 139 167 ....
Well- N 02/06/08 7,641 148 172 ....
Well- N 02/20/08 6,853 138 160 -- --
Well- N 03/13/08 6,278 149 161 ....
Well- N 03/18/08 6,956 137 160 ....
Well- N 04/02/08 7,427 150 171 ....
Well- N 04/23/08 7,017 143 163 ....
Well- N 05/08/08 6,949 139 159 ....
Well- N 06/24/08 8,406 135 168 ....
Well- N 07/07/08 9,346 144 183 ....
Well- N 08/07/08 9,026 142 178 ....
Well- N 08/21/08 9,675 129 176 ....
Well- N 09/02/08 9,899 128 178 ....
Well- N 11/14/08 8,991 142 177 ....
Well- N 12/08/08 8,845 133 172 1 ..
Well- 0 01/29/03 1,220 156 110 0.16 41 Well- 0 01/29/03 1,400 143 106 0.17 40 Well- 0 02/10/03 10,300 149 193 0.1 13 Well- 0 02/21/03 7,370 149 170 0.09 15 Well- 0 02/28/03 11,700 147 201 0.09 17 Well- 0 03/04/03 8,800 142 178 0.07 21 Well- 0 03/13/03 12,300 143 204 0.11 16 Well- O 03/17/03 11,000 155 206 0.08 12 Notes_
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
V Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported. /
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 10 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample 1Rl Tritium Ia Major CationadAio Identification Date INote lResult (pCifL)T LLD .IDeviation IBoron(mg/L) ISodium(mg/L)I Well- 0 03/25/03 8,660 141 178 Well- 0 03/31/03 8,010 155 180 Well- 0 04/07/03 7,290 137 165 Well- 0 04/15/03 12,400 141 204 Well- 0 04/21/03 11,800 139 201 Well- 0 04/29/03 10,500 140 191 Well- 0 05/06/03 10,200 134 187 Well- b 05/21/03 11,100 143 197 Well- 0 05/28/03 12,700 140 207 Well- 0 06/03/03 12,200 140 202 Well- 0 06/10/03 12,800 137 206 Well- 0 06/17/03 10,300 141 190 Well- 0 06/24/03 13,400 141 212 Well- 0 07/09/03 9,100 139 182 Well- 0 07/25/03 7,710 139 169 Well- 0 08/06/03 8,300 148 178 0.24 14 Well- 0 08/20/03 7,440 142 168 0.31 14 Well- 0 09/03/03 6,400 143 159 0.28 14 Well- 0 09/15/03 7,730 141 170 0.27 13 Well- 0 10/03/03 6,980 145 168 0.23 23 Well- 0 10/20/03 6,700 141 161 0.2 47 Well- 0 11/17/03 NA NA Well- 0 12/18/03 5,320 145 150 Well- 0 01/14/04 3,750 141 132 1
Well- 0 02/09/04 NA NA 1
Well- 0 02/09/04 NA NA 1
Well- 0 ,03/03/04 NA NA 1
Well- 0 03/23/04 NA NA Well- 0 04/06/04 19,300 136 247 2.81E-01 120 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
1 0 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page I11of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ItTritium I Major Cations and Anions Identification Date INote lResult (pCiIL) ILLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well- 0 05/03/04 140 253 Well- 0 05/11/04 140 254 Well- 0 06/10/04 4,974 2,855 Well- 0 06/24/04 14,174 141 218 Well- 0 07/13/04 9,510 141 185 Well- 0 07/29/04 6,739 146 163 Well- 0 08/31/04 7,307 159 179 Well- 0 09/22/04 6,637 146 167 Well- 0 10/04/04 5,543 140 151 Well- 0 10/18/04 5,874 150 161 Well- 0 11/22/04 14,027 144 218 Well- 0 12/16/04 15,000 3,230 1,950 Well- 0 01/18/05 18,840 152 257 0.297 22 Well- 0 02/08/05 4,660 2,640 Well- 0 03/08/05 10,911 139 195 Well- 0 04/11/05 7,096 148 170 Well- 0 05/10/05 6,722 148 166 Well- 0 06/07/05 5,803 147 156 Well- 0 07/06/05 3,827 145 136 Well- 0 07/19/05 4,999 156 154 Well- 0 08/02/05 4,295 148 143 Well- 0 09/07/05 5,400 146 152 Well- 0 10/04/05 4,326 153 146 Well- 0 11/02/05 14,530 151 224 Well- 0 12/09/05 15,734 152 235 Well- 0 01/16/06 3,550 2,460 Well- 0 02/07/06 18,595 157 254 Well- 0 03/07/06 1 8,560 3,310 1,720 Well- 0 04/04/06 7,340 161 178 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
0,0oConstituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 12 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) ILLD Deviation Boron(mg/L) Sodium(mg/L)
Well- 0 05/02/06 9,369 152 191 Well- 0 06/19/06 9,417 155 194 Well- 0 07/17/06 9,533 151 188 Well- 0 08/21/06 4,760 152 150 Well- 0 09/18/06 4,237 158 147 Well- 0 10/05/06 12,747 157 219 Well- 0 11/02/06 19,760 169 275 Well- 0 12/07/06 9,060 162 197 Well- 0 01/13/07 147 306 Well- 0 02/24/07 153 292 Well- 0 03/07/07 155 393 Well- 0 04/20/07 163 393 Well- 0 05/16/07 15,782 180 257 Well- 0 06/18/07 15,749 148 229 Well- 0 07/19/07 8,610 145 177 Well- 0 08/15/07 9,155 142 178 Well- 0 09/19/07 1,525 146 109 Well- 0 10/04/07 2,619 183 146 Well- 0 11/19/07 6,211 149 167 Well- 0 12/12/07 142 340 Well- 0 01/16/08 144 291 Well- 0 02/07/08 149 317 Well- 0 03/12/08 149 340 Well- 0 04/01/08 148 289 Well- 0 05/19/08 13,799 146 215 Well- 0 05/27/08 10,565 150 195 Well- 0 06/11/08 10,568 146 192 Well- 0 06/23/08 9,377 135 175 Well- 0 07/15/08 9,388 128 173 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
21O Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 13 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well- 0 07/28/08 12,170 143 203 ....
Well- 0 08/18/08 1 -4,530 4,530 NA ....
Well- 0 08/25/08 1 9,760 4,280 1,930 .....
Well- O 09/02/08 9,780 134 178 ....
Well- O 10/17/08 10,128 135 184 ....
Well- 0 11/18/08 " N 135 285 ....
Well- 0 12/16/08 152 333 Well- P 02/05/03 0.18 1,600 Well- P 02/06/03 '153 153 91 ....
Well- P 02/21/03 -148 148 91 ....
Well- P 03/13/03 303 143 90 0.2 --
Well- P 03/18/03 465 143 92 ....
Well- P 03/26/03 '143 143 87 ....
Well- P 04/03/03 -154 154 9 ....
Well- P 04/24/03 '139 139 82 ....
Well- P 04/29/03 ,144 144 85 ....
Well- P 05/05/03 '134 134 82 ....
Well- P. 05/20/03 '145 145 85 ....
Well- P 05/30/03 *142 142 85 ....
Well- P 06/04/03 '141 141 84 ....
Well- P 06/10/03 '138 138 84 ....
Well- P 06/17/03 '141 141 85 -- --
Well- P 06/24/03 '141 141 85 ....
Well- P 07/16/03 '141 141 85 ....
Well- P 08/13/03 -140 140 84 0.48 1,570 Well- P 09/08/03 '147 147 87 0.65 1,560 Well- P 09/09/03 1 '7,430 7,430 NA .....
Well- P 10/06/03 ' 143 143 86 0.48 1,610 Notes:
LLD Lower Limit'of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
A Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 14 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I ITritium Major Cations and Anions Identification Date Note Result (pCi/L)j LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- P 01/22/04 144 144 86 -- --
Well- P 04/28/04 *139 139 83 0.441 1,550 Well- P 08/03/04 *157 157 92 0.292 1,540 Well- P 10/05/04 149 149 87 -- --
Well- P 11/03/04 147 147 87 0.955 1,690 Well- P 12/14/04 1 -3,230 3,230 1,010 -- --
Well- P 01/11/05 -162 162 95 1.02 1,580 Well- P 02/09/05 148 148 88 -- --
Well- P 03/03/05 -158 158 92 ....
Well- P 04/12/05 -149 149 89 ....
Well- P. 05/10/05 -148 148 87 ....
Well- P 07/11/05 '151 15i 89 ....
Well- P 01/23/06 -150 150 89 ....
Well- P 07/24/06 '155 155 93 ....
Well- P 01/14/07 '154 154 92 ....
Well- P 07/19/07 '146 146 86 ....
Well- P 01/24/08 '137 137 81 ....
Well- P 07/16/08 ' 144 144 86 ....
Well- Q 02/06/03 '147 147 88 ....
Well- Q 03/11/03 -142 142 85 ....
Well- Q 03/12/03 '141 141 84 ....
Well- Q 03/14/03 '143 143 85 ....
Well- Q 03/19/03 '143 143 85 -- --
Well- Q 03/24/03 '143 143 85 ....
Well- Q 04/23/03 '139 139 82 ....
Well- Q 04/30/03 '142 142 84 ....
Well- Q 05/06/03 -135 135 81 ....
Well- Q 05/12/03 '144 144 84 ....
Notes:
LLD 'Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
~Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 15 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium T Major Cations and Anions Identification Date INote Result (pCi/L) LLD [ Deviation Boron(mg/L) I Sodium(mg/L)
Well- Q 05/19/03 144 144 84 Well- Q 05/30/03 140 140 84 Well- Q 06/05/03 '139 139 83 Well- Q 06/11/03 '138 138 83 Well- Q 06/16/03 '141 141 84 Well- Q 06/23/03 -143 143 85 Well- Q 07/17/03 -141 141 85 Well- Q 08/13/03 '142 142 85 0.32 1,830 Well- Q 09/10/03 '148 148 89 0.25 1,790 Well- Q 10/07/03 '144 144 85 0.33 1,920 Well- Q 11/09/03 '142 142 86 0.32 1,930 Well- Q 01/08/04 '142 142 83 0.3 1,850 Well- Q 02/04/04 '139 139 84 Well- Q 03/22/04 '144 144 85 0.285 1,720 Well- Q 06/04/04 -156 156 91 Well- Q 08/02/04 -146 146 88 0.28 1,630 Well- Q 10/04/04 '153 153 87 Well- Q 11/03/04 '150 150 88 0.312 1,960 Well- Q 12/29/04 '4,020 4,020 1,420 Well- Q 01/31/05 213 142 89 Well- Q 02/15/05 <3,910 3,910 1,130 Well- Q 03/14/05 '151 151 91 0.30 1,730 Well- Q 03/15/05 151 151 91 1,730 Well- Q 04/18/05 -145 145 85 Well- Q 05/16/05 '151 151 88 Well- Q 07/19/05 <150 150 89 Well- Q 01/23/06 -150 150 90 Well- Q 07/10/06 '159 159 93 Well- Q 01/08/07 '157 157 92 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2WO'jVConstituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 16 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions 1 Identification Date Note IResult (pCi/L) LLD Deviation Boron(mg/L) I Sodium(mg/L) 1 Well- Q 07/24/07 '146 146 86 ....
Well- Q 01/28/08 '137 137 81 .
Well- Q 07/24/08 -139 139 83 ....
Well- R 02/26/03 13,900 145 218 0.29 43 Well- R 03/03/03 7,490 140 166 0.23 37 Well- R 03/10/03 6,170 145 158 0.27 29 Well- R 03/17/03 7,270 144 168 0.27 33 Well- R 03/25/03 6,810 140 162 ....
Well- R 04/01/03 6,740 153 169 ....
Well- R 04/08/03 5,940 135 152 ....
Well- R 04/14/03 5,890 142 154 ....
Well- R 04/22/03 5,800 139 153 ....
Well- R 04/30/03 5,260 141 148 ....
Well- R 07/09/03 3,270 136 125 ....
Well- R 07/25/03 2,940 141 124 ....
Well- R 08/06/03 2,860 144 124 0.46 54 Well- R 08/20/03 2,860 142 124 0.51 48 Well- R 09/04/03 2,990 153 132 0.57 46 Well- R 09/17/03 2,800 141 122 0.47 50 Well- R 10/03/03 2,740 146 125 0.4 52 Well- R 10/21/03 2,650 140 120 ....
Well- R 12/05/03 2,550 147 122 0.37 50 Well- R 01/22/04 2,210 143 116 ....
Well- R 02/09/04 1 -5,390 5,390 NA ....
Well- R 02/09/04 2,230 140 115 ....
Well- R 03/05/04 2,200 146 117 ....
Well- R 04/28/04 1 '5,780 5,780 1,649 0.265 42 Well- R 05/24/04 2,420 144 120 0.30 41 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
i 'Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 17 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium I Major Cations and Anions Identification Date INote lResult (pCi/L) ' LLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well- R 06/10/04 2,390 148 123 0.24 42 Well- R 07/08/04 2,050 147 118 Well- R 08/17/04 2,124 159 126 Well- R 09/29/04 2,000 156 122 Well- R 10/11/04 1,708 143 110 Well- R 11/08/04 1,696 151 115 Well- R 12/27/04 I -4,053 4,053 1,290 Well- R 01/19/05 2,420 159 129 Well- R 02/09/05 2,450 150 123 0.122 45 Well- R 03/15/05 2,704 147 125 Well- R 04/11/05 2,742 157 132 Well- R 05/03/05 2,755 151 128 Well- R 06/22/05 2,736 151 127 Well- R 07/20/05 2,486 147 122 Well- R 08/16/05 2,752 155 130 Well- R 09/20/05 2,673 159 131 Well- R 10/10/05 2,435 149 123 Well- R 11/14/05 2,149 148 119 Well- R 12/13/05 I ý4,370 4,370 NA Well- R 01/17/06 2,131 151 120 Well- R 02/21/06 2,262 153 122 Well- R 03/20/06 j 4,350 3,730 1,560 Well- R 04/11/06 2,192 160 125 Well- R 05/16/06 2,010 150 118 Well- R 06/19/06 2,067 160 124 Well- R 07/18/06 2,090 156 123 Well- R 08/08/06 1,940 148 116 Well- R 09/18/06 2,138 162 126 Well- R 10/10/06 1,943 157 121 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 18 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) Sodium(mgIL)
Well- R 11/15/06 2,395 164 132 ....
Well- R 12/18/06 3,092 154 134 ....
Well- R 01/13/07 3,208 154 135 ....
Well- R 02/23/07 3,563 167 146 ....
Well- R 03/08/07 3,487 161 143 ....
Well- R 04/20/07 3,180 157 138 ....
Well- R 05/15/07 2,567 138 118 ....
Well- R 06/18/07 2,844 142 122 ....
Well- R 07/18/07 2,862 145 124 ....
Well- R 08/15/07 3,000 143 125 ....
Well- R 09/20/07 3,104 144 127 ....
Well- R 10/03/07 2,799 149 129 ....
Well- R 11/14/07 3,029 141 124 ....
Well- R 12/12/07 2,951 145 125 ....
Well- R 01/17/08 2,892 140 122 ....
Well- R 02/06/08 2,941 150 128 ....
Well- R 03/18/08 3,159 150 131 ....
Well- R 04/02/08 3,294 154 134 ....
Well- R 05/08/08 3,173 155 133 ....
Well- R 06/19/08 3,196 135 122 ....
Well- R 07/07/08 3,077 140 124 ....
Well- R 08/06/08 3,158 142 126 ....
Well- R 09/02/08 3,075 134 120 ....
Well- R 11/19/08 2,998 149 128 ....
Well- R 12/15/08 3,075 150 129 ....
Well- S 07/09/03 3SO.O 1,5 134 3,120 Well- S 08/07/03 1 29o*ooo NA NA ....
Well- S 08/21/03 1 27O.OO f NA NA Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F20000Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 19 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note rResult (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well- S 09/03/03 NA NA Well- S 09/15/03 2,340,0011 NA NA.
Well- S 10/04/03 2AS0,0011 NA NA Well- S 10/13/03 2.010,000 NA NA 1
Well- S 10/20/03 2JII 0, 1100 NA NA 1
Well- S 10/20/03 2,1100J)OO NA NA 1
Well- S 11/09/03 1ý060,0110 NA NA 1
Well- S 11/09/03 NA NA Well- S 11/09/03 2. 1)4 1),0110 NA NA Well- S 11/26/03 1 6 6 1),0 1111 NA NA Well- S 01/20/04 A20,0110 NA NA Well- S 02/17/04 1 1,250,000 NA NA Well- S 03/18/04 1 120,01111 NA Well- S 04/06/04 1 1.160.000 4,706 15,206 Well- S 05/04/04 1 1.100.01it) 5,589 15,212 44.5 35 Well- S 05/19/04 1 884,000 5,780 13,380 Well- S 06/25/04 1 1,020.0011 5,270 14,500 Well- S 07/13/04 qzý;'000 3,620 13,800 Well- S 08/09/04 IS-6.000 4,850 13,000 45 Well- S 09/13/04 84;,000 4,560 13,000 1
Well- S 11/08/04 8211.001) 3,230 12,800 Well- S 12/28/04 601.01111 4,060 11,300 Well- S 01/11/05 -53,000 3,910 12,100 Well- S 02/15/05 714,(11)11 3,910 11,900 Well- S 03/07/05 ;04.000 3,490 8,570 Well- S 03/14/05 1 7mZj)()(1 4,320 6,110 Well- S 03/23/05 I ý 2.000 3,790 6,190 Well- S 03/28/05 6,280 .3,540 Well- S 04/18/05 3'f'.000 4,420 8,380 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
- Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 20 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD I Deviation Boron(mg/L) Sodium(mg/L)
Well- S 10/17/05 1 90,0 3,790 4,570 ....
Well- S 11/15/05 1 64,70 3,430 3,840 Well-S 12/12/05 69 155 446 Well- T 07/10/03 '147 147 88 ....
Well- T 07/15/03 -140 140 82 ....
Well- T 07/30/03 '141 141 86 ....
Well- T 08/12/03 '140 140 83 0.64 931 Well- T 08/28/03 '141 141 83 0.66 896 Well- T 09/09/03 '147 147 88 0.63 899 Well- T 09/25/03 -142 142 84 0.63 912 Well- T 10/06/03 '146 146 86 0.65 966 Well- T 12/12/03 '149 149 88 ....
Well- T 03/22/04 '142 1422 84 0.649 986 Well- T 04/12/04 '141 141 84 0.762 920 Well- T 07/07/04 148 148 87 ....
Well- T 08/02/04 '152 152 91 0.622 8994 Well- T 08/31/04 -147 147 87 ....
Well- T 09/22/04 -146 146 87 ....
Well- T 10/11/04 -155 155 91 ....
Well- T 11/09/04 '148 148 87 - --
W ell- T 12/21/04 1 '3,910 3,910 1,340 ....
Well- T 01/10/05 '165 165 96 ....
Well- T 02/01/05 137 135 83 0.638 945 W ell- T 03/03/05 '152 152 90 ....
W ell- T 04/05/05 '148 148 90 ....
Well- T 05/09/05 '144 144 86 ....
Well- T 07/05/05 -145 145 86 ....
Well- T 10/03/05 -149 149 90 --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
oCorstituent was detected above its New Jersey Groundwater Quality Criteria.
I Not Available - Deviation and/or LLD were not reported.
-- Constituent not inalyzed.
04/03/2009 10:37 AM Page 21 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- T 01/09/06 '154 154 90 ....
Well- T 04/03/06 -162 162 96 ....
Well- T 07/10/06 '161 161 95 ....
Well- T 10/05/06 '161 161 95 ....
Well- T 10/06/06 1 '6,270 6,270 NA ....
Well- T 01/23/07 193 152 94 ....
Well- T 04/11/07 '168 168 101 ....
Well- T 07/12/07 <147 147 86 ....
Well- T 10/09/07 -152 152 91 ....
Well- T 01/16/08 <141 141 85 ....
Well- T 04/22/08 -145 145 85 ....
Well- T 07/16/08 '130 130 77 ....
Well- T 10/21/08 '146 146 86 ....
Well- U 07/10/03 '136 136 83 Well- U 07/16/03 146 NA 86 Well- U 07/29/03 -141 141 96 ....
Well- U 08/12/03 '139 139 84 0.34 139 Well- U 08/27/03 '143 143 87 0.35 144 Well- U 09/09/03 148 147 90 0.38 139 Well- U 09/25/03 '139 139 83 0.34 155 Well- U 10/06/03 203 145 90 0.35 140 Well- U 12/12/03 '148 148 86 ....
Well- U 03/22/04 -144 144 88 0.38 168 Well- U 04/12/04 182 136 84 0.392 146 Well- U 07/07/04 162 150 92 ....
Well- U 08/02/04 '152 152 91 0.346 143 Well- U 08/31/04 '148 148 90 -- --
Well- U 09/22/04 167 152 93 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
oiliij Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 22 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station..
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium I Maj r Cations and Anions Identification Date INote IResult (pCi/) ILLD IDeviation IBoron(mgfL) SoiMdm/
Well- U 10/04/04 '146 146 87 ....
Well- U 11/03/04 165 148 91 ....
Well- U 12/06/04 1 -4,520 4,520 1,160 ....
Well- U 01/10/05 ,157 157 93 ....
Well- U 02/08/05 -149 149 91 0.377 156 Well- U 03/03/05 '147 147 88 ....
Well- U 04/05/05 '142 142 86 ....
Well- U 05/09/05 -148 148 90 ....
Well- U 07/05/05 '143 143 87 -- --
Well- U 10/03/05 284 150 94 ....
Well- U 01/09/06 -157 157 94 ....
Well- U 04/03/06 '154 154 93 ..
Well- U 04/06/06 1 '5,000 5,000 NA - --
Well- U 07/10/06 -157 157 95 ....
Well- U 10/05/06 '160 160 98 ....
Well- U 10/06/06 1 '6,270 6,270 NA ....
Well- U 01/22/07 163 152 93 ....
Well- U 04/11/07 -167 167 102 ....
Well- U 07/12/07 -150 150 91 ....
Well- U 10/09/07 <153 153 92 ....
Well- U 01/16/08 '138 138 84 ....
Well- U 05/28/08 -148 148 90 ....
Well- U 07/16/08 189 128 79 ....
Well- U 10/20/08 1 145 145 88 ....
T Well- V 07/21/03 334 140 89 Well- V 07/29/03 285 142 89 Well- V 08/12/03 278 142 89 0.5 568 Well- V 08/27/03 338 141 90 0.61 584 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
' Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 23 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well- V 09/09/03 337 150 95 0.57 582 Well- V 09/25/03 261 140 87 0.47 670 Well- V 10/06/03 185 144 89 0.46 543 Well- V 11/19/03 '3,300 3,300 NA Well- V 12/12/03 207 147 91 Well- V 03/22/04 290 144 90 0.46 556 Well- V 04/12/04 316 137 87 0.529 567 Well- V 07/07/04 228 145 90 Well- V 08/02/04 309 154 97 0.433 504 Well- V 08/31/04 395 151 96 Well- V 09/22/04 402 141 91 Well- V 10/04/04 340 146 92 Well- V 11/03/04 224 143 89 Well- V 12/06/04 -4,170 4,170 1,360 Well- V 01/10/05 394 151 96 Well- V 02/08/05 307 152 95 Well- V 03/03/05 157 156 95 0.436 431 Well- V 04/05/05 294 141 89 Well- V 05/09/05 244 155 96 Well- V 07/05/05 197 144 89 Well- V 10/03/05 346 147 93 Well- V 01/09/06 264 157 98 Well- V 04/03/06 <152 152 93 Well- V 07/10/06 181 157 96 Well- V 10/05/06 '159 159 95 Well- V 01/22/07 199 157 97 Well- V 04/11/07 154 149 92 Well- V 07/12/07 163 153 94 Well- V 10/09/07 170 153 94 Notes:
LLD Lower Limit of Detection rng/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
- Constituent was detected above its New Jersey Groundwater Quality Criteria.
~Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 24 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- V 01/16/08 176 139 86 ....
Well- V 05/28/08 186 147 90 ....
Well- V 07/16/08 164 130 80 ....
Well- V 10/20/08 195 145 89 .....
Well- W 07/07/03 10,500 135 189 ....
Well- W 07/21/03 11,100 140 196 ....
Well- W 08/06/03 11,500 141 200 0.46 211 Well- W 08/07/03 1 6,010 NA NA ....
Well- W 08/19/03 10,700 142 194 0.59 215 Well- W 09/03/03 10,500 143 192 0.53 222 Well- W 09/15/03 10,900 140 195 0.57 237 Well- W 10/03/03 11,100 147 202 0.46 240 Well- W 10/21/03 10,600 147 195 ....
Well- W 11/17/03 1 12,200 NA NA ....
Well- W 11/19/03 1 13,200 NA NA ....
Well- W 12/16/03 1 15,500 NA NA ....
Well- W 12/16/03 15,200 147 226 ....
Well- W 01/14/04 )17,100 144 232 ....
Well- W 02/02/04 19,600 144 251 ....
Well- W 03/03/04 5,320 146 151 0.28 273 Well- W 04/29/04 4,570 140 140 0.14 212 Well- W 05/10/04 2,350 141 117 ....
Well- W 05/24/04 4,080 146 139 ....
Well- W 06/24/04 5,300 141 149 ....
Well- W 07/28/04 11,691 154 208 ....
Well- W 08/02/04 11,910 148 204 ....
Well- W 08/31/04 11,091 160 211 ....
Well- W 09/22/04 9,571 138 186 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
'NX Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 25 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well- W 10/11/04 9,947 147 194 Well- W 11/08/04 8,920 150 186 0.487 309 Well- W 12/14/04 5,560 3,230 1,390 Well- W 01/10/05 6,292 150 165 0.681 273 Well- W 02/01/05 7,340 159 178 Well- W 03/02/05 5,756 150 158 3.33 27 Well- W 04/05/05 8,826 155 192 Well- W 05/02/05 12,339 147 209 Well- W 06/06/05 11,480 154 207 Well- W 07/06/05 16,672 149 239 Well- W 08/01/05 14,920 149 227 Well- W 09/06/05 17,419 154 247 Well- W 10/03/05 12,455 149 211 Well- W 11/14/05 3,430 2,460 Well- W 12/20/05 3,430 2,830 Well- W 01/17/06 3,550 3,380 Well- W 02/07/06 3,090 3,470 Well- W 02/21/06 3,920 3,620 Well- W 03/07/06 3,310 3,750 Well- W 03/20/06 3,730 3,850 Well- W 04/03/06 5,000 3,880 Well- W 04/17/06 5,510 4,240 Well- W 05/02/06 5,000 3,800 Well- W 05/15/06 *5,000 3,870 Well- W 06/06/06 155 374 Well- W 06/19/06 4,890 3,500 Well- W 07/10/06 3,755 161 144 Well- W 07/24/06 1,234 152 109 3,471 Well- W 08/07/06 158 139 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AMP Page 26 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well- W 08/21/06 5,284 162 162 Well- W 09/07/06 12,991 158 220 Well- W 09/18/06 15,311 166 242 Well- W 10/09/06 18,859 166 266 Well- W 10/24/06 9,929 155 194 Well- W 11/01/06 12,968 170 231 Well- W 11/15/06 14,464 171 245 Well- W 12/07/06 10,046 184 220 Well- W 12/19/06 15,062 139 221 Well- W 01/13/07 18,705 152 259 Well- W 02/05/07 147 278 Well- W 03/08/07 5,838 165 169 Well- W 04/20/07 1,616 159 120 Well- W 06/18/07 1,530 142 107 Well- W 07/18/07 2,462 147 121 Well- W 08/15/07 3,000 147 127 Well- W 09/20/07 6,562 149 164 Well- W 10/03/07 12,492 165 229 Well- W 11/14/07 13,071 123 202 Well- W 12/12/07 13,940 147 216 Well- W 01/17/08 10,203 140 186 Well- W 02/06/08 6,988 141 162 Well- W 03/18/08 2,507 137 116 Well- W 04/02/08 4,169 157 145 Well- W 05/08/08 4,545 146 142 Well- W 06/19/08 5,909 135 149 Well- W 07/07/08 6,880 127 153 Well-W 08/06/08 1,966 132 106 Well- W 09/02/08 2,535 134 114 Notes:
LLD . Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
jjOfl Constituert was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 27 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ITritium -I Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- W 11/18/0 8 2,919 133 118 -
Well- W 12/15/08 2,996 139 123 ....
Well- X 08/20/03 Ii '4,820 4,820 NA - T -
Well- X 07/20/05 1,500 NA NA [ ...
Well- Y 10/27/03 '142 142 85 ....
Well- Y 11/09/03 '143 143 85 ....
Well- Y 11/19/03 1 -3,750 3,750 NA ....
Well- Y 11/25/03 '141 141 85 0.82 1,070 Well- Y 12/12/03 '148 148 87 ....
Well- Y 12/22/03 '147 147 87 ....
Well- Y 01/06/04 '142 142 85 ....
Well- Y 02/02/04 -145 145 84 ....
Well- Y 02/02/04 1 5,390 5,390 NA ....
Well- Y 03/23/04 145 145 86 ....
Well- Y 04/07/04 '136 136 82 0.83 1,080 Well- Y 05/10/04 143 143 .85 ....
Well- Y 06/24/04 141 141 86 0.82 1,060 Well- Y 07/28/04 '156 156 90 ....
Well- Y 08/02/04 '157 157 94 -- -
Well- Y 08/31/04 -145 145 87 ....
Well- Y 09/08/04 '158 158 94 ....
Well- Y 10/11/04 -162 162 96 ....
Well- Y 11/08/04 -151 151 88 ....
Well- Y 12/13/04 1 '3,230 3,230 1,150 ....
Well- Y 01/10/05 -162 162 94 0.801 1,160 Well- Y 02/01/05 '154 154 92 -- --
Well- Y 03/07/05 -149 149 89 ....
Well- Y 04/06/05 <144 144 84 0.761 1,190 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 2 8 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium IaMajor Cations and Anions Identification I Date INote Resulit (pCi/L) LLD Deviation IBoron(mg/L) ISodium(mg/L)
Well- Y 05/25/05 -155 155 92 1,230 Well- Y 06/07/05 ,155 155 92 Well- Y 07/20/05 '159 159 93 1,270 Well- Y 08/01/05 '149 149 89 1,290 Well- Y 09/07/05 *149 149 89 Well- Y 10/04/05 *151 151 91 Well- Y 11/01/05 ,155 155 93 Well- Y 12/13/05 -151 151 91 Well- Y 01/17/06 '157 157 94 Well- Y 02/07/06 '161 161 94 Well- Y 03/07/06 -158 158 93.
Well- Y 04/04/06 S173 173 101 Well- Y 05/02/06 '156 156 91 Well- Y 05/16/06 -152 152 90 Well- Y 06/06/06 -159 159 93 Well- Y 06/19/06 -165 165 97 Well- Y. 07/11/06 -160 160 96 Well- Y 07/24/06 -155 155 92 Well- Y 08/07/06 '155 155 93 Well- Y 08/22/06 -157 157 96 Well- Y 09/07/06 '157 157 94 Well- Y 09/19/06 '161 161 95 Well- Y 10/09/06 -171 171 102 Well- Y 10/24/06 '171 171 100 Well- Y 11/01/06 -166 166 100 Well- Y 11/15/06 -166 166 98 Well- Y 12/07/06 -193 193 109 Well- Y 12/18/06 -157 157 92 Well- Y 01/14/07 -155 155 93 Notesi LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
SConstituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 29 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCiIL) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well- Y 02/20/07 165 165 97 ...
Well- Y 03/14/07 -162 162 94 ....
Well- Y 04/19/07 '163 163 97 ....
Well- Y 05/16/07 '180 180 101 ....
Well- Y 06/19/07 '149 149 87 ....
W ell- Y 07/12/07 '155 155 91 ....
Well- Y 08/16/07 -146 146 87 ..
W ell- Y 09/20/07 -146 146 88 ....
Well- Y 10/04/07 ' 154 154 91 ...
Well- Y 11/20/07 ' 149 149 90 ....
W ell- Y 12/20/07 '140 140 82 ....
Well- Y 03/13/08 '138 138 82 ....
Well- Y 04/22/08 -146 146 86 ....
Well- Y 05/15/08 -148 148 87 ....
Well- Y 06/24/08 -147 147 87 ....
Well- Y 07/17/08 '138 138 83 ....
Well- Y 08/19/08 '134 134 79 ....
Well- Y 09/03/08 ' 134 134 79 ....
Well- Y 10/18/08 '133 133 80 ....
Well- Y 11/21/08 -131 131 78 ....
Well-Y 12/23/08 -132 132 78 ....
Well- Z 10/27/03 573 142 94 ....
Well- Z 11/09/03 '140 140 92 ....
Well- Z 11/19/03 1 -3,500 3,500 NA ....
Well- Z 11/24/03 583 141 93 0.5 519 Well- Z 12/12/03 621 141 94 -- --
Well- Z 12/22/03 659 140 94 ....
Well- Z 01/06/04 648 142 95 --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
I Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 30 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Ia Major Cations and Anions Identification Date INote ýResulIt (pCiIL) ILLD IDeviation IBoron(mg/L) SoiMdm/
Well- Z 02/02/04 538 145 95 Well- Z 03/23/04 412 144 92 Well- Z 04/07/04 580 137 91 0.5 531 Well- Z 05/10/04 561 142 93 Well- Z 06/24/04 474 147 95 0.51 510 Well- Z 07/28/04 519 150 97 Well- Z 07/29/04 519 150 97 Well- Z 08/02/04 706 159 106 Well- Z 08/31/04 585 152 100 Well- Z 09/08/04 444 141 91 Well- Z 10/11/04 268 144 90 Well- Z 11/08/04 339 155 .98 0.491 548 Well- Z 12/13/04 I -3,230 3,230 1,060 Well- Z 01/10/05 249 159 99 Well- Z 02/01/05 228 153 95 Well- Z 03/07/05 192 153 94 0.535 688 Well- Z 04/06/05 274 165 103 0.506 716 Well- Z 05/25/05 <149 149 91 635 Well- Z 06/07/05 182 149 91 Well- Z 07/20/05 177 158 97 702 Well- Z 08/01/05 202 147 91 696 Well- Z 08/16/05 ,160 160 98 Well- Z 08/29/05 186 149 91 Well- Z 09/07/05 201 149 92 Well- Z 09/19/05 <156 156 94 Well- Z 10/04/05 271 148 93 Well- Z 10/18/05 -153 153 93 Well- Z 11/01/05 <158 158 94 Well- Z 12/13/05 ,157 157 96 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2F 7 Constituent was detected above its New Jersey Groundwater Quality Criteria.
~Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 31 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Io Major Cations and Anions Identification Date INote ýResult (pCiIL) I LLD Deviation IBoron(mg/L) ISodium(mg/L)
Well- Z 01/17/06 '153 153 93 Well- Z 02/07/06 240 149 93 Well- Z 02/21/06 238 152 94 Well- Z 03/07/06 1 -3,310 3,310 NA 1
Well- Z 03/20/06 -3,730 3,730 NA Well- Z 04/04/06 -177 177 108 Well- Z 04/17/06 -160 160 96 Well- Z 05/02/06 -153 153 93 Well- Z 05/16/06 '151 151 93 Well- Z 06/06/06 '163 163 99 Well- Z 06/19/06 '155 155 94 Well- Z 07/11/06 194. 159 98 Well- Z 07/24/06 211 151 93 Well- Z 08/07/06 -157 157 96 Well- Z 08/22/06 217 161 99 Well- Z 09/07/06 -160 160 97 Well- Z 09/19/06 -163 163 99 Well- Z 10/09/06 -160 160 95 Well- Z 10/24/06 -160 160 97 Well- Z 11/01/06 -162 162 97 Well- Z 11/15/06 248 155 96 Well- Z 12/07/06 -203 203 120 Well- Z 12/18/06 -175 175 107 Well- Z 01/14/07 '155 155 94 Well- Z 02/20/07 -152 152 91 Well- Z 03/14/07 -164 164 98 Well- Z 04/19/07 217 160 99 Well- Z 05/16/07 -143 143 85 Well- Z 06/19/07 154 148 90 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
~'Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 32 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well- Z 07/12/07 '150 150 90 ....
Well- Z 08/16/07 -146 146 88 ....
Well- Z 09/20/07 156 145 89 ....
Well- Z 10/04/07 173 153 94 ....
Well- Z 11/20/07 '147 147 90 ....
Well- Z 12/20/07 -138 138 83 ....
Well- Z 03/13/08 -137 137 84 ....
Well- Z 04/22/08 -143 143 86 ....
Well- Z 05/15/08 '148 148 89 ....
Well- Z 06/24/08 136 136 83 ....
Well- Z 07/17/08 '138 138 84 ....
Well- Z 08/19/08 173 134 83 ....
Well- Z 09/03/08 195 134 83 ....
Well- Z 10/18/08 278 132 83 ....
Well- Z 11/21/08 289 132 83 ....
Well- Z 12/23/08 253 133 83 ....
Well-AA 10/27/03 613 141 93 ....
Well-AA 11/10/03 645 141 94 ....
Well-AA 11/19/03 1 3,750 NA NA ....
Well-AA 11/24/03 639 145 96 0.25 253 Well-AA 12/10/03 785 141 96 ....
Well-AA 12/22/03 682 142 95 ....
Well-AA 01/06/04 713 141 95 ....
Well-AA 02/09/04 1,130 139 100 ....
Well-AA 02/19/04 1 '5,390 5,390 NA ....
Well-AA 03/18/04 2,610 140 120 ....
Well-AA 04/12/04 3,140 140 126 2.40E-01 169 Well-AA 05/03/04 1 '5,590 5,590 1,770 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 33 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008.
Well Sample Tritium I Major Cations and Anions Identification Date INote [Result (pCiIL) ILLD IDeviation IBoron(mg/L) ISodium(mgfL)
Well-AA 05/19/04 ,3,320 3,320 1,198 <3.3 168 Well-AA 06/23/04 4,376 142 141 <3.33 138 Well-AA 07/29/04 1,650 156 118 Well-AA 08/02/04 1,580 148 112 Well-AA 08/31/04 1,543 159 118 Well-AA 09/08/04 1,512 152 113 Well-AA 10/11/04 1,529 146 110 Well-AA 11/08/04 1,927 152 118 0.59 147 Well-AA 12/14/04 ,3,230 3,230 1,130 Well-AA 01/11/05 6,640 151 168 Well-AA 02/02/05 11,100 154 205 Well-AA 02/02/05 11,150 155 205 Well-AA 03/07/05 142 260 0.036 152 Well-AA 04/06/05 4,220 2,970 Well-AA 05/02/05 3,320 2,310 Well-AA 06/06/05 16,136 150 235 Well-AA 07/06/05 14,547 150 226 Well-AA 08/01/05 13,174 155 220 Well-AA 09/06/05 15,887 150 234 Well-AA 09/07/05 13,500 4,940 2,271 Well-AA 10/03/05 10,930 148 199 Well-AA 11/01/05 8,911 159 189 Well-AA 12/08/05 5,255 147 151 Well-AA 01/10/06 6,416 159 168 Well-AA 02/06/06 5,683 182 177 Well-AA 03/06/06 4,251 157 146 WelI-AA 04/04/06 3,483 158 140 Well-AA 05/01/06 3,625 149 137 Well-AA 06/06/06 2,813 168 138 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
t Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 34 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well ti Sample N I Tritium Ia Major Cations and Anions Identification Date INote IResult (pCi/L) ILLD IDeviation IBoron(mg/L) I Sodium(mgfL)I WelU-AA 07/17/06 2,745 162 133 Well-AA 08/08/06 2,647 157 129 Well-AA 09/06/06 2,651 158 130 Well-AA 10/09/06 2,302 158 126 Well-AA 11/02/06 2,413 167 133 Well-AA 12/08/06 1,847 179 134 Well-AA 01/13/07 2,236 161 128 Well-AA 02/05/07 1,518 147 110 Well-AA 03/07/07 1,871 155 120 Well-AA 04/19/07 1,805 158 121 Well-AA 05/15/07 1,422 167 120 WellAA 06/18/07 1,336 144 105 Well-AA 07/13/07 1,569 148 110 Well-AA 08/15/07 1,423 144 106 WelI-AA 09/19/07 1,238 150 107 Well-AA 10/03/07 1,460 161 119 WelI-AA 11/14/07 1,166 141 103 Well-AA 12/12/07 1,521 137 104 WelI-AA 01/23/08 1,570 142 107 WelI-AA 02/21/08 1,414 140 104 Well-AA 03/12/08 1,569 138 105 Well-AA 04/01/08 1,536 151 112 Well-AA 05/08/08 1,474 146 108 Well-AA 06/19/08 1,498 146 108 Well-AA 07/07/08 1,423 138 103 Well-AA 08/07/08 1,459 131 99 Well-AA 09/02/08 1,475 134 101 WelI-AA 10/17/08 1,360 135 100 Well-AA 11/18/08 1,381 131 98 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2g ]Constituent.was detected above its New Jersey Groundwater Quality Criteria.
~Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 35 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) Sodium(mg/L)
Well-AA 12/15/08 1 1,456 1 135 1I -- I -- I Well-AB 10/28/03 1
- NA NA ....
Well-AB 11/02/03 1 8001) NA NA ....
Well-AB 11/19/03 1 321J)00 NA NA ....
Well-AB 12/04/03 1 409000I NA NA ....
Well-AB 12/16/03 1 600 NA NA ....
Well-AB 12/16/03 1 4A .1 NA NA ....
Well-AB 01/14/04 1 281,000 NA...
Well-AB 02/17/04 1 K214.000 NA NA ....
Well-AB 03/03/04 1 3 11 NA NA ....
Well-AB 04/06/04 1 '260110 4,706 7,380 -- --
Well-AB 05/04/04 1 136.000. 5,589 5,817 9.3 134 Well-AB 05/11/04 1 10 5,392 5,967 -- --
Well-AB 05/19/04 1 10 5,780 6,108 <3.3 292 Well-AB 05/24/04 1 2 0 4,563 6,779 -- --
Well-AB 06/03/04 1 210000 4,563 6,746 <3.3 105 Well-AB 06/17/04 1 104.0011 5,666 6,509 -- --
Well-AB 07/07/04 1 *20.2.011 3,360 6,330 -- -
Well-AB 07/12/04 1 206,000 3,620 6,380 -- --
Well-AB 07/19/04 1 0 0 2,870 6,160 8.12 156 Well-AB 07/28/04 1 23000 4,280 6,600 -- --
Well-AB 08/02/04 1 184.000 4,420 6,120 ...--
Well-AB 08/09/04 1 1(,4.0 4,850 5,840 -- 214 Well-AB 08/16/04 1 0 3,320 5,490 -- -
Well-AB 08/25/04 1 V1 100 3,030 5,880 ....
Well-AB 09/01/04 1 3180.000 4,520 6,220 ....
Well-AB 09/08/04 1 .165.OO0" 3,790 5,750 -- --
Well-AB 09/13/04 1 1101 4,560 5,980 15.90 212 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
21j Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 36 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ItTritium MaijLr Cat-ions and Anions Identification IDate INote lResult (pCiIL) I-LLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-AB 09/22/04 166,OU0 5,230 5,910 Well-AB 10/04/04 I :;2, 0 00 3,320 6,000 Well-AB 10/12/04 1521000 1 2,220 5,520 Well-AB 10/18/04 3,230 5,340 Well-AB 11/03/04 2,720 5,850 Well-AB 11/08/04 3,230 5,650 Well-AB 11/15/04 3,910 5,800 Well-AB 11/29/04 2,650 5,730ý Well-AB 12/13/04 146MOO 3,230 5,410 Well-AB 01/11/05 3,910 5,330 Well-AB 01/27/05 60,001) 2,470 5,650 Well-AB 01/31/05 1 ;6.600 4,560 5,770 Well-AB ,02/01/05 1:;5MOO 2,650 5,630 Well-AB 02/08/05 14 1,0110 4,660 5,560 Well-AB 03/02/05 1;A 3-6 144 664 Well-AB 03/07/05 1011,0110 3,490 5,770 Well-AB 03/14/05 4,320 5,760 Well-AB 03/23/05 1 3,790 5,830 Well-AB 03/28/05 1 6,280 5,920 Well-AB 04/18/05 13'5,0111) 4,420 5,470 Well-AB 05/18/05 '24,000 3,490 7,050 Well-AB 06/22/05 97,101) 3,750 4,460 Well-AB 08/15/05 71 3,905 3,950 Well-AB 10/17/05 59,200 3,790 3,730 Well-AB 11/15/05 00"'501) 3,430 3,740 Well-AB 12/12/05 ý;2.1000 4,370 3,600 Well-AB 01/24/06 411,'00 3,550 3,480 Well-AB 02/23/06 38.900 3,920 3,200 Well-AB 03/21/06 4 8,5 U1) 3,730 3,580 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
MConstituent was detected above its New Jersey Groundwater Quality Criteria.
NA- Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 37 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cation/ andAnions Identification Date INote lResult (pCiIL) I LLD IDeviation Boron(mg/L) I Sodium(mg/L)
Well-AB 04/17/06 1 ý)00 5,510 3,990 Well-AB 05/15/06 1 3 9," 5,000 3,590 Well-AB 06/20/06 1 4 1) 4,890 3,680 Well-AB 07/24/06 1 5,470 3,540 Well-AB 09/21/06 1 42..30) 7,550 3,700 Well-AB 01/23/07 5,014 159 158 Well-AB 02/06/07 172 387 Well-AB 06/19/07 31 145 316 Well-AB 08/23/07 2(,.13 141 283 Well-AB 09/20/07 148 283 Well-AB 10/17/07 2114 151 286 Well-AB 10/07/08 1,294 150 108 Well-AC 10/28/03 1 10,900.1100 NA NA 253 31 Well-AC 11/03/03 332 --
Well-AC 11/03/03 1 14,000- NA NA 332- 30 Well-AC 11/18/03 1 14,...0 NA NA -- --
Well-AC 11/18/03 1 14,0.0 NA NA ....
Well-AC 12/18/03 1 1;000 NA NA -- --
Well-AC 01/20/04 1 1070 0M NA NA ....
Well-AC 02/18/04 1 1
- NA NA ....
Well-AC 03/18/04 1 "3600 NA NA ....
Well-AC 04/08/04 1 000 5,822 36,309 --...
Well-AC 06/04/04 1 000 6,283 26,713 <3.3 12 Well-AC 07/07/04 1 700 3,360 23,200 -- --
Well-AC 07/28/04 1 3l0om 4,280 25,100 ....
Well-AC 08/02/04 1 400 3,320 23,400 -- --
Well-AC 08/09/04 1 2,30, 4,850 20,900 17.90 71 Well-AC 08/16/04 1 -1, 3,320 20,400 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria, N Not Available -Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 38 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date INote IResult (pCi/L) I LLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-AC 08/25/04 3,030 19,900 Well-AC 09/01/04 4,520 19,400 Well-AC 01/11/05 3,910 11,600 Well-AC 01/17/05 3,360 11,600 Well-AC 02/09/05 4,660 11,200 Well-AC 04/29/05 3,320 2,650 Well-AC 05/24/05 3,320 2,760 Well-AC 06/16/05 3,750 2,520 Well-AC 07/29/05 3,320 2,340 Well-AC 08/18/05 4,753 6,877 Well-AC 09/26/05 4,220 3,390, Well-AC 11/21/05 13686J0 *4,370 2,520 Well-AC 12/12/05 4,370 3,340 Well-AC 01/12/06 3,550 2,770 Well-AC 02/28/06 153 239 Well-AC 03/23/06 3 2.900~ 5,000 3,360 Well-AC 06/16/06 158 226 Well-AC 07/14/06 152 192 Well-AC 08/23/06 5,100 5,340 Well-AC 09/27/06 159 224 Well-AC 11/17/06 143 284 Well-AC 12/28/06* 3,730 3,010 Well-AC 01/22/07 159 280 Well-AC 02/12/07 151 319 Well-AC 03/27/07 151 265 Well-AC 04/23/07 169 316 Well-AC 05/10/07 178 287 Well-AC 06/19/07 147 268 Well-AC 07/30/07 149 286 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
ýConstituent was detected above its New Jersey Groundwater Quality Criteria.
-Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 39 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
Iwo,, t-I I Well ti Identificaon Sample Date Note tResult (pCi/L) I T,o for Samples collected between 01/22/2003 and 12/31/2008 Tritium LLD I Deviation Major Cations and Anions Boron(mg/L) Sodium(mg/L)
Well-AC 08/28/07 144 308 ....
Well-AC 10/30/07 40,98 158 370 .....
Well-AC 11/27/07 3.0 123 300 ....
Well-AC 12/29/07 1 50 4,780 4,010 Well-AC 03/30/08 1 1* 4,540 3,780 ....
Well-AC 04/29/08 1 7 4,190 4,400 -- --
Well-AC 05/30/08 s
- 140 289 ....
Well-AC 06/18/08 260;6 135 272 .....
Well-AC 07/21/08 ' 139 277 ....
Well-AC 08/21/08 2 128 264 ....
Well-AC 09/22/08 2 145 267 ....
Well-AC 10/30/08 24 144 268 ...
Well-AC 11/25/08 133A266 .. .
Well-AC 12/15/08 29 152 294 ...
Well-AD 10/27/03 1 2441 NA NA..
Well-AD 11/02/03 1 20 NA NA Well-AD 11/17/03 1 225.01111 NA NA ....
Well-AD 12/04/03 1 4942000 NA NA Well-AD 12/04/03 1 3142000* NA NA ....
Well-AD 12/16/03 1 _______ NA NA ....
Well-AD 12/16/03 1 10 NA NA ....
Well-AD 01/14/04 1 =720000 NA NA -- --
Well-AD 02/17/04 1 401100 NA NA ....
Well-AD 03/03/04 1 421UMO NA NA ....
Well-AD 04/06/04 1 f; 20011 4,706 10,418 ....
Well-AD 05/04/04 1 624.0 5,589 11,649 5.8 65 Well-AD 05/11/04 1 59.0I
ý 5,392 11,469 Well-AD 05/19/04 1 611.000 5,780 11,152 <3.3 109 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 'Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 40 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Ia Major Cations and Anions Identification Date INote lResult (pCiJL) I LLD Deviation IBoron(mg/L) ISodiurn(mg/L)
Well-AD 06/03/04 4,563 12,461 <3.3 71 Well-AD 06/17/04 5,666 12,887 Well-AD 07/07/04 3,360 11,900 Well-AD 07/12/04 1 3,620 12,300 Well-AD 07/19/04 2,870 12,100 12.00 81 744,0110 Well-AD 07/28/04 4,280 12,500 Well-AD 08/02/04 3,030 12,600 Well-AD 08/09/04 4,850 1,230 12.80 90 Well-AD 08/16/04 I 3,320 13,000 Well-AD 12/28/04 4,060 1,130 Well-AD 03/02/05 *3,670 11,700 Well-AD 03/07/05 3,490 11,300 Well-AD 03/14/05 4,320 12,100 3S6,001)
Well-AD 03/23/05 3,790 10,700 Well-AD 03/28/05 6,280 3,640 Well-AD 04/18/05 4,420 10,000 4611111~i Well-AD 05/18/05 3,490 9,320 Well-AD 06/22/05 3,750 8,160 Well-AD 07/19/05 "44,.000 3,750 7,610 Well-AD 08/15/05 3,905 6,575 Well-AD 10/17/05 3,790 7,010
'Well-AD 11/15/05 3,430 6,700 Well-AD 12/12/05 1~ 4,370 5,860 Well-AD 01/24/06 3,550 5,710 Well-AD 02/23/06 3,920 5,640 Well-AD 03/21/06 3,730 5,330 Well-AD 04/17/06 5,510 5,460 Well-AD 05/15/06 5,000 5,780 Well-AD 06/20/06 4,890 4,870 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
]Constituent was detected above its New Jersey Groundwater Quality Criteria.
X Not Available -Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 41 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium T Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) Sodium(mg/L)
Well-AD 07/24/06 1 S(,1 5,470 4,650 ....
Well-AD 08/22/06 1 81 2,520 2,100 ....
Well-AD 09/21/06 1 7,550 4,240 ....
Well-AD 10/06/06 1 _160 6,270 4,430 Well-AD 11/16/06 7 43 168 517 ....
Well-AD 12/15/06 7 147 471 --
Well-AD 01/23/07 155 4815....
Well-AD 02/06/07 1 0 0 4,370 4,130 ....
Well-AD 03/14/07 1 ;6.1101) 4,020 3,770 Well-AD 06/19/07 1 6S.400 3,430 4,300@
Well-AD 07/19/07 1 67 4,530 4,200 Well-AD 08/23/07 1 -L300 4,280 4,520 Well-AD 09/20/07 6.; 146 431 ....
Well-AD 10/17/07 42 167 416 ....
Well-AD 11/15/07 46 123 351 Well-AD 12/13/07 4t 148 376 ....
Well-AD 01/24/08 4 140 372 Well-AD 03/12/08 77 146 416 ....
Well-AD 04/23/08 1 58 00 5,060 4,090 Well-AD 05/09/08 1,197 148 105 ....
Well-AD 06/12/08 1 (A11 5,210 3,980 -
Well-AD 07/16/08 1 67 4,780 4,060 ....
Well-AD 09/22/08 f 7,2> 134 394 ....
Well-AE 10/27/03 5,990 145 156 0.23 14 Well-AE 11/02/03 1 5,710 NA NA ....
Well-AE 11/19/03 1 6,910 NA NA ....
Well-AE 12/04/03 10,200 146 190 0.17 10 Well-AE 12/18/03 1 16,100 NA NA ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 42 of 8 1
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well I Sample I Tritium Major Cations and Anions Identification Date LLD Deviation Boron(mg/L) I Sodium(mg/L)
Ir"ote IResult (pCi/L) I Well-AE 12/18/03 15,800 147 229 WeIl-AE 01/14/04 16,100 144 229 Well-AE 02/09/04 16,600 139 232 Well-AE 02/09/04 19,200 NA NA Well-AE 03/03/04 17,000 147 237 Well-AE 03/18/04 19,000 145 248 Well-AE 04/28/04 14,900 140 220 0.09 8 Well-AE 05/03/04 14,000 5,589 2,409 Well-AE 06/17/04 7,810 5,666 2,152 <3.33 11*
Well-AE 07/13/04 7,820 149 175 Well-AE 08/16/04 7,238 151 173 Well-AE 09/22/04 5,939 140 156 Well-AE 10/18/04 5,375 150 156 Well-AE 11/22/04 4,636 152 149 Well-AE 12/16/04 ,3,230 3,230 1,200 Well-AE 01/18/05 7,530 164 185 Well-AE 02/08/05 10,100 147 192 0.099 11 Well-AE 03/08/05 13,026 142 212 Well-AE 04/11/05 8,832 157 192 Well-AE 05/10/05 9,305 147 187 Well-AE 06/07/05 7,741 147 173 Well-AE 07/06/05 6,336 148 162 Well-AE 08/02/05 4,947 148 149 Well-AE 09/07/05 3,384 150 134 Well-AE 10/04/05 3,305 152 135 Well-AE 11/02/05 3,592 151 136 Well-AE 12/09/05 5,123 153 154 Well-AE 01/16/06 3,550 2,390 Well-AE 02/07/06 9,966 149 193 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
- j Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 43 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Io Major Cations and Anions Identiflcation Date INote IResult (pCiIL) ILLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-AE 03/07/06 I 13,400 3,310 2,000 Well-AE 04/04/06 9,924 161 200 Well-AE 05/02/06 7,075 150 171 Well-AE 06/19106 3,945 151 141 Well-AE 07/17/06 4,379 '160 150 Well-AE 08/21/06 3,822 152 140 Well-AE 09/18/06 11,860 167 219 Well-AE 10/05/06 4,300 161 151 Well-AE 11/02/06 5,226 161 160 Well-AE 12/07/06 5,000 172 167 Well-AE 01/13/07 4,289 156 150 Well-AE 02/24/07 5,721 170 171 Well-AE 03/07/07 4,749 143 146 Well-AE 04/20/07 5,233 156 159 Well-AE 05/16/07 8,428 153 182 Well-AR 06/18/07 6,863 146 164 Well-AE 07/19/07 5,663 146 153 Well-AE 08/15/07 5,174 147 149 Well-AE 09/19/07 4,064 144 137 Well-AE 10/04/07 4,065 158 149 Well-AE 11/19/07 4,673 151 153 Well-AE 12/12/07 4,998 148 148 Well-AE 01/16/08 7,322 140 165 Well-AE 02/07/08 9,715 151 190 Well-AE 03/12/08 10,326 152 196 Well-AE 04/01/08 11,548 160 210 Well-AE 05/08/08 10,692 140 188 Well-AE 06/19/08 7,902 134 163 Well-AE 07/16/08 7,569 143 168 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
~Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 44 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Io Major Cations and Anions Identification Date [Note lResult (pCiJL) ILLD IDeviation IBoron(mg/L) ISodhsiumgL WelI-AF 10/07/03 4142 142 86 0.38 227 Well-AF 10/27/03 1 ,2,430 2,430 NA WelI-AF 10/27/03 242 145 90 ....
Well-AF 11/10/03 330 144 91 ....
WelI-AF 11/24/03 245 146 91 0.43 545 Well-AF 12/10/03 343 140 89 ....
Well-AF 12/22/03 302 141 89 ....
W ell-AF 01/06/04 366 142 90 ....
Well-AF 01/20/04 262 143 89 ..
Well-AF 02/02/04 295 144 91 ....
Well-AF 03/18/04 150 144 88 .....
Well-AF 04/20/04 247 141 88 4.80E-01 654 Well-AF 05/03/04 308 141 89 ....
Well-AF 06/25/04 301 144 90 0.523 766 Well-AF 07/13/04 270 145 91 .....
Well-AF 08/16/04 177 156 96 ....
Well-AF 09/23/04 241 147 92 ....
Well-AF 10/12/04 151 151 90 ....
Well-AF 11/16/04 168 153 94 --...
Well-AF 12/21/04 1 -3,910 3,910 1,130 ....
Well-AF 01/11/05 1 -3,910 3,910 1,180 ....
WelI-AF 02/08/05 -154 154 94 0.644 843 Well-AF 03/14/05 1 -4,320 4,320 1,240 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L *Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2iioo Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 45 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anon Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well-AF 04/11/05 363 148 94 ....
Well-AF 05/09/05 245 143 89 ....
Well-AF 07/11/05 193 152 93 ....
WelI-AF 10/17/05 182 157 96 ....
Well-AF 01/16/06 264 152 95 ....
Well-AF 04/10/06 244 156 97 ....
Well-AF 07/17/06 372 154 97 ....
Well-AF 10/09/06 249 162 100 ....
Well-AF 01/22/07 347 158 99 -- --
Well-AF 04/19/07 223 165 102 ....
WelI-AF 07/13/07 210 146 90 ....
Well-AF 10/09/07 '173 173 101 ....
WelI-AF 01/23/08 158 139 85 ....
WelI-AF 04/22/08 '154 154 93 ....
Well-AF 07/16/08 177 143 88 ....
Well-AF 10/20/08 '137 137 81 ....
Well-AG-D 02/23/04 6,100 140 156 0.34 849 Well-AG-D 03/09/04 3,280 149 132 -- --
WeUI-AG-D 03/29/04 2,540 151 125 ..--
Well-AG-D 04/12/04 4,990 141 145 5.10E-01 765 WelI-AG-D 04/19/04 2,920 141 124 0.5 868 WelI-AG-D 04/28/04 896 135 95 0.38 866 Well-AG-D 05/03/04 1 '5,590 5,590 NA --...
Well-AG-D 05/10/04 1,490 140 106 5.60E-01 885 Well-AG-D 05/24/04 1,290 152 109 ..--
Well-AG-D 05/28/04 1 '4,560 4,560 1,551 ....
Well-AG-D 06/03/04 4,040 145 139 ....
Well-AG-D 06/08/04 13,625 142 214 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
211201Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 46 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2068 Well Sample ITritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) Sodium(mg/L)
Well-AG-D 06/16/04 566 154 101 0.18 239 Well-AG-D 06/25/04 1,865 141 111 0.539 862 Well-AG-D 07/07/04 2,698 141 121 -- --
Well-AG-D 07/14/04 3,426 142 130 0.506 798 Well-AG-D 07/19/04 2,718 152 128 -- --
Well-AG-D 07/28/04 2,939 145 127 0.518 826 Well-AG-D 08/09/04 4,217 148 143 0.533 883 Well-AG-D 08/23/04 6,538 156 171 -- --
Well-AG-D 09/13/04 7,191 149 172 ....
Well-AG-D 09/29/04 13,241 148 218 ....
Well-AG-D 10/05/04 8,613 156 190 ....
Well-AG-D 10/18/04 12,456 144 209 ....
Well-AG-D 11/04/04 7,424 139 167 ....
Well-AG-D 11/09/04 1 3,230 2,690 ....
WeUl-AG-D 11/15/04 11,993 150 209 ....
Well-AG-D 11/22/04 3,813 148 138 ....
Well-AG-D 11/29/04 1 8,860 2,650 1,580 ....
Well-AG-D 12/07/04 1 ,4,170 4,170 1,510 ....
Well-AG-D 12/14/04 1 6,910 3,230 1,500 ....
Well-AG-D 12/21/04 1 <3,910 3,910 1,370 ....
Well-AG-D 12/28/04 1 5,710 4,060 1,570 -- -
Well-AG-D 01/07/05 6,300 150 166 ....
Well-AG-D 01/11/05 8,700 143 180 -- --
Well-AG-D 01/18/05 4,880 154 153 0.823 836 Well-AG-D 01/26/05 4,040 141 139 -- --
Well-AG-D 02/02/05 6,455 155 168 ....
Well-AG-D 02/09/05 6,310 149 162 Well-AG-D 02/14/05 5,995 146 159 ....
Well-AG-D 02/22/05 958 155 107 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 47 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium I . Major Cations and Anions Idniiaio Dae INt esl (pCiIL) I LLD IDeviation -IBoron(mg/L) I Sodium(mg/L)
Well-AG-D 03/03/05 1,099 148 105 Well-AG-D. 03/07/05 937 155 106 Well-AG-D 03/14/05 1,026 143 101 Well-AG-D 03/23/05 1,203 149 107 Well-AG-D 03/28/05 1,217 141 102 Well-AG-D 04/05/05 764 169 113 0.39 1,060 Well-AG-D 04/18/05 938 162 111 0.344 971 Well-AG-D 05/03/05 1,380 149 109 958 Well-AG-D 05/16/05 798 144 98 876 Well-AG-D 06/06/05 883 148 102 929 Well-AG-D 07/11/05 884 149 102 858 Well-AG-D .08/01/05 762 144 97 865 Well-AG-D 09/06/05 1,170 149 106 Well-AG-D 10/11/05 901 147 101 Well-AG-D 11/01/05 995 150 104 Well-AG-D 12/08/05 712 146 98 Well-AG-D 01/09/06 525 156 101 Well-AG-D 02/06/06 575 177 114 Well-AG-D 03/06/06 620 159 104 Well-AG-D 04/03/06 270 156 97 Well-AG-D 05/01/06 486 152 99 Well-AG-D 06/05/06 685 155 102 Well-AG-D 07/11/06 763 162 108 Well-AG-D 08/07/06 720 153 102 Well-AG-D 09/18/06 663 158 104 Well-AG-D 10/06/06 413 160 101 Well-AG-D 11/15/06 671 160 106 Well-AG-D 12/08/06 496 198 126 Well-AG-D 01/14/07 543 159 103 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
( Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 48 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ITritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD I Deviation Boron(mg/L) Sodium(mg/L)
Well-AG-D 02/20/07 204 158 97 ....
Well-AG-D 03/14/07 201 179 110 ....
Well-AG-D 04/19/07 391 175 111 ....
Well-AG-D 05/03/07 633 141 94 ....
Well-AG-D 06/18/07 716 142 95 ....
Well-AG-D 07/12/07 490 151 97 ....
Well-AG-D 08/16/07 702 147 98 ....
Well-AG-D 09/20/07 608 144 95. -- --
Well-AG-D 10/17/07 2,172 149 118 -- -
Well-AG-D 11/20/07 1,491 150 113 ....
Well-AG-D 12/20/07 905 137 96 ....
Well-AG-D 01/23/08 1,019 154 106 ....
Well-AG-D 02/20/08 1,116 153 107 ....
Well-AG-D 03/13/08 1,141 137 99 -- --
Well-AG-D 04/01/08 1,153 149 106 ....
Well-AG-D 05/15/08 1,724 135 105 ....
Well-AG-D 06/24/08 1,974 136 1(09 ....
Well-AG-D 07/17/08 1,536 138 104 ....
WeIl-AG-D 08/18/08 1,205 134 98 ....
Well-AG-D 09/03/08 1,120 134 96 ....
Well-AG-D 10/17/08 1,367 132 99 ....
Well-AG-D 11/21/08 882 131 91 ....
Well-AG-D 12/23/08 1 1,070 134 96 Well-AG-S 02/23/04 2,320 138 115 0.04 348 Well-AG-S 03/09/04 3,000 146 126 -- --
Well-AG-S 03/29/04 4,810 153 150 ....
Well-AG-S 04/12/04 6,620 143 161 0.26 319 Well-AG-S 04/20/04 8,060 142 173 0.23 338 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
-Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 49 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Ia Major Cations and Anions Identification Date INote Result 7(pCiIL) ILLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-AG-S 04/28/04 10,300 136 188 0.19 312 Well-AG-S 05/10/04 9,580 139 184 Well-AG-S 05/24/04 9,390 147 189 Well-AG-S 05/26/04 11,300 5,780 2,281 Well-AG-S 05/27/04 18,300 4,563 2,383 Well-AG-S 05/28/04 14,400 4,563 2,193 Well-AG-S 06/03/04 17,329 150 242 Well-AG-S 06/08/04 13,226 154 220 Well-AG-S 06/16/04 17,244 145 237 0.247 286 Well-AG-S 06/25/04 20,049 152 263 0.271 300 Well-AG-S 07/07/04 13,528 147 217 Well-AG-S 07/14/04 17,361 149 241 0.243 323 Well-AG-S 07/19/04 12,601 149 210 Well-AG-S 07/26/04 3,230 2,230 341 15,617 Well-AG-S 07/28/04 147 232 0.231 315 Well-AG-S 07/30/04 4,850 2,700 365 Well-AG-S 08/09/04 144 263 0.241 321 Well-AG-S 08/23/04 3,025 2,176 Well-AG-S 09/13/04 10,430 151 200 Well-AG-S 09/29/04 7,074 160 179 Well-AG-S 10/05/04 11,088 154 207 Well-AG-S 10/18/04 16,353 143 233 Well-AG-S 11/04/04 15,313 150 231 Well-AG-S 11/09/04 3,230 2,320 Well-AG-S 11/15/04 3,910 2,390 Well-AG-S 11/22/04 4,220 2,350 Well-AG-S 11/29/04 2,650 2,220 Well-AG-S 12/07/04 .. 3.,00 4,170 2,480 Well-AG-S 12/14/04 3,230 2,330 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
I 04/03/2009 10:37 AM Page 50 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample N -_ Tritium Ia Major Cations andiAnLon Identification Date INote ýReslt (pCiIL) ILLD IDeviation IBoron(mg/L) ISodium(mg/L Well-AG-S 12/21/04 1 2 4,020 2,700 ....
Well-AG-S 12/28/04 1 2*2.0 4,060 2,380 -- --
Well-AG-S 01/07/05 1 2280'0 3,910 2,610 ....
Well-AG-S 01/11/05 1 1 3,910 2,770 ....
Well-AG-S 01/18/05 1 29A00 3,950 2,630 Well-AG-S 01/26/05 <21,600 149 267 ....
Well-AG-S 02/02/05 1 11200 2,650 2,660 -- --
Well-AG-S 02/02/05 1 29,700 4,660 2,810 Well-AG-S 02/09/05 1 271X00 4,660 2,710 ....
Well-AG-S 02/14/05 1 24 0 3,910 2,480 Well-AG-S 02/22/05 11,929 154 211 Well-AG-S .03/03/05 6,944 158 174 ....
Well-AG-S 03/07/05 7,239 136 164 ....
Well-AG-S 03/14/05 7,693 143 171 ....
Well-AG-S 03/23/05 9,248 147 187 ....
Well-AG-S 03/28/05 9,399 141 183 ....
Well-AG-S 04/05/05 9,357 143 187 0.175 240 Well-AG-S 04/18/05 3,472 152 138 0.144 426 Well-AG-S 05/03/05 6,858 151 169 -- 236 Well-AG-S 05/16/05 2,493 146 121 -- 192 Well-AG-S 06/06/05 1,007 148 103 -- 567 Well-AG-S 07/11/05 2,022 150 119 -- 582 Well-AG-S 08/01/05 3,537 151 136 -- 606 Well-AG-S 09/06/05 4,295 151 144 ....
Well-AG-S 10/11/05 6,309 146 160 ....
Well-AG-S 11/01/05 4,043 149 139 ....
Well-AG-S 12/08/05 349 150 95 ....
Well-AG-S 01/09/06 744 159 106 ....
Well-AG-S 02/06/06 1,551 165 121 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
n2ooo Constituent was detected above its New Jersey Groundwater Quality Criteria.
-Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 51 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium I Major Cations and Anions Identification IDate Note lResult (pCi/L) ILLD IDeviation IBoron(mg/L) ISodium(mg/L)I Well-AG-S 03/06/06 1,926 157 120 ....
Well-AG-S 04/03/06 1,616 159 118 ....
Well-AG-S 05/01/06 1,150 149 106 ..
Well-AG-S 06/05/06 639 158 103 ....
Well-AG-S 07/11/06 499 162 104 ....
Well-AG-S 08/07/06 453 158 101 ....
Well-AG-S 09/18/06 403 159 101 ....
Well-AG-S 10/06/06 339 165 103 ....
W ell-AG-S 11/15/06 602 158. 104 ....
Well-AG-S 12/08/06 487 194 123 ....
Well-AG-S 01/14/07 513' 157 102 ....
Well-AG-S 01/22/07 1 -4,610. 4,610 NA ....
Well-AG-S 02/20/07 406 152 97 -- --
Well-AG-S 03/14/07 336 190 118 ....
Well-AG-S 04/19/07 363 160 101 ....
Well-AG-S 05/03/07 201 142 88 ....
VWell-AG-S 06/18/07 888 141 97 ....
Well-AG-S 07/12/07 645 150 99 ....
Well-AG-S 08/16/07 1,101 144 102 ....
W ell-AG-S 09/20/07 671 146 97 ....
W ell-AG-S 11/20/07 304 142 90 ....
W ell-AG-S 12/20/07 343 137 87 ....
W ell-AG-S 01/23/08 291 151 94 ....
Well-AG-S 02/20/08 432 151 96 ....
W ell-AG-S 03/13/08 341 139 88 ....
Well-AG-S 04/01/08 320 144 91 -- --
Well-AG-S 05/15/08 383 147 93 -- --
Well-AG-S 06/24/08 633 136 91 ....
Well-AG-S 07/17/08 653 138 92 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
'762 Constituent was detected above the laboratory method detection limit.
[). Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 52 of 8 1
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) Sodium(mg/L)
Well-AG-S 07/21/08 1 -4,780 4,780 NA ....
Well-AG-S 08/18/08 590 133 88 ....
Well-AG-S 09/03/08 537 134 88 ....
Well-AG-S 10/17/08 1,074 133 95 ....
Well-AG-S 11/21/08 1,580 131 101 ....
Well-AG-S 12/23/08 2,405 143 119 ....
Well-AH-D 02/23/04 548 142 93 0.21 309 Well-AH-D 03/08/04 620 142 95 ....
Well-AH-D 03/29/04 522 142 93 0.31 290 Well-AH-D 04/19/04 563 140 93 0.19 241 Well-AH-D 05/03/04 637 142 95 ....
Well-AH-D 06/03/04 619 157 103 ....
Well-AH-D 06/16/04 1 -5,670 5,670 1,571 ....
Well-AH-D 07/19/04 552 147 97 0.191 260 Well-AH-D 08/23/04 586 140 93 ....
Well-AH-D 09/13/04 557 151 99 ....
Well-AH-D 09/29/04 517 155 101 ....
Well-AH-D 10/18/04 308 144 90 ....
Well-AH-D 11/15/04 1 '3,910 3,910 1,328 ....
Well-AH-D 12/20/04 1 '3,910 3,910 1,130 ....
Well-AH-D 01/11/05 487 154 100 0.235 250 Well-AH-D 02/15/05 493 147 96 ....
Well-AH-D 03/08/05 529 146 96 ....
Well-AH-D 04/18/05 407 150 96 0.298 673 Well-AH-D 05/16/05 492 146 95 -- 654 Well-AH-D 06/07/05 610 148 98 -- 1,020 Well-AH-D 07/11/05 665 143 96 ....
Well-AH-D 08/02/05 599 145 96 -- --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
260)Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 53 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cation. and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well-AH-D 09/07/05 522 151 98 Well-AH-D 10/17/05 361 156 99 Well-AH-D 11/02/05 403 152 97 WeIl-AH-D 12/09/05 257 151 94 Well-AH-D 01/10/06 260 151 94 Well-AH-D 02/06/06 264 165 102 Well-AH-D 03/06/06 318 156 98 Well-AH-D 04/10/06 303 155 97 Well-AH-D 05/01/06 439 152 98 Well-AH-D 06/05/06 297 157 98 Well-AH-D 07/17/06 321 160 100 Well-AH-D 08/08/06 330 157 98 Well-AH-D 09/06/06 322 161 101 Well-AH-D 10/06/06 278 162 101 Well-AH-D 11/02/06 430 152 97 Well-AH-D 12/19/06 209 159 98 Well-AH-D 01/22/07 333 159 100 Well-AH-D 02/20/07 -177 177 108 Well-AH-D 03/14/07 <155 155 94 Well-AH-D 04/19/07 1270 168 104 Well-AH-D 05/15/07 142 142 86 Well-AH-D 06/18/07 343 141 89 Well-AH-D 07/13/07 221 149 92 Well-AH-D 08/15/07 1,089 148 104 Well-AH-D 09/19/07 376 145 92 Well-AH-D 10/03/07 1,311 151 109 Well-AH-D 11/19/07 920 177 119 Well-AH-D 12/12/07 973 138 97 Well-AH-D 01/23/08 1,104 152 106 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
T Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 54 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium I Major Cations and Anions Identification Date Note IResult (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L) I Well-AH-D 02/07/08 1,209 150 107 Well-AH-D 03/12/08 1,524 146 109 Well-AH-D 04/01/08 1,799 148 113 Well-AH-D 05/29/08 1,675 136 105 Well-AH-D 06/20/08 1,265 136 99 WelI-AH-D 07/07/08 1,010 139 98 Well-AH-D 08/18/08 729 131 89 Well-AH-D 09/22/08 751 141 95 Well-AH-D 10/17/08 741 137 93 Well-AH-D 11/18/08 809 132 91 Well-AH-D 12/16/08 489 133 87 Well-AH-S 02/23/04 899 143 99 0.14 135 Well-AH-S 03/08/04 894 142 98 -- --
Well-AH-S 03/29/04 878 141 97 0.27 56 Well-AH-S 04/20/04 932 141 98 0.25 67 Well-AH-S 05/03/04 908 141 98 -- --
Well-AH-S 06/03/04 759 149 100 -- --
Well-AH-S 06/16/04 835 142 97 0.263 48 Well-AH-S 07/19/04 816 151 103 0.204 38 Well-AH-S 08/23/04 752 155 105. -- --
Well-AH-S 09/13/04 512 144 94 ....
Well-AH-S 09/29/04 533 149 97 ....
Well-AH-S 10/18/04 420 159 101 ....
Well-AH-S 11/15/04 1 '3,910 3,910 1,235 ....
Well-AH-S 12/20/04 1 '3,910 3,910 1,130 --..
Well-AH-S 01/11/05 658 163 107 0.446 61 Well-AH-S 02/15/05 633 146 97 -- --
Well-AH-S 03/08/05 614 147 97 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above'the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 55 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected-between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well-AH-S 04/18/05 319 146 92 0.138 216 Well-AH-S 05/16/05 249 150 93 277 Well-AH-S 06/07/05 238 147 91 151 Well-AH-S 07/11/05 293 144 91 Well-AH-S 08/02/05 241 147 92 Well-AH-S 09/07/05 162 149 91 Well-AH-S 10/17/05 -153 153 92 Well-AH-S 11/02/05 298 151 94 Well-AH-S 12/09/05 218 148 91 Well-AH-S 01/10/06 251 153 95 Well-AH-S 02/06/06 213 170 105 Well-AH-S 03/06/06 -158 158 94 Well-AH-S 04/10/06 -155 155 92 Well-AH-S 05/01/06 163 151 92 Well-AH-S 06/05/06 190 156 96 Well-AH-S 07/17/06 -171 171 104 Well-AH-S 08/08/06 178 160 98 Well-AH-S 09/06/06 211 157 97 Well-AH-S 10/06/06 238 159 99 Well-AH-S 11/02/06 366 154 97 Well-AH-S 12/19/06 252 163 101 Well-AH-S 01/22/07 384 155 98 Well-AH-S 02/20/07 242 151 93 Well-AH-S 03/14/07 248 149 93 Well-AH-S 04/19/07 '162 162 98 Well-AH-S 05/15/07 154 137 84 Well-AH-S 06/18/07 236 142 88 Well-AH-S 07/13/07 1,193 147 105 Well-AH-S 08/15/07 -145 145 88 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
()oo Constituent was detected above its New Jersey Groundwater Quality Criteria.
NNot Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 5 6 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ITritium Major Cations and Anions Identification Date Note lResult (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well-AH-S 09/19/07 -144 144 88 ....
Well-AH-S 10/03/07 195 164 101 ....
Well-AH-S 11/19/07 2,790 190 152 ....
Well-AH-S 12/12/07 5,579 142 150 ....
Well-AH-S 01/23/08 1,322 152 109 ....
Well-AH-S 02/07/08 1,365 139 103 ....
Well-AH-S 03/12/08 1,377 145 107 ....
Well-AH-S 04/01/08 400 142 91 ....
Well-AlH-S 05/29/08 274 148 92 ....
Well-AH-S 06/20/08 546 136 89 ....
Well-AH-S 07/07/08 434 138 89 ....
Well-AH-S 08/18/08 488 132 87 ....
Well-AH-S 09/22/08 620 128 86 ....
Well-AH-S 10/17/08 738 133 91 ....
Well-AH-S 11/18/08 1,345 131 98 ....
Well-AH-S 12/16/08 858 139 96 ....
Well-AI 02/02/04 1 -5,780 5,780 NA ....
Well-Al 02/26/04 4,360 140 138 0.05 8 Well-AI 03/11/04 4,370 145 141 -- --
Well-AI 03/30/04 3,550 143 131 -- --
Well-Al 05/04/04 11,800 140 200 0.17 16 Well-Al 05/11/04 1 10.8M) 5,392 3,466 -- --
Well-Al 05/19/04 1 ~44,100 5,780 3,439 <3.3 47 Well-Al 06/03/04 1 4ý40 4,563 3,360 -- --
Well-Al 07/19/04 1 3,0 2,870 2,550 Well-Al 07/28/04 1 203,79 2,650 Well-Al 08/02/04 1 31,00i 3,320 2,670 ..--
Well-Al 08/09/04 1 3,00 4,850 3,030 -- 28 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit, (IOoui)Constituent was detected above its New Jersey Groundwater Quality Criteria.
NANot Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 57 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well-Al 08/16/04 3,320 3,000 Well-Al 08/25/04 3,030 3,050 13,120 Well-A! 12/27/04 153 222 13,120 Well-A! 04/19/05 153 222 Well-AI 05/10/05 3,620 2,640 Well-Al 06/21/05 3,750 2,820 Well-Al 07/12/05 14,060 155 226 Well-Al 08/15/05 7,683 147 172 Well-Al 09/06/05 6,669 150 166 Well-Al 10/10/05 5,081 148 151 Well-Al 11/14/05 4,535 152 148 Well-Al 12/20/05 3,602 156 139 Well-AI 01/17/06 2,755 150 127 Well-AI 02/21/06 2,730 149 126 Well-Al 03/20/06 4,200 3,730 1,530 Well-Al 04/10/06 ,4,720 4,720 NA Well-Al 04/11/06 5,194 157 156 Well-Al 05/16/06 2,354 149 122 Well-Al 06/19/06 2,082 162 126 Well-Al 07/18/06 1,572 150 112 Well-Al 07/19/06 ,4,890 4,890 NA Well-Al 08/08/06 1,621 160 118 Well-Al. 09/18/06 1,782 157 119 Well-Al 10/10/06 2,110 159 124 Well-AL 11/01/06 1,543 157 116 Well-AL 12/18/06 2,495 178. 142 Well-Al 12/19/06 ,4,840 4,840 NA Well-AI 01/13/07 2,784 149 127 Well-Al 02/06/07 2,393 157 127 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
'Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 58 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium FMajor Cations and Anions Identification Date Note Result (pCifL) I LLD Deviation Boron(mg/L) Sodium(mgJL)
Well-Al 03/08/07 2,100 149 119 ....
Well-Al 04/20/07 2,677 161 134 ....
Well-AI 05/15/07 2,556 140 119 ....
Well-Al 06/18/07 21867 142 123 ....
Well-Al 07/18/07 2,784 145 123 ....
Well-AI 08/15/07 3,204 143 128 ....
Well-Al 09/20/07 3,137 150 131 ....
Well-Al 10/03/07 3,360 149 132 ....
Well-Al 11/14/07 3,173 154 138 ....
Well-Al 12/12/07 2,902 138. 121 ....
Well-Al 01/17/08 2,933 151 128 ....
Well-Al 02/06/08 2,920 138 122 ....
Well-Al 03/18/08 3,035 149 129 ....
Well-Al 04/02/08 3,255 151 132 ....
Well-Al 05/08/08 3,339 146 129 ....
Well-Al 06/19/08 2,708 136 117 ....
Well-AI 07/07/08 2,934 128 116 ....
Well-AI 08/06/08 2,005 140 111 ....
Well-Al 09/02/08 2,478 136 114 ....
Well-Al 11/19/08 3,732 133 127 ....
Well-Al 12/15/08 5,220 151 152 ....
Well-AJ 02/25/04 1,150 142 102 0.62 616 Well-AJ 03/09/04 1,040 140 99 0.68 650 Well-AJ 03/30/04 1,080 146 103 0.62 642 Well-AJ 04/19/04 1,190 139 101 0.67 621 Well-AJ 05/10/04 1,240 142 103 -- --
Well-AJ 05/24/04 1,270 158 113 Well-AJ 06/16/04 1,495 148 111 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
,oo Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 59 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well-AJ 07/13/04 2,193 142 116 Well-AJ 07/20/04 1,525 152 113 WelI-Aj' 08/16/04 1,677 141 110 Well-AJ 09/08/04 4,254 152 146 Well-AJ 10/18/04 3,230 3,560 Well-AJ 11/16/04 3,910 6,440 Well-AJ 12/28/04 2,820 5,450 Well-Al 01/12/05 3,910 8,540 Well-AJ 02/14/05 3,910 8,260 Well-AJ 03/02/05 3,670 6,710 Well-AJ 03/07/05 3,490 5,670 Well-AJ 03/14/05 4,320 6,120 Well-AJ 03/23/05 3,790 3,720 193MOO~
Well-AJ 03/28/05 6,280 5,880 Well-AJ 04/18/05 4,420 5,490 Well-AJ 05/18/05 144AQ000 3,490 4,900 Well-AJ 08/15/05 36M0 3,905 3,877 Well-AJ 10/17/05 3,790 6,330 Well-Al .11/15/05 0003.' 3,430 3,770 Well-AJ 12/12/05 4,370 5,750 Well-AJ 01/24/06 4,6401 3,550 3,520 Well-Al 02/23/06 3,920 3,280 Well-AJ 03/21/06 3,730 4,120 Well-AJ 04/17/06 5,510 4,030 Well-AJ 05/15/06 5,000 3,780 Well-Al 07/24/06 5,470 3,500 Well-AJ 08/22/06 2,520 1,340 Well-AJ 06/19/07 150 329 Well-AJ 08/28/08 140 139 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
1,0 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 60 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well-AL 02/25/04 -141 141 83 0.21 60 Well-AL 03/09/04 '147 147 86 0.20 55 Well-AL 03/30/04 -146 146 86 0.22 63 Well-AL 04/19/04 ,141 141 85 0.3 62 Well-AL 05/19/04 -151 151 89 Well-AL 06/16/04 -141 141 85 Well-AL 07/13/04 '141 141 85.
Well-AL 07/28/04 '147 147 88 Well-AL 08/16/04 -150 150 91 Well-AL 09/08/04 '153 153 91 Well-AL 10/12/04 -146 146 85 Well-AL 11/16/04 1 -3,910 3,910 1,126 1
Well-AL 12/21/04 '3,910 3,910 1,130 Well-AL 01/11/05 '157 157 92 Well-AL 02/08/05 '157 157 92 0.23 74 Well-AL 03/14/05 ' 146 146 87 Well-AL 04/11/05 -158 158 93 Well-AL 05/09/05 -150 150 88 Well-AL 07/11/05 -154 154 90 Well-AL 10/10/05 -148 148 89 Well-AL 01/23/06 '153 153 91 Well-AL 04/10/06 '165 165 99 Well-AL 07/17/06 -154 154 92 Well-AL 10/09/06 '162 162 97 Well-AL 01/13/07 '153 153 91 Well-AL 04/19/07 243 158 98 Well-AL 07/19/07 203 146 90 Well-AL 10/09/07 '175 175 103 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Uji Constituent was detected above its New Jersey Groundwater Quality Criteria.
KNAN ot Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 61 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note IResult (pCi/L) I LLD Deviation Boron(mg/L) Sodium(mg/L)
Well-AL 01/23/08 366 151 96 ....
Well-AL 04/22/08 375 154 98 ....
Well-AL 07/16/08 426 142 91 ....
Well-AL 10/20/08 396 139 *89 ....
Well-AM 02/02/04 1 425.000 NA NA -- --
Well-AM 02/26/04 1 1 NNA-110 NA NA ....
Well-AM 02/26/04 1 NA.NA NA NA Well-AM 03/11/04 1 2 NA NA Well-AM 03/11/04 1 234. 00NA NA N Well-AM 04/08/04 1 1960 5,822 6,425 ....
Well-AM 04/08/04 1 196.00 5,822 6,425 ....
Well-AM 05/06/04 1 1500 5,589 5,807 ....
Well-AM 05/06/04 1 fI 0.000 5,589 5,807 Well-AM 05/20/04 1 1 1 4,563 5,651 <3.3 6 Well-AM 06/10/04 1 L. 4,974 5,832 <3.33 5 Well-AM 07/20/04 1 280003/4 2,870 5,020 ....
Well-AM 08/17/04 1 37.t0 3,320 5,270 ....
Well-AM 09/14/04 1 1. 4,560 5,380 -- 6 Well-AM 10/25/04 1 124,00 3,030 5,080 --
Well-AM 11/23/04 1 i(1000 1 4,220 4,940 ....
Well-AM 12/27/04 1 103. 4,060 4,590 ....
Well-AM 01/12/05 1 1S08010 3,910 4,660 Well-AM 02/22/05 1 * - 3,550 4,340 ....
Well-AM 03/15/05 1 ___ 4,320 4,100 ....
Well-AM 04/19/05 1 54,200 4,420 3,570 ....
Well-AM 05/17/05 1 58,400 3,490 3,480 -- --
Well-AM 06/21/05 1 53800 1; 3,750 3,420 Well-AM 07/11/05 1 43200 3,750 3,110 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
SConstituent was detected above its New Jersey Groundwater Quality Criteria.
- Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 62 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well-AM 08/15/05 3,905 2,979 Well-AM 09/20/05 4,563 4,478 Well-AM 10/10/05 3,790 2,930 Well-AM 11/14/05 3,430 3,210 Well-AM 12/20/05 3,430 2,580 Well-AM 01/23/06 3,550 2,750 Well-AM 02/23/06 3,920 4,200 Well-AM 03/21/06 3,730 10,100 Well-AM 04/11/06 4,720 13,700 Well-AM 05/16/06 5,000 15,100 Well-AM 06/20/06 187,003 4,890 12,100 Well-AM 07/17/06 4,670 5,130 18,2191 Well-AM 07/21/06 NA NA 129,500 Well-AM 08/08/06 NA NA Well-AM 08/21/06 2,520 3,590 Well-AM 09/07/06 151 241 Well-AM 09/13/06 7~~f~ NA NA Well-AM 09/19/06 161 257 Well-AM 10/09/06 156 261 Well-AM 11/01/06 162 275 Well-AM 11/15/06 162 290 Well-AM 12/07/06 153 330 Well-AM 12/18/06 148 352 Well-AM 01/13/07 148 266 Well-AM 01/22/07 155 294 Well-AM 02/06/07 162 311 Well-AM 02/23/07 157 407 Well-AM 03/08/07 149 266 Well-AM 04/20/07 160 275 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
j),oo1 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 63 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) ILLD I Deviation Boron(mg/L) Sodium(mg/L)
Well-AM 05/15/07 174 363 Well-AM 06/19/07 3,430 3,730 Well-AM 07/18/07 146 335 Well-AM 07/30/07 139 321 Well-AM 08/15/07 148 342 Well-AM 09/21/07 3,830 7,330 Well-AM 09/25/07 3,730 7,950 Well-AM 10/03/07 3,830 7,550 Well-AM 10/17/07 4,370 5,690 Well-AM 11/14/07 4,110 5,210 Well-AM 11/28/07 3,630 5,330 Well-AM 12/12/07 150 272 19,329 Well-AM 12/27/07 149 250 18,293 Well-AM 01/17/08 140 239 19,454 Well-AM 01/28/08 140 246 Well-AM 02/06/08 19,910 140 250 19,927 Well-AM 02/20/08 149 255 Well-AM 03/13/08 17,686 146 241 Well-AM 03/18/08 146 265 Well-AM 04/02/08 155 287 Well-AM 04/23/08 22 ý0 91 146 282 Well-AM 05/08/08 147 270 Well-AM 06/24/08 135 256 Well-AM 06/30/08 '5ý'2 136 262 Well-AM 07/07/08 141 281 Well-AM 07/24/08 140 253 Well-AM 08/07/08 140 254 Well-AM 08/21/08 128 290 Well-AM 09/02/08 132 316 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 64 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Aniuns Identification Date INote lResult (pCi/L), LLD -1Deviation Boron(mg/L) ISodium(mgL Well-AN 08/10/04 21143 263 0.685 32 Well-AN 08/24/04 19,632 155 263 Well-AN 09/14/04 9;150 141 182 0.567 23 Well-AN 10/25/04 8,950 147 185 Well-AN 11/23/04 6,245 144 158 Well-AN 12/29/04 1 '4,020 4,020 1,210 Well-AN 01/12/05 6,180 159 169 Well-AN 03/02/05 1 1 0 3,670 6,300 Well-AN 03/07/05 1 1.001 3,490 5,940 Well-AN 03/14/05 1 1c0 4,320 5,700 Well-AN 03/23/05 1 12100 3,790 6,030 Well-AN 03/28/05 1 09.900 6,280 4,900 Well-AN 04/18/05 1 144,0 4,420 5,650 Well-AN 05/18/05 1 1. 3,490 4,920 Well-AN 06/22/05 1 90 3,750 4,470 Well-AN 07/19/05 148 479 Well-AN 08/15/05 1 69000 3,905 3,879 Well-AN 10/17/05 1 7m'Im 3,790 4,150 Well-AN 11/15/05 1 160 i 3,430 4,860 Well-AN 12/12/05 1 7 4,370 4,260 Well-AN 01/24/06 1 99
- l;ti 3,550 4,800 Well-AN 02/22/06 -8.129 149 485 Well-AN 02/23/06 1 W*60 3,920 4,030 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
_ Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 65 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Io Major Cations and Anions Identification Date INote lResult (pCiIL) ILLD IDeviation IBoron(mg[L) ISodium(mg/L)
Well-AN 03/21/06 1 8204 3,730 4,630 Well-AN 04/17/06 1 :54.500 5,510 4,070 Well-AN 05/15/06 1 8,0 iW 5,000 4,870 Well-AN 06/20/06 1 74 4,890 4,730 Well-AN 07/24/06 1 .8 5,470 3,930 Well-AN 08/22/06 1 W06,00 2,520 2,320 Well-AN 09/21/06 1 '82400 7,550 4,720 Well-AN 10/06/06 3,169 161 138 Well-AN 11/16/06 1 8 3,630 4,680 Well-AN 12/15/06 2. 158 286 Well-AN 01/23/07 5,973 154 164 Well-AN 02/06/07 .6 181 404 Well-AN 08/23/07
- 143 289 Well-AN 09/20/07 7 1).7()S 151 492 Well-AN 10/17/07 41.105 158 381 Well-AN 11/15/07 1 54,400 4,110 3,930 Well-AN 12/13/07 1 70 4,030 4,300 Well-AN 03/12/08 1 60500 3,980 3,950 Well-AN 04/23/08 1 73700 5,060 4,590 Well-AN 05/09/08 4,827 140 141 Well-AN 06/12/08 4L94 i 136 338 Well-AN 07/16/08 ;4.45* 144 400 Well-AN 08/21/08 1 5 4,530 3,600 Well-AN 09/22/08 7 (Is 148 278 Well-AO 07/29/04 6,739 146 163 Well-AO 08/10/04 2,399 153 125 0.24 27 Well-AO 08/16/04 5,420 146 155 Well-AO 08/24/04 2,225 155 125 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was. detected above the laboratory method detection limit.
,ooo Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 66 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium I Major Cations and Anions Identification Date INoeI~sl (pCi/L) I LLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-AO 09/14/04 2,417 149 123 Well-AO 09/29/04 2,794 152 130 Well-AO 10/25/04 2,706 158 132 Well-AO 11/23/04 2,570 147 123 Well-AO 12/27/04 1 -4,060 4,060 1,370 Well-AO 01/12/05 1,780 166 125 Well-AO 03/02/05 1 15,900 3,670 2,100 Well-AO 03/07/05 1 IS.000 1 3,490 5,710 Well-AO 03/14/05 1 138MOO 4,320 5,430 Well-Ao 03/23/05 1 192,01 3,790 6,570 Well-AO 03/28/05 6,395 147 162 Well-AO 11/15/05 1 34700 3,430 2,900 Well-AO 12/12/05 1 0 4,370 3,750 Well-AO 07/24/06 1 ý;8AOO 5,470 3,410 Well-AO 08/22/06 1 M 2,520 2,290 Well-AO 10/06/06 4,190 160 148 Well-AO 11/16/06 14,7 04 164 301 Well-AO 12/15/06 7,629 168 190 Well-AO 01/23/07 5,136 154 154 Well-AP 07/19/04 2,078 148 118 0.06 59 Well-AP 08/09/04 1,455 150 112 0.126 105 Well-AP 08/23/04 1,006 151 106 -- --
Well-AP 09/08/04 1,039 148 105 ....
Well-AP 09/22/04 1,679 156 119 ....
Well-AP 10/11/04 777 151 102 ....
Well-AP 11/22/04 1,531 150 112 0.204 65 Well-AP 12/14/04 1 -3,230 3,230 984 -- --
Well-AP 01/27/05 1,200 138 102 0.16 134 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Ljjij0lj Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 67 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) I Sodium(rgIL)
Well-AP 02/01/05 2,680 153 128 Well-AP 03/07/05 3,490 3,970 Well-AP 04/05/05 4,220 4,730 Well-AP 05/02/05 3,320 1,690 Well-AP 06/06/05 3,460 4,630 Well-AP 06/21/05 3,750 3,220 1,968 Well-AP 07/06/05 144 114 Well-AP 07/19/05 4,563 148 145 Well-AP 08/01/05 6,190 3,320 3,640 Well-AP 08/16/05 3,905 2,564 Well-AP 08/29/05 961 151 105 Well-AP 09/06/05 1,196 150 107 Well-AP 09/19/05 10,097 152 195 Well-AP 10/03/05 4,220 3,530 Well-AP 10/18/05 12,250 156 212 Well-AP 11/01/05 798 149 101 Well-AP 12/08/05 3,730 2,750 Well-AP 01/10/06 14,354 152 225 Well-AP 02/07/06 9,723 152 191 Well-AP 02/21/06 14,580 152 226 Well-AP 03/06/06 9,829 161 199 Well-AP 03/20/06 8,860 3,730 1,850 Well-AP 04/03/06 9,490 155 192 Well-AP 04/17/06 8,284 158 184 Well-AP 05/01/06 8,316 154 184 Well-AP 05/15/06 7,686 158 180 Well-AP 06/05/06 5,639 167 167 Well-AP 06/20/06 5,681 150 158 Well-AP 07/10/06 757 157 105 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 68 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note lResult (pCiIL) ILLD Deviation Boron(mg/L) ISodiummgL Well-AP 07/24/06 465 152 98 Well-AP 08/07/06 2,006 159 123 Well-AP 08/21/06 4,405 153 147 Well-AP 09/06/06 2,560 157 128 Well-AP 10/10/06 5,939 161 166 Well-AP 11/01/06 779 153 103 Well-AP 12/08/06 5,412 186 179 Well-AP 01/13/07 1,086 156 109 Well-AP 02/05/07 4,348 151 145 Well-AP 03/07/07 1,169 151 109 Well-AP 04/19/07 1,059 158 111 Well-AP 05/15/07 781 186 123 Well-AP 06/18/07 1,093 145 102 Well-AP 07/18/07 1,049 144 101 Well-AP 08/15/07 2,730 144 122 Well-AP 09/19/07 3,830 161 144 Well-AP 10/03/07 3,442 150 133 Well-AP 11/14/07 4,025 124 128 Well-AP 12/12/07 3,806 137 130 Well-AP 01/17/08 1,282 154 110 Well-AP 02/21/08 1,225 149 106 Well-AP 03/12/08 1,123 138 99 Well-AP 04/01/08 1,224 147 105 Well-AP 05/08/08 1,130 136 98 Well-AP 06/19/08 1,143 143 102 Well-AP 07/07/08 831 128 89 Well-AP 08/07/08 1,070 133 95 Well-AP 09/02/08 936 133 93 Well-AP 10/17/08 947 146 101 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
0 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 69 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well-AP 12/15/08 1,113 144 102 Well-AQ 07/08/04 1 '3,260 3,260 1,094 -- --
WeIl-AQ 07/19/04 217 142 88 0.436 308 Well-AQ 08/09/04 309 152 95 0.57 1,090 WelI-AQ 08/23/04 243 147 92 -- --
WelI-AQ 09/08/04 273 150 94 ....
Well-AQ 09/22/04 213 138 86 ....
WeU-AQ 10/26/04 201 144 89 ....
WelI-AQ 11/16/04 218 147 91 ....
WeI1-AQ 12/21/04 1 '4,280 4,280 1,300 ....
Well-AQ 01/27/05 225 135 84 -- --
Well-AQ 02/02/05 '148 148 90 0.448 1,100 Well-AQ 03/14/05 367 145 92 -- --
Well-AQ 04/12/05 247 143 89 ....
Well-AQ 05/09/05 248 151 94 ....
Well-AR 07/14/04 1 <2'.OO 3,620 7,980 Well-AR 07/19/04 1 1911000 2,870 8,700 Well-AR 08/09/04 1 t, 4,850 9,620 6.00 75 Well-JAR 08/23/04 1 3,670 10,000 -- --
Well-AR 09/13/04 1 ;55 000i 4,560 10,500 7.10 65 Well-AR 09/30/04 1 2(00 5,780 10,800 -- --
Well-AR 10/26/04 1 ýKQ.0001 3,030 11,000 Well-AR 12/28/04 1 423,01 4,060 9,050 Well-AR 01/27/05 1 330.0 2,470 8,140 Well-AR 02/22(05 1 334JMO 3,550 8,220 Well-AR 03/14/05 1 -204,1104,320 6,510 ....
Well-AR 04/12/05 1 '33.000 4,220 7,010 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
o Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 70 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium Ia Major CationsadAiuns Identification Date INote lResult (pCiIL) ILLD IDeviation IBoron(mgIL) ISodium(mgfL)I Well-AR 05/10/05 3,620 6,420 Well-AR 06/21/05 3,750 6,670
~215O4,00 Well-AR 07/19/05 2,820 6,310 Well-AR 08/16/05 3,905 6,592 Well-AR 09/19/05 4,563 6,272 Well-AR 10/10/05 3,790 5,540 Well-AR 11/02/05 3,030 6,560 Well-AR 12/08/05 3,730 6,090 Well-AR 01/10/06 4,370 6,250 Well-AR 02/06/06 3,090 4,810 16,5720 Well-AR 03/20/06 3,730 3,510 Well-AR 04/10/06 155 240 Well-AR 05/15/06 12,555 156 215 Well-AR 06/06/06 12,751 162 221 Well-AR '07/17/06 4,670 5,000 Well-AR 08/08/06 4,440 4,330 Well-AR 09/06/06 157 273 Well-AR 10/10/06 12,619 158 216 Well-AR 11/02/06 169 506 Well-AR 12/18/06 f,61.49 155 447 Well-AR 12/19/06 4,840 4,060 Well-AR 01/13/07 3,730 4,700 Well-AR 02/05/07 4,370 4,350 62ý900 Well-AR 03/07/07 3,630- 4,110 Well-AR 06/18/07 3,430 4,620 Well-AR 07/19/07 4,370 4,780 62,100O Well-AR 0.7/23/07 1,840 2,180 Well-AR 08/08/07 4,110 .4,390 Well-AR 08/15/07 3,830 4,760 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry,
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 71 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Identification Sample Date Note Result (pCi/L) Tritium LLD Deviation Major CationsSodinm(mg/L)
Boron(mg/L) and An-ons Well-AR 09/19/07 1 5 0 3,830 3,760 ....
Well-AR 09/25/07 1 (0.400 3,730 4,170 Well-AR 10/03/07 02 157 267 Well-AR 10/17/07 12,266 137 200 ....
Well-AR 11/14/07 1 5 4,110 3,940 ....
Well-AR 11/28/07 ý5ti 123 374 Well-AR 12/12/07 47,105* 146 373 Well-AR 12/27/07 43,084 149 360 ....
Well-AR 01/23/08 37 140 334 Well-AR 02/21/08 139 313 ....
Well-AR 03/12/08 13 147 323 ...
Well-AR 04/01/08 11,929 152 297 Well-AR 05/08/08 21.014 146 272 Well-AR 06/19/08 16,288 135 220 ....
Well-AR 07/07/08 15,470 139 220 ....
Well-AR 08/18/08 2_L857Y< 129 256 Well-AR 09/04/08 280 134 266 Well-AR 09/22/08 11,194 147 196 ....
Well-AR 10/13/08 11,555 135 194 ....
Well-AR 10/27/08 12,787 135 202 -' --
Well-AR 11/18/08 10,362 137 186 ....
Well-AR 11/25/08 8,539 132 168 ....
Well-AR 12/15/08 8,935 148 181 ....
Well-AR 12/23/08 8,735 145 178 ....
Well-AS 07/08/04 1 37,00 20 2,460 Well-AS 07/19/04 1 27.,...
- 32,0 2,920460 Well-AS 08/09/04 1 7,510 4,850 1,920 ....
Well-AS 08/23/04 1 41,30 3,030 2,990 --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
04/03/2009 10:37 AM Page 72 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Iot Tritium I Major Cations and Anions Identifiaio Date INote MResu t (pCiIL) I LLD IDeviation I Boron(mg/L) I Sodium(mg/L)
Well-AS 09/13/04 145 259 0.727 199 Well-AS 09/29/04 18,171 146 248 Well-AS 10/11/04 9,899 156 200 Well-AS 11/16/04 14,400 3,910 2,090 Well-AS 12/21/04 15,200 3,910 2,070 Well-AS 01/27/05 14,000 143 224 0.459 186 Well-AS 03/02/05 3,670 2,430 Well-AS 03/07/05 3,490 3,020 Well-AS 03/14/05 1 12,600 4,320 2,080 Well-AS 03/23/05 1 3,790 4,050 Well-AS 03/28/05 1 6,280 4,180 Well-AS 04/18/05 4,420 4,140 Well-AS 05/18/05 3,490 3,520 Well-AS 06/22/05' 3,750 3,730 Well-AS 07/19/05 1 2,820 3,530 Well-AS 08/15/05 1 3,905 3,334 Well-AS 10/17/05 3,790 3,010 Well-AS 11/15/05 66,500 3,430 3,910 Well-AS 12/12/05 4,370 3,870 Well-AS 01/24/06 3,550 4,150 Well-AS 02/23/06 3,920 4,190 Well-AS 03/21/06 3,730 3,640 Well-AS 04/17/06 5,510 3,820 Well-AS 05/15/06 5,000 3,850 Well-AS 06/20/06 4,890 3,970 Well-AS 07/24/06 5,470 3,640 Well-AS 08/22/06 2,520 1,850 Well-AS 09/21/06 7,550 4,350 Well-AS 10/06/06 6,270 4,260 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F'Constituent was detected above its New Jersey Groundwater Quality Criteria.
-Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 73 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD [Deviation Boron(mg/L) Sodium(mg/L)
Well-AS 11/16/06 101,284 163 584 ....
Well-AS 12/15/06 C4S104 151 394 ....
Well-AS 01/23/07 48 , 158 403 Well-AS 02/06/07 '2ýz5h 162 334 ....
Well-AS 03/14/07 41,00 165 383 ....
Well-AS 06/19/07 21.799 147 298 ....
Well-AS 07/19/07 4,925 146 146 ....
Well-AS 08/23/07 14,497 141 218 ....
Well-AS 09/20/07 13,072 149 214 ....
Well-AS 10/17/07 8,922 168 204 ....
Well-AS 11/15/07 15,870 124 220 ....
Well-AS 12/13/07 F 7 7,876 150 296 Well-AS 01/24/08 *3(4;3 141 326. -- --
Well-AS 02/25/08 27.44ý; 149 294 ....
Well-AS 03/12/08 , 148 286 ....
Well-AS 04/23/08 15,043 160 233 ....
Well-AS 05/09/08 2,435 137 115 ....
Well-AS 07/16/08 1 5 4,780 3,800 ....
Well-AS 08/28/08 6,876 128 154 ....
Well-AS 09/22/08 145 288 ..
Well-AT 07/02/04 1 311,6 0 3,490 2,650 --
Well-AT 07/08/04 4,288 .142 139 0.275 309 Well-AT 07/12/04 1 '3 2.7 0 3,620 2,750 ....
Well-AT 07/22/04 1 21,600 2,870 2,200 ....
Well-AT, 08/03/04 1 28,700 3,320 2,580 ....
Well-AT 08/11/04 1 23300 3,030 2,320 ....
Well-AT 08/12/04 1 1),0 0 3,030 2,620 ....
Well-AT 08/13/04 1 20,70 3,030 2,220 --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20,Ooo1 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 74 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I Tritium DT i Major CationadAion Identification IDate INote IResult (pCiIL) ILLD Deviation IBoron(mg/L) ISodium(mg/L)I Well-AT 08/21/04 3,030 2,460 Well-AT 08/31/04 17,124 157 250 Well-AT 12/28/04 -4,060 4,060 1,260 Well-AT 01/19/05 1,991 159 124 0.286 163 Well-AT 03/02/05 3,670 3,030 1
Well-AT 03/07/05 3,490 2,330 Well-AT 03/14/05 4,320 3,660 Well-AT 03/23/05 10,039 150 '195 Well-AT 03/28/05 7,973 148 176 Well-AT 04/18/05 4,974 151 153 0.267 396 Well-AT 05/18/05 3,451 151 136 Well-AT 06/22/05 1,777, 145 112 Well-AT 07/19/05 1,687 146 112 Well-AT 08/15/05 1,578 150 112 Well-AT 10/17/05 2,224 157 124 Well-AT 11/15/05 1,451 151 112 Well-AT 12/12/05 1,722 153 116 Well-AT 01/24/06 2,139 153 121 Well-AT 02/22/06 2,375 152 123 Well-AT 02/23/06 1 '3,920 3,920 NA 1
Well-AT 03/21/06 -3,730 3,730 NA Well-AT 04/17/06 1,396 159 115 Well-AT 05/15/06 1,517 156 115 Well-AT 06/20/06 1,911 151 117 Well-AT 07/24/06 2,110 151 120 Well-AT 08/22/06 3,715 152 139 Well-AT 09/21/06 4,002 158 145 Well-AT 10/06/06 4,785 159 154 Well-AT 11/16/06 6,235 170 178 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
<. Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 75 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
Well-AT 12/15/06 2,458 166 134 ....
Well-AT 01/23/07 2,103 146 118 ...
Well-AT 02/06/07 1,401 149 110 ....
Well-AT 03/14/07 2,359 197 152 ....
Well-AT 04/24/07 4,046 160 149 ....
Well-AT 05/22/07 3,482 151 135 Well-AT 06/19/07 1,892 143 112 ....
Well-AT 07/19/07 2,158 145 116 ....
Well-AT 08/22/07 1 '4,280 4,280 NA ....
Well-AT 08/23/07 2,182 148 118 ....
Well-AT 09/20/07 2,114 148 118 ....
Well-AT 10/17/07 1,705 149 112 ....
Well-AT 11/15/07 2,221 176 136 ....
Well-AT 12/13/07 4,326 140 137 -- --
Well-AT 03/12/08 1 <) 4,890 3,700 -
Well-AT 04/23/08 1 00 5,060 4,490 --...
Well-AT 05/09/08 14,174 136 210 ....
Well-AT 08/28/08 707 139 94 ....
Well-AT 12/18/08 3,250 132 121 ....
Well-AV 07/20/05 3,060 NA NA --
Well-AY 07/20/05 3,000 NA NA -- --
Well-AZ 07/20/05 8,710 NA NA -- --
Well-BA 10/16/06 <157 157 94 --
Well-BA 04/10/07 <126 126 75 ....
Well-BA 05/07/07 172 172 105 ....
Well-BA 10/17/07 -150 150 89 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
L Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 76 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(ag/L)
Well-BA 04/17/08 '147 147 88...
Well-BA 10/20/08 -133 133 78 ....
Well-BB 10/16/06 289 162 101 ....
Well-BB 12/08/06 338 165 104 ....
Well-BB 04/10/07 -161 161 97 ....
Well-BB 10/17/07 '149 149 89 ....
Well-BB 04/17/08 168 143 88 ....
Well-BB 10/20/08 -134 134 81 ....
Well-BC 110/16/06 1 163 163 98 1 --
Well-BC 04/10/07 '162 162 94 ....
Well-BC 10/17/07 '150 150 89 ....
Well-BC 04/17/08 '144 144 86 ....
Well-BD 10/16/06 325 ,157 99 ....
Well-BD 04/10/07 256 152 95 ....
Well-BD 10/10/07 264 156 97 ....
Well-BD 04/22/08 323 148 93 ....
Well-BD 10/20/08 264 133 83 ....
Well-BE 10/16/06 '159 159 95 ....
Well-BE 04/10/07 '168 168 98 ....
Well-BE 10/10/07 -158 158 93 ....
Well-BE 04/17/08 '152 152 90 ....
jWell-BE 10/21/08 659 134 90 ....
Well-BF, 10/16/06 '155 155 91 ....
Well-BF 04/11/07 -164 164 94 ....
Well-BF 10/17/07 '189 189 109 ....
Well-BF 04/17/08 -152 152 91 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
'P Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 77 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L) Sodium(mg/L)
F 1Wel0 10/21/081 I-136 j 136 8800- --
Well-BG 10/17/06 '162 162 97 -- ) --
Well-BG 04/11/07 '152 152 92 ....
Well-BG 11/01/07 '165 165 94 ....
Well-BG 04/22/08 322 152 95 ....
Well-BG 10/21/08 '137 137 82 ....
Well-BU 04/24/07 -181 181 106 -
Well-BU 10/18/07 " 153 153 90 ....
Well-BU 04/16/08 '157 157 94 ....
Well-BU 10/27/08 - 149 149 88 ....
Well-BW 02/24/07 2,556 162 132 ....
Well-BW 03/27/07 3,728 164 149 ....
Well-BW 04/20/07 3,054 159 138 ....
Well-BW 05/22/07 1,517 168 122 ....
WelI-BW 06/25/07 1 3,730 3,730 NA ....
Well-BW 07/12/07 1,593 146 110 ....
Well-BW 08/22/07 1,719 149 113 ....
Well-BW 09/21/07 1,917 149 115 ....
Well-BW 10/09/07 2,056 150 117 ....
Well-BW 11/20/07 1,729 179 132 ....
Well-BW 12/19/07 1,641 147 111 ....
Well-BW 01/16/08 1,638 141 107 ....
Well-BW 02/25/08 1,347 142 104 ....
Well-BW 03/13/08 1,201 138 100 ....
Well-BW. 04/02/08 1,657 151 113 ....
Well-BW 05/28/08 762 136 93 ....
Well-BW 06/19/08 1,299 135 99 --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
i Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 7 8 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L) Sodium(mg/L)
Well-BW 07108/08 1,569 129 100 ....
Well-BW 08/18/08 1,549 131 -101 ....
Well-BW 09/22/08 1,915 128 104 ....
Well-BW 10/18/08 1,748 135 106 ....
Well-BW 11/21/08 1,347 144 105 ....
Well-BW 12/04/08 1,803 146 113 ....
Well-BX 02/24/07 1,958 155 120 -- --
Well-BX 03/27/07 962 151 105 ....
Wel1-BX 04/20/07 883 161 110 ....
Well-BX 05/22/07 1,265 138 102 ....
Well-BX 06/25/07 1 ý3,730 3,730 NA ....
Well-BX 07/12/07 1,556 144 108 ....
Well-BX 08/22/07 1,806 147 113 ....
Well-BX 09/21/07 1,430 150 110 ....
Well-BX 10/09/07 996 151 104 ....
Well-BX 11/20/0'7 1,270 173 122 ....
Well-BX 12/19/07 1,378 146 107 ....
Well-BX 01/16/08 1,097 154 107 ....
Well-BX 02/25/08 599 142 94 ....
Well-BX 03/13/08 536 139 91 ....
Well-BX 04/02/08 864 151 103 ....
Well-BX 05/28/08 770 137 93 ..
Well-BX 06/19/08 1,115 135 97 ....
Well-BX 07/08/08 1,354 129 97 ....
Well-BX 08/18/08 1,189 139 101 ....
Well-BX 09/22/08 3,213 130 120 ....
Well-BX 10/18/08 1,585 149 111 ....
Well-BX 11/21/08 968 144 100 --
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
U Constituent was detected above its New Jersey Groundwater Quality Criteria.
NNot Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 79 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample I ITritium Major Cations and Anions Identification Date Note Result (pCiIL) I LLD I Deviation Boron(mg/L) I Sodium(mg/L)
Well-BX 12/04/08 j 1,147 132 96 - I -
Well-CA 02/21/07 695 1.61 107 ....
Well-CA 03/15/07 932 165 113 ....
Well-CA 04/11/07 853 160 109 ....
Well-CA 05/22/07 665 170 111 ....
Well-CA 06/19/07 639 138 92 ....
Well-CA 07/12/07 710 144 96 ....
Well-CA 08/22/07 670 147 97 ....
Well-CA 09/20/07 599 150 98 ....
Well-CA 10/09/07 549 153 99 ....
Well-CA 11/19/07 437 177 112 ....
Well-CA 12/19/07 729 146 98 ....
Well-CA 01/16/08 792 156 104 ....
Well-CA 02/20/08 817 141 96 ....
Well-CA 05/28/08 1,006 137 97 ....
Well-CA 06/19/08 992 137 97 ....
Well-CA 07/08/08 964 133 94 ....
Well-CA 08/18/08 647 139 92 ....
Well-CA 09/22/08 753 128 88 ....
Well-CA 10/18/08 568 152 99 ....
Well-CA 11/21/08 1,330 145 106 ....
Well-CA 12/04/08 828 135 93 ....
Well-CB 02/21/07 156 152 93 -- -
Well-CB 03/27/07 K158 158 95 ....
Well-CB 04/11/07 -162 162 97 ....
Well-CB 05/22/07 '180 180 106 ....
Well-CB 06/19/07 '145 145 87 ....
Well-CB 07/12/07 '147 147 89 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 80 of 81
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2008 Well Sample ITritiunm Major Cations and Anions Identification Date Note Result (p i/L) LLD I' Deviation Boron(mg/L) Sodium(mg/L)
Well-CB 08/22/07 -149 149 90 ...
Well-CB 09/20/07 '144 144 87 ....
Well-CB 10/09/07 -150 150 89 ....
WeU-CB 11/19/07 -180 180 108 ....
Well-CB 12/19/07 '146 146 89 ....
Well-CB 01/16/08 -152 152 91 ....
Well-CB 02/20/08 181 141 87 ....
Well-CB 05/28/08 1,813 137 107 ....
Well-CB 05/29/08 1 -3,730 3,730 NA ....
Well-CB 06/19/08 1,499 143 106 ....
Well-CB 07/08/08 2,730 129 114 ....
Well-CB 08/18/08 1,674 139 107 ....
Well-CB 09/22/08 6,296 146 157 ....
Well-CB 10/18/08 2,074 150 118 ....
Well-CB 11/21/08 1,114 134 97 ....
Well-CB 12/04/08 861 133 92 ....
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.
< Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
i Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA -Not Available - Deviation and/or LLD were not reported.
-- Constituent not analyzed.
04/03/2009 10:37 AM Page 81 of 81
Table 03. Unit I Seismic Gap Drain Tritium Analytical Results, PSEG Nuclet, .
LLC, Salem Generating Station Date of Operation Tritium Results (pCiIL)
October 5, 2004 2,590,000 --
October 13, 2004 74,600,000 October 21, 2004 75,600,000 October 27, 2004 1,920,000 November 3, 2004 66,300,000 November 8, 2004 103,000,000 November 15, 2004 61,900,000 November 23, 2004 46,800,000 December 1,2004 40,400,000 December 8, 2004 63,400,000 December 14, 2004 44,800,000 December 21, 2004 89,900,000 January 4, 2005 13,600,000 January 11, 2005 40,900,000 January 19, 2005 17,700,000 January 24, 2005. 57,900,000 February 2, 2005 46,700,000 February 9, 2005 53,800,000 February 25, 2005 26,800,000 February 28, 2005 59,400,000 March 9, 2005 31,800,000 March 18, 2005 44,200,000 April 1, 2005 39,300,000 April 13,2005 34,600,000 t April 21, 2005 29,900,000 May 11, 2005 25,600,000 May 19, 2005 33,400,000 May 25, 2005 37,400,000 June 9, 2005 35,800,000 July 8, 2005 31,800,000 July 15, 2005 47,900,000 September 4, 2005 32,600,000 September 28, 2005 50,300,000 November 27, 2005 29,700,000 December 26, 2005 27,800,000 February 19, 2006 28,000,000 March 13, 2006 28,000,000 March 20, 2006 28,000,000' March 27, 2006 28,000,000 April 10, 2006 58,400,000 April 17, 2006 70,300,000 April 23,2006 70,300,000 May 1, 2006 74,600,000 May 7, 2006 88,000,000 May 14, 2006 85,800,000 May 20, 2006 83,800,000 May 27, 2006 6,970,000 May 29, 2006 ND June 5, 2006 ND June 12, 2006 73,100,000 June 18, 2006 58,400,000 June 25, 2006 72,400,000 June 29, 2006 63,200,000 July 2, 2006 30,000,000 July 15, 2006 30,000,000 July 22, 2006 63,200,000 July 29, 2006 36,300,000 August 5, 2006 45,800,000 August 12, 2006 68,600,000 August 20, 2006 68,600,000 September 17, 2006 123,000,000 September 30, 2006 118,000,000 October 7, 2006 128,000,000 October 14, 2006 133,000,000 October 21, 2006 116,000,000 October 28, 2006 84,000,000 November 4, 2006 113,000,000 November 11, 2006 100,000,000 Notes:
' concentration estimated based upon results of prior events ND = Data not availible Volume data after September 2005 estimated due to change in draining proceedt 1 of 3
Table 03. Unit I Seismic Gap Drain Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Date of Operation Tritium Results (pCi/L)
November 19, 2006 97,200,000 November 25, 2006 116,000,000 December 2, 2006 122,000,000 December 9, 2006 110,000,000 December 17, 2006 100,000,000 December 23, 2006 115,000,000 December 31, 2006 134,000,000 January 8, 2007 131,000,000 January 14, 2007 105,000,000 January 21, 2007 102,000,000 January 27, 2007 77,900,000 February 3, 2007 71,800,000 February 11, 2007 67,700,000 February 17, 2007 67,400,000 February 24, 2007 66,400,000 March 3, 2007 76,000,000 March 7, 2007 40,800,000 March 25, 2007 75,800,000 April 15, 2007 69,900,000 April 20, 2007 1,770,000 May 1, 2007 58,600,000 May 6, 2007 79,100,000 May 11, 2007 80,900,000 May 13, 2007 77,100,000 May 15, 2007 82,300,000 May 16, 2007 82,600,000 May 18, 2007 82,900,000 June 1, 2007 65,700,000 June 10,2007 66,600,000 June 17, 2007 63,200,000 June 21, 2007 70,200,000 June 24, 2007 73,900,000 June 26, 2007 81,400,000 July 6, 2007 39,000,000 July 8, 2007 1,970,000 July 11, 2007 66,200,000 July 19, 2007 60,400,000 July 24, 2007 57,300,000 July 29, 2007 12,800,000 August 5, 2007 61,500,000 August 12, 2007 66,600,000 August 15, 2007 71,400,000 August 21, 2007 76,400,000 August 26, 2007 66,300,000 September 6, 2007 88,200,000 September 9, 2007 87,000,000 September 16, 2007 89,000,000 September 26, 2007 100,000,000 October 7, 2007 94,600,000 October 14, 2007 98,200,000 October 21, 2007 190,000,000 October 24, 2007 107,000,000 November 1, 2007 100,000,000 November 4, 2007 97,400,000 November 11, 2007 102,000,000 November 19, 2007 4,800,000 November 30, 2007 99,000,000 December 9, 2007 124,000,000 December 16, 2007 107,000,000 December 23, 2007 40,500,000 January 6, 2008 107,000,000 January 13, 2008 70,900,000 January 20, 2008 104,000,000 Januray 27, 2008 ND February 3, 2008 139,000,000 February 10, 2008 509,000 February 17, 2008 ND February 20, 2008 144,000,000 February 24, 2008 142,000,000 March 2, 2008 149,000,000 March 9, 2008 142,000,000 March 16, 2008 169,000,000 March 23, 2008 178,000,000 March 30, 2008 164,000,000 April 6, 2008 181,000,000 April 13, 2008 170,000,000 April 20, 2008 183,000,000 April 27, 2008 5,860,000 May 4, 2008 169,000,000 May 11, 2008 159,000,000 2 of 3
Table 03. Unit 1 Seismic Gap Drain Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Date of Operation Tritium Results (pCi/L)
May 19, 2008 154,000,000 May 25, 2008 82,000,000 June 1, 2008 145,000,000 June 10, 2008 150,000,000 June 15, 2008 110,000,000 June 22, 2008 168,000,000 June 29, 2008 191,000,000 July 6, 2008 231,000,000 July 13, 2008 ND July 20, 2008 212,000,000 July 27, 2008 212,000,000 August 3, 2008 209,000,000 August 10, 2008 165,000,000 August 16, 2008 221,000,000 August 24, 2008 229,000,000 August 31, 2008 246,000,000 September 7, 2008 ND September 14, 2008 250,000,000 September 21, 2008 246,000,000 September 28, 2008 ND October 5, 2008 ND October 12, 2008 ND October 19, 2008 ND October 27, 2008 200,000,000 November 2, 2008 238,000,000 November 9, 2008 ND November 23, 2008 ND November 30, 2008 ND December 6, 2008 172,000,000 December 14, 2008 186,000,000 December 21, 2008 181,000,000 December 27, 2008 202,000,000 Notes:
1 concentration estimated based upon results of prior events ND = Data not availible Volume data after September 2005 estimated due to change in draining proceedt 3 of 3
THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED:
DRAWING NO. 1, "STATION LAYOUT" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
DRAWING 1 D-O1
THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, TIFAT CAN BE VIEWED AT TE[E RECORD TITLED:
DRAWING NO. FIGURE 2, "GROUNDWATER TRITIUM RESULTS" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
FIGURE 2 D-02
THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED:
DRAWING NO. DRAWING 3, "TRITIUM RESULTS BEYOND UNIT 1 GRS AREA" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
DRAWING 3 D-03
I THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED:
DRAWING NO. FIGURE 4, "WATER TABLE ELEVATION CONTOURS DURING OPERATION OF THE PERMANENT SYSTEM JANUARY 2008" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
FIGURE 4 D-04
THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED:
DRAWING NO. FIGURE 5, "WATER TABLE ELEVATION CONTOURS DURING OPERATION OF THE PERMANENT SYSTEM APRIL 2008" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
FIGURE 5 D-05
THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED:
DRAWING NO. FIGURE 6, "WATER TABLE ELEVATION CONTOURS DURING OPERATION OF THE PERMANENT SYSTEM AUGUST 2008" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
FIGURE 6 D-06
THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED:
DRAWING NO. FIGURE 7 "WATER TABLE ELEVATION CONTOURS DURING OPERATION OF THE PERMANENT SYSTEM DECEMBER 2008" WITHIN THIS PACKAGE... OR BY SEARCHING USING THE DOCUMENT/REPORT NO.
FIGURE 7 D-07
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