ML090540140

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Entergy - Unit 2 Spent Fuel Pool History
ML090540140
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 09/30/2005
From:
- No Known Affiliation
To:
NRC Region 1
References
Download: ML090540140 (2)


Text

Unit 2 Spent Fuel Poolo4&se Action Item 6 Time Line (from interview with C. Jackson, L.Liberatori and mod list)

  • Late 1960's IP2 design and construction without tell-tale drain system 1970 IP2 FSAR issued o FSAR discusses fuel pool with liner 1970 IP3 good idea for tell-tale drain system 1970-73 IP2 to NRC correspondence files (Cahill files) 1973 IP2 License to load fuel issued o

1980 Re-rack U2 SFP via mod MNF-80-2-001 1990 Re-rack U2 SFP via mod CPG-90-6038 1-C 1996 (oct)

NRC letter to IP2 Resolution of spent fuel pool storage issues 1996 (nov)

IP2 letter to NRC Comments regarding NRC letter fromOct 1996 1 1997 (sept)

NRC internal memo Follow-up on the Spent fuel pool action plan

  • 2000 Retirement of Spent fuel pool skimmer loop via mod FPX-00-.

12330-F 10-2-03 CR IP2-2003-6165 written for finding activity in soil samples taken below U2 SFP truck bay floor

  • 2004 Start removal of floor in U2 FSB for DCS o Removal of drain line found contaminated soil o

Shorten Aux coolant line through pool wall, in excavation area per ER 2-012, See Dwg 9321-F-2577 rev 23 for details o Remove loose soil via sandsucker S

S S

2005 (june) 7-22-05 Begin excavation of dirt and break rock for DCS crane foundation CR IP2-2005-3040 written for finding soil with activity

  • Action Item 14 OE Who does not have pool drain system?

" Per NRC IP2 is only plant in Region 1 without a pool leak detection sys

" Per former Rx Engr Manager. (MD) IP2 is only operating pool without a pool leak detection sys

  • Per Holtec users group conference call, No plant without a pool leak detection sys (plants include Southern Nuclear, TVA, Columbia, Quad Cities, Dresden, Salem Hope creek, JAF, VY ANO)

Action Item 15 Contact other Plants with pool leaks 0

S S

Salem JAF Seabrook?

From: Berko, David E (INPO) <BerkoDE@INPO.org>

To: Walpole, Robert <rwalpol@entergy.com>

Sent: Fri Sep 30 10:28:56 2005

Subject:

RE: IPEC UNIT 2 SPENT FUEL POOL WALL

Bob, I heard in the hall that Seabrook had a SFP liner leak and conducted a repair; might want to pass it on.

Dave Action Item 39 IP3 Drain check 0

0 CR IP2-2005-03557 CA3 issued to check IP3 drain WO IP3-05-22693 issued to check IP3 tell tale drain system with boroscope to determine if there is any blockage.

Action Item 40 Find 1992 Root cause 0

S S

Search for 1992 SAO 132 report has not been found in Merlin or Iron Mountain Search for OIR has not been found in Merlin or Iron Mountain Merlin search found Lucas-Pitkin report on core bore analysis of Unit 2 SFP in area of leak Action ?? Environmental report form Salem A complete report of the Salem Environmental testing plan and report has been received from Exelon.