ML081090617
| ML081090617 | |
| Person / Time | |
|---|---|
| Site: | Pilgrim |
| Issue date: | 04/28/2003 |
| From: | Digeronimo M Entergy Nuclear Generation Co, Entergy Nuclear Operations |
| To: | NRC/SECY |
| SECY RAS | |
| References | |
| 50-293-LR, ASLBP 06-848-02-LR, Pilgrim-Applicant-10, RAS J-98 | |
| Download: ML081090617 (4) | |
Text
Entergy CONDITION REPORT CR-PNP-2003-01706 Originator: DiGeronimo,Mark E Originator Group: QA Insp Staff Supervisor Name: Kelly,Gary R Discovered Date: 04/28/2003 21:00 Originator Phone: 8632 Operability Required: N Reportability Required:.N Initiated Date: 04/28/2003 21:23 Condition
Description:
The test pieces obtained from the west end of the CIPP liner at "A" SSW discharge line exhibit thickness measurements averaging.490 in. including the liner membrane, which is below the minimum requirement. The minimum thickness specified for the test samples is greater than or equal to.495 in., after deducting the thickness of the liner membrane. Note:
This condition report is being issued concurrently with NCR 03-027.
Immediate Action
Description:
Notified Maintenance supervision and Engineering, and initiated NCR 03-027.
Suggested Action
Description:
Evaluate the condition for any impact to anticipated performance of the liner.
EQUIPMENT:
Tag Name Taz Suffix Name Component Code Process System Code 29 TRENDING (For Reference Purposes Only):
Trend Type Trend Code KA=IN CRT=EF P1=10 WP=MAINT DOCKETED I I.RNlr Andl 15. 2008 (10:00am)
OFFICE OF SECRETARY PI I1 FMAKIN!(,R AND AFl.II JI'I.ATION5R,RTAFF U.S. NUCLEAR REGULATORY COMMISSION In the Matterc~ lof 5 ?~~w '
i Docket No."*'Z?1 4 Official Exhibit No.
6>4 OFFERED
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Intervenor,
/0 NRC Staff Othe.,
HDENTIFIED oo 0 q'O °t WitnessPane_
Action T ke o:
- o.
REJECTED WIThDRAWN ftof~erk
- basii S6~%62~2 Ar The0?
SEntergy ADMIN CR-PNP-2003-01706 Initiated Date: 4/28/2003 21:23 Owner Group: CRG Mgmt Current
Contact:
Current Significance: D - ADMIN CLOSE Closed by: Buckley,Patricia A 4/29/2003 12:58 Summary
Description:
Remarks
Description:
Closure
Description:
ADMIN CLOSE.
The CRG has determined that the CR identified condition is not a Condition Adverse to Quality or is an enhancement as defined in LI-102. Therefore, further analysis or actions recommended or needed to address the condition do not warrant tracking in the CR process. Any further actions should be addressed through the NCR process. This CR will be administratively closed as a -
CAT "D". NCR 03-027
Entergy OPERABILITY CR-PNP-2003-01706 OperabilityVersion:
1 Operability Code:
EQUIPMENT INOPERABLE Immediate Report Code:
NOT REPORTABLE Performed By:
OrNeill,Robert J 04/28/2003 23:39 Approved By:
Haislet,Randy E 04/29/2003 04:09 Operability
Description:
The test pieces obtained from the west end of the CIPP liner at "A" SSW discharge line exhibit thickness measurements averaging.490 in. including the liner membrane, which is below the minimum requirement. The minimum thickness specified for the test samples is greater than or equal to.495 in., after deducting the thickness of the liner membrane. NCR 03-027 was issued and must be closed prior to declaring "A" SSW operable.
Approval Comments:
added to the SSW LCO
vEntergy ASSIGNMENTS CR-PNP-2003-01706 Version: 1 Significance Code: D:7 ADMIN CLOSE Classification Code: NON-SIGNIFICANT Owner Group: CRG Mgmt Performed By: Buckley,Patricia A 04/29/2003 12:56 Assignment
Description:
ADMIN CLOSE.
The CRG has determined that the CR identified condition is not a Condition Adverse to Quality or is an enhancement as defined in LI-102. Therefore, further analysis or actions recommended or needed to address the condition do not warrant tracking in the CR process. Any fw-ther actions should be addressed through the NCR process. This CR will be administratively closed as a CAT "D". NCR 03-027