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MONTHYEARML0720004052007-05-14014 May 2007 Ssg Tube Inspection Discussion Points Prepared by the Office of NRR for Diablo Canyon Nuclear Generating Station Project stage: Other ML0720003672007-07-19019 July 2007 Summary of Conference Call with Diablo, Unit 1, Regarding Their 2007 Steam Generator Tube Inspections (TAC No. MD5549 Project stage: Other ML0721300342007-08-0808 August 2007 Summary of 5/15/2007 Conference Call Regarding the 2007 Steam Generator Tube Inspections Performed During 14th Refueling Outage Project stage: Other ML0722005192007-08-10010 August 2007 Notice of Meeting with Entergy Operations, Inc. Regarding Steam Generator Tube Inspection Results at Arkansas Nuclear One, Unit 1 Project stage: Meeting 2007-07-19
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Category:Letter
MONTHYEARIR 05000275/20230042024-02-0909 February 2024 Integrated Inspection Report 05000275/2023004 and 05000323/2023004 ML24002B1802024-01-29029 January 2024 LRA Audit Plan DCL-24-010, Nuclear Material Transaction Report for New Fuel2024-01-29029 January 2024 Nuclear Material Transaction Report for New Fuel ML24018A0152024-01-29029 January 2024 License Renewal Application Review Schedule Letter ML24017A2492024-01-24024 January 2024 Letter to Neil Peyron, Chairman, Tule River Tribe, Re. Diablo Canyon ML24024A1752024-01-24024 January 2024 Letter to Tribal Council San Luis Obispo County Chumash Indians on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24003A8902024-01-24024 January 2024 Letter to P. Gerfen - Diablo Canyon Notice of Intent to Conduct Scoping and Prepare an Environmental Impact Statement ML24012A1582024-01-24024 January 2024 Letter to Hon. Violet Sage Walker, Chairwoman Northern Chumash Tribal Council on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24012A0062024-01-24024 January 2024 Achp Scoping Letter for Diablo Canyon License Renewal ML24012A0552024-01-24024 January 2024 Letter to J. Polanco, Shpo, on Request to Initiate Section 106 Consultation and Scooping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24024A1562024-01-24024 January 2024 Letter to Hon. Gabe Frausto, Coastal Band of Chumash Indians on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24024A1652024-01-24024 January 2024 Letter to Hon. Mona Olivas Tucker, Yak Tityu Tityu Yak Tilhini Northern Chumas Indians on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24024A1612024-01-24024 January 2024 Letter Hon. Gary Pierce, Salian Tribe of Monterey and San Luis Obispo Counties on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24012A0362024-01-24024 January 2024 Request to Initiate Section 106 Consultation and Scoping Process for the Environmental Review License Renewal Application DCL-24-009, Nuclear Material Transaction Report for New Fuel2024-01-17017 January 2024 Nuclear Material Transaction Report for New Fuel DCL-24-008, Schedule Considerations for Review of the DCPP License Renewal Application2024-01-17017 January 2024 Schedule Considerations for Review of the DCPP License Renewal Application DCL-24-004, Supplement to License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2024-01-15015 January 2024 Supplement to License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b IR 05000275/20230112024-01-12012 January 2024 NRC License Renewal Phase 1 Inspection Report 05000275/2023011 DCL-23-129, Nuclear Material Transaction Report for New Fuel2023-12-27027 December 2023 Nuclear Material Transaction Report for New Fuel ML23326A0122023-12-21021 December 2023 12-21-23 Letter to the Honorable Byron Donalds from Chair Hanson Responds to Letter Regarding 2.206 Petition to Close Diablo Canyon Nuclear Power Plant, Unit 1 ML23341A0042023-12-19019 December 2023 LRA Acceptance Letter ML23352A2342023-12-18018 December 2023 Notification of Age-Related Degradation Inspection (05000275/2024014 and 05000323/2024014) and Request for Information DCL-23-122, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-12-14014 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation DCL-23-128, Emergency Plan Update2023-12-13013 December 2023 Emergency Plan Update ML23355A0952023-12-0808 December 2023 License Renewal Application Online Reference Portal DCL-23-125, Core Operating Limits Report for Unit 1 Cycle 252023-12-0606 December 2023 Core Operating Limits Report for Unit 1 Cycle 25 ML23291A2702023-11-28028 November 2023 Letter to Nakia Zavalla, Shpo, the Santa Ynez Band of Chumash Indians; Re., Diablo Canyon ISFSI Initiating Section 106 Consultation ML23320A2442023-11-28028 November 2023 Letter to Kerri Vera, Director of Department of Environmental Protection, Tule River Tribe; Re., Diablo Canyon ISFSI Initiating Section 106 Consultation ML23325A1382023-11-27027 November 2023 ISFSI Tribal Letter to San Luis Obispo County Chumash Indians ML23325A1322023-11-27027 November 2023 ISFSI Tribal Letter to Salian Tribe of Montgomery, San Luis Obispo ML23325A1332023-11-27027 November 2023 ISFSI Tribal Letter to Yak Tityu Tityu Northern Chumash Indians ML23307A0062023-11-27027 November 2023 ISFSI Tribal Letter to Northern Chumash Tribal Council ML24003A7242023-11-27027 November 2023 Independent Safety Committee; Diab Lo Canyon Nuclear Power Plant Operations, Thirty-Third Annual Report on the Safety ML23325A1292023-11-27027 November 2023 ISFSI Tribal Letter to Coastal Band of Chumash ML23320A1502023-11-17017 November 2023 Individual Notice of Consideration of Issuance of Amendment to Facility Operating License, Proposed No Significant Hazards Consideration Determination, & Opportunity for Hearing (Exigent Circumstances) (EPID L-2023-LLA-0155) - LTR DCL-23-121, Supplement to License Amendment Request 23-03, Revision to Technical Specification3.7.8, Auxiliary Saltwater System2023-11-16016 November 2023 Supplement to License Amendment Request 23-03, Revision to Technical Specification3.7.8, Auxiliary Saltwater System ML23296A0982023-11-15015 November 2023 Notification and Request for Consultation Regarding Pacific Gas and Electric Diablo Canyon Independent Spent Fuel Storage Installation Material License Renewal Request (Docket Number: 72-26) DCL-23-120, License Amendment Request 23-03 Revision to Technical Specification 3.7.8, Auxiliary Saltwater (Asw) System2023-11-14014 November 2023 License Amendment Request 23-03 Revision to Technical Specification 3.7.8, Auxiliary Saltwater (Asw) System ML23293A1052023-11-14014 November 2023 Receipt and Availability of License Renewal Application IR 05000275/20230032023-11-13013 November 2023 Integrated Inspection Report 05000275/2023003 and 05000323/2023003 ML23311A2082023-11-0909 November 2023 Reassignment of U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch IV DCL-23-118, License Renewal Application2023-11-0707 November 2023 License Renewal Application ML23318A2102023-10-31031 October 2023 Independent Safety Committee; Thirty-Third Annual Report on the Safety of Diablo Canyon Nuclear Power Plant Operations DCL-2023-520, Discharge Self-Monitoring at Diablo Canyon Power Plant (DCPP)2023-10-19019 October 2023 Discharge Self-Monitoring at Diablo Canyon Power Plant (DCPP) DCL-23-103, Independent Spent Fuel Storage Installation - Withdrawal of License Amendment Request 22-01, Request for Approval of Alternative Security Measures for Early Warning System2023-10-13013 October 2023 Independent Spent Fuel Storage Installation - Withdrawal of License Amendment Request 22-01, Request for Approval of Alternative Security Measures for Early Warning System IR 05000275/20240152023-10-10010 October 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection (050002752024015 and 050003232024015) 2024-02-09
[Table view] Category:Meeting Summary
MONTHYEARML23268A4072023-09-27027 September 2023 Summary of September 19, 2023, Closed Public Meeting with Pacific Gas and Electric Company Regarding Alternative Security Measures for Early Warning System License Amendment Request for Diablo Canyon Nuclear Power Plant, Units 1 and 2 ML23265A1902023-09-26026 September 2023 Meeting Summary: September 13, 2023 Diablo Canyon, Units 1 and 2 License Renewal Application Pre-Application Meeting ML23143A2262023-06-0101 June 2023 May 3, 2023, Summary of Public Meeting to Discuss the End of Cycle Assessment and Pre-Submittal License Renewal Process Overview for Diablo Canyon Power Plant, Units 1 and 2 ML22272A5072022-09-29029 September 2022 Summary of September 27, 2022, Closed Meeting with Pacific Gas and Electric Company Regarding Planned Security Plan Changes for Diablo Canyon Nuclear Power Plant, Units 1 and 2 ML22147A0932022-06-0606 June 2022 2021 Annual Assessment Public Meeting Summary ML22126A0162022-05-0909 May 2022 Summary of April 27, 2022, Closed Teleconference with Pacific Gas and Electric Company Regarding Alternative Security Measures for Early Warning System License Amendment Request for Diablo Canyon Nuclear Power Plant, Units 1 and 2 ML21246A0202021-09-0808 September 2021 Summary of August 30, 2021, Pre-Submittal Teleconference with Pacific Gas and Electric Company Regarding a Post-Shutdown Emergency Plan License Amendment Request for Diablo Canyon Nuclear Power Plant, Units 1 and 2 ML21140A3892021-05-24024 May 2021 Riv Column 1 EOC 2020 Public Meeting Summary ML20332A1802020-12-0101 December 2020 Summary of November 24, 2020, Pre-Submittal Teleconference with Pacific Gas and Electric Company a Permanently Defueled Technical Specification License Amendment Request ML20231A6522020-08-24024 August 2020 Summary of Teleconference with Pacific Gas & Electric Company Regarding an Exigent Amendment Request to Modify Diablo Canyon Power Plant, Units 1 & 2, Technical Specification 3.7.5, Auxiliary Feedwater (AFW) System EPID L-2020-LLA-017 ML20189A2832020-07-0707 July 2020 Summary of Region IV Annual Assessment Public Meeting ML19318F5272019-11-15015 November 2019 Summary of the August 27, 2019, Public Meeting Near the Diablo Canyon Nuclear Power Plant Regarding the Establishment and Operation of Community Advisory Boards ML19196A0742019-07-22022 July 2019 Summary of Meeting with Pacific Gas and Electric Company Regarding Forthcoming Activities Associated with Diablo Canyon Nuclear Power Plant, Units 1 and 2 Planned Decommissioning ML19064B2652019-03-14014 March 2019 Summary of February 28, 2019, Public Meeting with Pacific Gas and Electric Company to Discuss the Proposed Relief Request Concerning Reactor Vessel Internal Visual Examination for the Diablo Canyon Nuclear Power Plant, Units 1 & 2 ML18348A4202018-12-31031 December 2018 Summary of Meeting with Pacific Gas & Electric Co. to Discuss Exemption Request to Withdraw Funds from the Nuclear Decommissioning Trusts to Fund Decommissioning Planning Activities at Diablo Canyon Nuclear Power Plant ML18207A7332018-08-10010 August 2018 Summary of Pre-Licensing Meeting with PG&E Co. to Discuss the Proposed LAR to Implement WCAP-16996-A, Revision 1, Realistic LOCA Evaluation Methodology Applied to the Full Spectrum of Break Sizes at Diablo Canyon ML17198A6032017-07-17017 July 2017 Summary of Annual Assessment Meeting Regarding Diablo Canyon Power Plant 2016 Performance ML16190A1782016-07-0808 July 2016 Summary of Annual Assessment Town Hall Meeting and Public Outreach Regarding Diablo Canyon Power Plant 2015 Performance ML16011A2042016-01-14014 January 2016 Summary of Conference Call on January 7, 2016, Between the U.S. NRC and Pacific Gas and Electric Co. Concerning the Responses to RAI for the Review of the Diablo Canyon Power Plant, Units 1 and 2, License Renewal Application (CAC Nos. MF401 ML15343A1272015-12-24024 December 2015 Summary of Meeting with Pacific Gas and Electric to Discuss Diablo Canyon, Units 1 and 2 Amendment Request to Revise UFSAR for Beacon Power Distribution Monitoring System Methodology and TS 5.6.5 (COLR) Paragon and Nexus Methodologies ML15348A1702015-12-17017 December 2015 Summary of Telephone Conference Call Held Between NRC and Pacific Gas and Electric Co., Concerning the RAI Responses Pertaining to the Diablo Canyon Power Plant LRA Environmental Review ML15280A2842015-10-20020 October 2015 Summary of Meeting with Pacific Gas & Electric to Discuss Diablo Canyon, Units 1 and 2 Request to Adopt National Fire Protection Association NFPA 805, Performance-Based Standard for Fire Protection for LWR Generating Plants (2001 Edition), ML15279A4222015-10-0909 October 2015 Summary of 8/25/15 Meeting with Pacific Gas and Electric to Discuss Diablo Canyon Units 1 and 2 Amendment Request to Adopt Risk-Informed Completion Times, TSTF-505, Revision 1, Provide Risk-Informed Extended Completion Times-RITSTF Initiati ML15275A0942015-10-0707 October 2015 Summary of the Severe Accident Mitigation Alternatives Site Audit Related to the Diablo Canyon Power Plant, Units 1 and 2 License Renewal Review ML15275A1302015-10-0707 October 2015 Summary of the Site Audit Related to the Diablo Canyon Power Plant, Units 1 and 2 License Renewal Environmental Review ML15233A0062015-09-10010 September 2015 Summary of Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML15233A0052015-09-0909 September 2015 Summary of Meeting with Pacific Gas and Electric to Discuss Diablo Canyon, Units 1 & 2 License Amendment Request to Adopt Risk-Informed Completion Times, TSTF-505, Revision 1, Provide Risk-Informed Extended Completion Times-RITSTF. Initiati ML15233A4912015-09-0101 September 2015 August 5, 2015, Public Scoping Meetings for the Environmental Review of the Diablo Canyon Power Plant, Units 1 and 2 License Renewal Application ML15209A9442015-07-28028 July 2015 June 24, 2015, Summary of Annual Assessment Meeting with Pacific Gas and Electric and Public Open House Regarding Diablo Canyon Power Plant 2014 Performance ML15125A1862015-05-27027 May 2015 April 28, 2015, Summary of Category 1 Public Meeting with Pacific Gas and Electric Company to Discuss Diablo Canyon'S Seismic Hazard Reevaluation Associated with Implementation of Japan Lessons-Learned Near-Term Task Force Recommendation 2. ML15134A2572015-05-18018 May 2015 5/7/15 Summary of Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML15092A0792015-04-16016 April 2015 July 14-17, 2014 - Summary of Diablo Canyon, Units 1 and 2, Audit to Adopt National Fire Protection Association NFPA 805, Performance-Based Standard for Fire Protection for LWR Generating Plants (2001 Edition) ML15069A0952015-03-24024 March 2015 Summary of Telephone Conference Call Held on March 4, 2015 Between the U.S. Nuclear Regulatory Commission and Pacific Gas and Electric Company Concerning the Diablo Canyon Power Plant, Units 1 and 2, License Renewal Application ML15043A1992015-02-19019 February 2015 2/3/2015 Summary of Meeting with Pacific Gas and Electric Regarding Presubmittal Discussion on Alternate Source Term License Amendment Request for Diablo Canyon Power Plant, Units 1 and 2 ML15037A2482015-02-0505 February 2015 Summary of Regulatory Conference to Discuss Safety Significance of Diablo Canyon Power Plant Protective Action Recommendations for Areas of the Ocean Finding ML14350A2712014-12-22022 December 2014 Summary of 12/11/14 Preapplication Meeting with Pacific Gas and Electric Company to Discuss License Amendment Request to Support Installation of 500 Kilovolt Output Generator Breakers at Diablo Canyon, Units 1 and 2 ML14029A4502014-12-10010 December 2014 Summary of 12/18/13 Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML14295A7332014-11-17017 November 2014 9/24/14 Summary of Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML14197A3522014-07-22022 July 2014 7/9/14 Summary of Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML14157A0912014-06-17017 June 2014 Summary of 5/21/14 Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML14155A3742014-06-0404 June 2014 May 22, 2014, Summary of Annual Assessment Meeting with Pacific Gas and Electric Regarding Diablo Canyon Power Plant 2013 Performance ML14113A4932014-05-0606 May 2014 Summary of Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML14113A4222014-04-23023 April 2014 Public Meeting with Pacific Gas & Electric (Pg&E)To Discuss the Operating Performance for Diablo Canyon Power Plant for the Period January 1 - December 31, 2013 ML13329A4172013-12-30030 December 2013 Summary of Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 ML13354C0912013-12-23023 December 2013 Summary of Annual Assessment Meeting with Pacific Gas & Electric Re Diablo Canyon Nuclear Power Plant 2012 Performance ML13282A3822013-11-0707 November 2013 10/2/2013 Summary of Pre-Application Meeting with Pacific Gas and Electric Company to Discuss Upcoming Structural Weld Overlay Relief Request to Use an Alternative to Disposition Detected Laminar Indications at Diablo Canyon, Unit 2 ML13269A0042013-10-0808 October 2013 9/24/13 Summary of Pre-Application Meeting to Discuss License Amendment Request for Technical Specification 3.8.1 Diesel Generator Surveillance Requirements at Diablo Canyon, Units 1 and 2 ML13270A2922013-10-0202 October 2013 Summary of 9/26/13 Meeting to Discuss Amendment Request to Adopt Technical Specifications Task Force TSTF-505, Provide Risk-Informed Extended Completion Times, RITSTF Initiative 4B at Diablo Canyon, Units 1 and 2 ML13269A0072013-10-0101 October 2013 Summary of 9/25/13 Pre-Application Meeting to Discuss Emergency Core Cooling System Evaluations for License Amendment Request at Diablo Canyon, Units 1 and 2 ML13266A0882013-09-30030 September 2013 9/18/13 - Summary of Closed Meeting with Pacific Gas and Electric Company to Discuss Digital Replacement of Process Protection System at Diablo Canyon Power Plant, Units 1 and 2 2023-09-27
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Text
August 8, 2007 Mr. Jack S. Keenan Senior Vice President and CNO Pacific Gas and Electric Company Diablo Canyon Power Plant P.O. Box 770000 San Francisco, CA 94177-0001
SUBJECT:
DIABLO CANYON POWER PLANT, UNIT 1 -
SUMMARY
OF CONFERENCE CALL REGARDING THE 2007 STEAM GENERATOR TUBE INSPECTIONS (TAC NO. MD5549)
Dear Mr. Keenan:
On May 15, 2007, the Nuclear Regulatory Commission (NRC) staff, participated in a conference call with Pacific Gas and Electric (PG&E) to discuss the 2007 steam generator tube inspections performed at Diablo Canyon Power Plant, Unit 1, during their 14th refueling outage (1R14). To facilitate the phone call, PG&E was provided some discussion points for the call. On May 15, 2007, PG&E provided preliminary information regarding the results of its inspection. This information is attached as Enclosure 2.
Based on the information provided during the conference call, the NRC staff did not identify any issues that warranted additional follow-up at this time. Enclosure 1 is a summary of the conference call.
This completes our review of the preliminary results for the 2007 steam generator tube inspections at the Diablo Canyon Power Plant, Unit 1.
Sincerely,
/RA/
Alan B. Wang, Project Manager Plant Licensing Branch IV Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-275
Enclosures:
- 1. Summary of Conference Call
- 2. PG&E Preliminary SG Inspection Results cc w/encls: See next page
PKG ML072140015, Summary/Encl 1 ML072130034, Encl 2 ML072000405 OFFICE NRR/DORL/LPL4/PM NRR/DORL/LPL4/LA NRR/DORL/LPL4/BC NAME AWang JBurkhardt THiltz DATE 8/8/07 8/7/07 8/8/07 Diablo Canyon Power Plant, Units 1 and 2 cc:
NRC Resident Inspector Jennifer Post, Esq.
Diablo Canyon Power Plant Pacific Gas & Electric Company c/o U.S. Nuclear Regulatory Commission P.O. Box 7442 P.O. Box 369 San Francisco, CA 94120 Avila Beach, CA 93424 City Editor Sierra Club San Lucia Chapter The Tribune ATTN: Andrew Christie 3825 South Higuera Street P.O. Box 15755 P.O. Box 112 San Luis Obispo, CA 93406 San Luis, Obispo, CA 94306-0112 Ms. Nancy Culver Director, Radiologic Health Branch San Luis Obispo State Department of Health Services Mothers for Peace P.O. Box 997414, MS 7610 P.O. Box 164 Sacramento, CA 95899-7414 Pismo Beach, CA 93448 Mr. James Boyd, Commissioner Chairman California Energy Commission San Luis Obispo County 1516 Ninth Street MS (31)
Board of Supervisors Sacramento, CA 95831 1055 Monterey Street, Suite D430 San Luis Obispo, CA 93408 Mr. James R. Becker, Vice President Diablo Canyon Operations and Mr. Truman Burns Station Director Mr. Robert Kinosian Diablo Canyon Power Plant California Public Utilities Commission P.O. Box 56 505 Van Ness, Room 4102 Avila Beach, CA 93424 San Francisco, CA 94102 Jennifer Tang Diablo Canyon Independent Safety Field Representative Committee United States Senator Barbara Boxer Attn: Robert R. Wellington, Esq. 1700 Montgomery Street, Suite 240 Legal Counsel San Francisco, CA 94111 857 Cass Street, Suite D Monterey, CA 93940 Regional Adminstrator, Region IV U.S. Nuclear Regulatory Commission Harris Tower & Pavillion 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011-8064 June 2007
NRC
SUMMARY
OF MAY 15, 2007, CONFERENCE CALL ON STEAM GENERATOR TUBE INSPECTIONS FOR REFUELING OUTAGE 14 PACIFIC GAS AND ELECTRIC COMPANY DIABLO CANYON POWER PLANT, UNIT 1 DOCKET NO. 50-275 On May 15, 2007, the Nuclear Regulatory Commission (NRC) staff participated in a conference call with Diablo Canyon Power Plant, Unit 1, representatives regarding their 2007 steam generator (SG) tube inspections. A summary of the information discussed during the call is provided below.
The four SGs at Diablo Canyon Unit 1 are Westinghouse model 51. Each SG contains approximately 3400 mill-annealed Alloy 600 tubes. Each tube has a nominal outside diameter of 0.875 inches and a nominal wall thickness of 0.050 inches. Each tube is roll-expanded for approximately 2.75 inches from the bottom of the tubesheet, and is secured into the remaining portion of the tubesheet by the Westinghouse Explosive Tube Expansion (WEXTEX) process.
The tubesheet is approximately 21 inches thick and each tube is expanded for essentially the full thickness of the tubesheet. Each SG contains seven carbon steel tube support plates with drilled holes through which the tubes pass. All four SGs are scheduled to be replaced during the next refueling outage in 2009.
In addition to a depth-based tube repair criteria, the licensee is authorized to apply the voltage-based tube repair criteria for predominantly axially-oriented outside diameter stress-corrosion cracking (ODSCC) within the tube support plates. The licensee is also authorized to implement an alternate repair criteria for primary water stress-corrosion cracking (PWSCC) indications at the tube support plate elevations and to leave certain flaws within the tubesheet region in service, provided they satisfy the W* repair criteria.
Prior to the call, the licensee was provided with discussion points to help facilitate the phone conference. In support of the phone call, the licensee provided a document that provided the inspection status as of May 15, 2007 (see Enclosure 2). At the time of the call, the eddy current inspections for Diablo Canyon Unit 1 were complete and repairs (tube plugging) were in progress. No unusual degradation or unexpected conditions were detected during the inspections. Most of the new indications were less than 0.5 volts.
Additional clarifying information or information not included in Enclosure 2 provided by the licensee is summarized below:
C Acronyms used by the licensee in the material they provided include: SG (steam generator), HTS (hotleg tubesheet), TSP (tube support plate), AVB (antivibration bar), SCC (stress corrosion cracking), DSI (distorted support indication), CLT (cold leg thinning), AONDB (axial ODSCC not detectable by bobbin), ET (eddy current testing), TTS (top of tubesheet), ARC (alternate repair criteria), ID (inside diameter), OD (outside diameter), DNT (dent), SAI (single axial indication), SPR ENCLOSURE 1
(support plate residual), NDD (no detectable degradation), and DIS (distorted ID support plate bobbin signal).
C The amount of primary-to-secondary leakage observed during cycle 14, just completed, was very small and was similar to that observed during prior cycles.
C A deviation from Electric Power Research Institute guidelines for secondary water chemistry has existed for many years.
C No additional indications were found in the expanded scope examinations performed in SG 1-1 and SG 1-3 at dented TSPs.
C Approximately 16 CLT indications that were greater than 1.5 volts were re-inspected with a rotating probe. There were no unusual results. There were 11 new CLT indications identified this outage and these were inspected with a rotating probe. The total population of tubes with known CLT is approximately 171.
C All crack-like indications not covered by an ARC are plugged.
C In Table 2, the DIS Overcall Rate should be 94 percent since 2 of the 32 DIS indications in less than 2 volt dents were confirmed as SAIs. The DIS overcall rate is typical.
C In Table 2, the axial PWSCC (New) row should indicate that there were two indications in SG 1-1 and none in SG 1-3.
C In Table 2, there were a total of 13 circumferential ODSCC indications.
C Of the 219 axial PWSCC indications that were present since the prior outage, the worst underprediction in the burst pressure (from the projections based on the last inspection) was only approximately 300 pounds per square inch (psig).
C The number of axial-oriented ODSCC indications at the TSPs was less than the projections from the last inspection.
C The axial ODSCC indication in the sludge pile was approximately 1 inch above the TTS. The sludge pile extends to approximately 2-inches above the TTS.
The sludge pile is considered small. This is the first time that an indication was found in the sludge pile. The indication was found with the rotating probe. The licensee concluded that this was not a free-span crack based on the location and the number of rotating probe exams performed in the free-span region (as a result of indications at tube supports (i.e., 2 inches above and below the support), the free-span ding sampling program, and the inspection of other bobbin indications in the free-span region).
C All of the volumetric OD indications were located at the TSP elevations. All indications were at the lower TSPs and associated with bobbin indications. The indications were attributed to intergranular attack or closely spaced axial ODSCC indications.
C The performance criteria associated with the steam line break and feedwater line break differential pressures are 3367 psig and 3790, psig, respectively (i.e., 1.4 times the differential pressure). The performance criteria associated with three times the normal operating differential pressure is 4473 psig.
C In Table 3, the projected (i.e., 2009) burst pressure for the tube in row 34 column 53 in SG 1-2 was 3582 psig based on the Argonne National Laboratory burst pressure model. This tube was plugged. The burst pressure for this indication (in the as-found 2007 condition) was slightly less than the projected burst pressure (based on the projection from the prior inspection in 2005).
C The axial indications in the sludge pile and at the TTS were small so the flaw dimensions were not profiled.
C All circumferential indications were considered small (i.e., less than the threshold value for in-situ pressure testing).
The NRC staff did not identify any issues that warranted follow-up action at this time; however, the NRC staff asked to be notified in the event that any unusual conditions were detected during the remainder of the outage.