ML070790110

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CR-PNP-2003-01582, Primary Containment Isolation Valve (PCIV) 6-CK-62B Failed to Meet Its Individual Valve Local Leak Rate Test (LLRT) Acceptance Criteria
ML070790110
Person / Time
Site: Pilgrim
Issue date: 04/25/2003
From:
Entergy Corp
To:
Office of Nuclear Reactor Regulation
References
CR-PNP-2003-01582
Download: ML070790110 (12)


Text

3 Originator: Manderino,Peter Originator Group: Eng P&C Components Mgmt Supervisor Name: Veglia,Vincenzo P Discovered Date: 04/25/2003 OR32 Entergy I

CONDITION REPORT CR-PNP-2003-01582 Originator Phone: 8044 Operability Required: Y Reportability Required: Y Initiated Date: 04/25/2003 0958 Condition

Description:

Primary Containment Isolation Valve (PCIV) 6-CK-62B failed to meet its individual valve Local Leak Rate Test (LLRT) acceptance criteria of less than or equal to 7.89 SLM. Since LLRT was acceptable on the inboard PCIV (6-CK-58B) the actual penetration leakage was small and does not exceed overall Primary Containment Containment allowable leakage.

Immediate Action

Description:

Perform maintenance IAW P99008 18 to achieve acceptable post maintenance LLRT results.

Suggested Action

Description:

EQUIPMENT:

Tag Name Tag Suffi Name Component Code Process System Code CK 06 TRENDING (For Reference Purposes Only):

Trend Type Trend Code PI=SI CRT=EF

ADMIN Entergy I

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Initiated Date: 4/25/2003 958 Current

Contact:

R. HUNNEFELD+

Owner Group :Eng P&C Components Mgmt Current Significance: B - EFA (DCA)

Closed by: McWilliams,Dorena C 10/14/2003 7:07 CR-PNP-2003-01582 Summary

Description:

Remarks

Description:

Closure

Description:

All CAS associated with this CR were reviewed by the responsible manager. Upon the manager's recommendation, this CR is being closed.

Per ENN-LI-102, Para. 5.8.2.3: Independent reviews are not required for non-significant condition reports. The documented closeout verification performed by the Responsible Management is adequate authorization for closure of the CR

Enterffy I

OPERABILITY I CR-PNP-2003-01582 OperabilityVersion: 1 Operability Code: EQUIF'MENT INOPERABLE Immediate Report Code: NOT REPORTABLE Performed By: Noyes,David E 04/25/2003 17:40 Approved By: NoyesDavid E 04/25/2003 17:41 Operability

Description:

Individual outboard valve is inoperable. OveraIl penetration remains operable due to performance of inboard valve.

Approval Comments:

A S S I G N M E N T S 1 CR-PNP-2003-01582 L

E n f w I Version: 1 Significance Code: B - EFA (DCA)

Classification Code: NON-SIGNIFICANT Owner Group: Eng P&C Components Mgmt Performed By: Buckley,Patricia A Assignment

Description:

Responsible Manager: T. White

[4/29/03; T. WHITE] Changed owner to T. Fox.

04/26/2003 10:27

REPORTABILITY I CR-PNP-2003-01582 En-w I

Reportability Version: 1 Report Number:

Report Code: NOT REPORTABLE (1)

Boilerplate Code: NOT REPORTABLE Performed By : Ellis,Douglas W Reportability

Description:

Not reportable - This event does not meet the screening criteria of WI 3.06-01.

04/27/2003 06:02

CA Number:

1 I--

Name Bethay,Stephen J Fox,Thomas M Carrol1,William G Assigned By: Engineering Director Assigned To: Eng P&C Components Mgmt Subassigned To : Eng P&C Plant Programs Staff Originated By: Buckley,Patricia A Performed By: Veglia,Vincenzo P 4/26/2003 10:29:39 5/23/2003 16:17:14 Subperformed By: Carrol1,William G 5/23/2003 16: 1 1 :46 Approved By:

Closed By: Veglia,Vincenzo P 5/23/2003 16: 17:49 Current Due Date: 05/26/2003 Initial Due Date: 05/26/2003 CA Type: DISPOSITION - EFA Plant Constraint: NONE CA

Description:

Please provide an Equipment Failure AnalysisDirect Cause and develop a corrective action plan using the guidance provided in LI-102.

Response

Subresponse :

See sub-response.

See attached Equipment Failure Analysis.

Closure Comments:

The response to this CA has been reviewed and found acceptable for closure of the CA.

Attachments:

Subresp Description 6CK-62B Equipment Failure Analysis

Attachment Header Document Name:

Document Location Subresp Description 1 i I _.-.

Attach

Title:

6CK-62B Equipment Failure Analysis I _ _ -

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IEQUIPMENT FAILURE ANALYSlSl CONDITION REPORT NO. 03-1582 1. Problem

Description:

Primary Containment Isolation Valve (PCIV) 6-CK-62B failed the Appendix J as-found local leak rate test.

2. Direct Cause: Inspection of the valve internals revealed worn hinge pins and bushings which resulted in misalignment of the disc in relation to the valve body seating surface. As-found condition: Disc off center to left, Disc metal to metal with seat @ -2 oclock (not touching anywhere that could be measured-top half of disc), Disc was loose on hinge pins and could be moved side to side, When dropped disc did not self-center side to side-disc stayed to left with metal to metal contact, Disc was.015 low measured at 12 oclock position. Soft seat elastomer appeared to have eroded over the cycle resulting in less than full contact around the valve seating surface. Prior to RFO-13 an industry search was done to evaluate the elastomer seating material looking at the material PNPS uses vs. industry peers. There were no suitable material replacements found.
3. Contributing Causes: none
4. Maintenance Rule Failure: YES
5. Extent of Problem: 4 possible check valves-6-CK-62 A/B and 6-CK-58A/B. Disassembly of 62 A showed wear in hinge pin bushings similar to, but not as severe to 6 2 B The hinge pins on 62 B showed more signs of wear than 62A. Disassembly of 58s showed internals to be in good shape-hinge pins and bushings were replaced during RFO-13. Soft seat material was found to be good in 58 A and B. The soft seats had been installed in 58 A/B during RFO -13.

The soft seats had been installed in 62 A/B during RFO-12.

6. Corrective Actions Completed (include Dates if possible) 6-CK-62B rebuilt per P9900820 (4/30/03). Passed PWT LLRT. Initiated WRT for RFO-15 to map valve journals both for alignment and concentricity combined with replacement of soft seats. Findings will be used to determine if valve body requires machining to improve hinge pin alignment.

Cause: worn hinge pins-replaced 4/30/03 Cause: worn hinge pin bushings-replaced 4/30/03 Cause: eroded soft seats-replaced 4/30/03 Potential Cause: worn body journals (diameters egg-shaped or alignment skewed) WRT written to Add to RFO-15 scope during rebuild of 6-CK-62 A/B (WRT #080873) 1

IEQUIPMENT FAILURE ANALYSlSl

7) Corrective Actions Required (if not required, state I'N/R") N/R Action Required/New CA Number:

(add additional actions as needed)

8) Corrective Actions required to eliminate and/or reduce the likelihood of recurrence of Corrective Action #3) Evaluate use of stellite or other hard surfacing of hinge pins to reduce Propensity to wear.

identified cause(s) and contributing cause(s).

(NOTE: Address each cause and contributing cause. If corrective actions are not proposed, for each cause and contributing cause, provide a basis for why no corrective action is necessary.)

Action Required/New CA Number: C/A #3) Evaluate use of stellite or other hard surfacing of hinge pins to reduce propensity to wear. Initiate ER for PDC if suitable replacement is found.

(add additional actions as needed) 2

CORRECTIVE ACTION I CR-PNP-2003-01582 CA Number:

2 Assigned By: CRG Mgmt Assigned To: Maint Mechanical Mgmt Subassigned To :

Sholler,Robert B Originated By: Buckley,Patricia A Performed By: Mulligan,Kevin J Subperformed By:

Approved By:

Closed By: Mulligan,Kevin J 4/26/2003 10:33:13 5/4/2003 08:50:44 5/4/2003 08:50:44 Current Due Date: 05/05/2003 Initial Due Date: 05/05/2003 CA Type: CORRECTIVE ACTION Plant Constraint: RF014D-DRN DWN VSSL CA

Description:

Primary Containment Isolation Valve (PCIV) 6-CK-62B failed to meet its individual valve Local Leak Rate Test (LLRT) acceptance criteria of less than or equal to 7.89 SLM. Since LLRT was acceptable on the inboard PCIV (6-CK-58B) the actual penetration leakage was small and does not exceed overall Primary Containment Containment allowable leakage.

"As the Responsible Manager, validate the problem statement and determine corrective actions as needed to resolve the adverse condition(s). Perform repairs as needed to support acceptable PWT LLRT. Coordinate repair activities with Engineering point-of-contact. Engineering wants to be notified when valve is disassembled to capture information for an Equipment Failure Evaluation.

Response

In accordance with this Corrective Action and associated Maintenance Request, the required repairs to this valve have been completed and it satisfactorily passed it's "As-Left LLRT. Even though the Maintenance Request can not be closed out until completion of the final hot torque and in-service leak tests are completed, this Corrective Action can be closed out.

Subresponse :

Closure Comments:

EnfeTgy I

CANumber:

3 CORRECTIVE ACTION CR-PNP-2003-01582 Group 1 1 -

Name I

-xlllll Assigned By: Eng P&C Components Mgmt Fox,Thomas M Assigned To: Eng P&C Plant Programs Staff Carroll,William G Subassigned To :

I Originated By: Fox,Thomas M Performed By: Carrol1,William G Subperformed By:

Approved By:

Closed By: Carrol1,William G 5/22/2003 02 : 04: 5 5 9/30/2003 15: 045 8 9/30/2003 15:04:58 Current Due Date: 09/30/2003

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Initial Due Date: 09/30/2003 CA Type: ADMIN CA Plant Constraint: NONE CA

Description:

Evaluate use of stellite or other hard surfacing for hinge pins to reduce susceptability to wear. Initiate ER for PDC if suitable replacement material is found.

Response

Reviewed the specification for the existing hinge pins and evaluated hardness of material. The existing hinge pins are manufactured using 410 stainless hardened to an RC hardness of 43. This material is judged to be very hard and an ideal selection for the application. After discussing material with Vendors it is doughtful a more cost effective material exibiting the required strength and hardness can be procurred. The combiation of stellite bushings with stainless hinge pins is acceptable. No additional actions are required.

Subresponse :

Closure Comments:

CA Number:

4

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11111-Group 1

Name Assigned By: CA&A Staff Assigned To: Eng P&C Components Mgmt Fox,Thomas M Subassigned To :

Originated By: McWilliams,Dorena C Performed By: Fox,Thomas M Subperformed By:

Approved By:

Closed By: Fox,Thomas M 10/1/2003 12:15:08 10/10/2003 10:38: It 10/10/2003 10:38: 1 e Current Due Date: 10/15/2003 Initial Due Date: 10/15/2003 CA Type: CR CLOSURE REQUEST Plant Constraint: NONE CA

Description:

Please review the closed corrective action(s) to verify adequacy and completeness to remedy the identified condition, by using the guidance in Section 5.8.1 of LI-102. If the CR is appropriate for closure, please indicate your concurrence by closure of this action. Should the closure not be satisfactory, issue a new action item to correct the deficiency.

Response

Subresponse :

Corrective actions have been completed and are sufficient to address the identified condition. No further actions are required.

Closure Comments: