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Category:Inspection Report
MONTHYEARIR 05000219/20240022024-09-0505 September 2024 – NRC Inspection Report 05000219/2024002 and 07200015/2024001 IR 05000219/20240012024-05-14014 May 2024 Decommissioning Intl, LLC Oyster Creek Nuclear Generating Station - NRC Inspection Report No. 05000219/2024001 ML24046A1242024-02-29029 February 2024 – NRC Inspection Report 05000219/2023003 IR 05000219/20230022023-11-0909 November 2023 EA-23-076 Oyster Creek Nuclear Generating Station - Notice of Violation and Proposed Imposition of Civil Penalty - $43,750 - NRC Inspection Report No. 05000219/2023002 ML23214A2472023-08-22022 August 2023 NRC Inspection Report 05000219/2023002 IR 05000219/20230012023-05-31031 May 2023 NRC Inspection Report No. 05000219/2023001 IR 07200015/20234012023-05-16016 May 2023 NRC Independent Spent Fuel Storage Installation Security Inspection Report 07200015/2023401 IR 05000219/20220022023-02-0909 February 2023 NRC Inspection Report No. 05000219/2022002 IR 07200015/20224012022-12-0606 December 2022 NRC Independent Spent Fuel Storage Installation Security Inspection Report 07200015/2022401 (Letter & Enclosure 1) IR 05000219/20220012022-08-11011 August 2022 NRC Inspection Report 05000219/2022001 IR 05000219/20214022022-01-26026 January 2022 EA-21-041: Confirmatory Order Related to Oyster Greek Nuclear Generating Station - NRC Investigation Report I-2020-007; NRC Inspection Report Nos. 05000219/2021402 & 07200015/2021401 IR 05000219/20214032021-12-21021 December 2021 EA-21-093 Notice of Violation and Proposed Imposition of Civil Penalty - $150,000, Inspection Report No. 05000219/2021403 IR 05000219/20210032021-11-16016 November 2021 NRC Inspection Report No. 05000219/2021003 IR 05000219/20214042021-08-26026 August 2021 NRC Independent Spent Fuel Storage Security Inspection Report No. 07200015/2021402 and Security Decommissioning Inspection Report 05000219/2021404 - (Public) ML21202A2312021-07-28028 July 2021 Discretionary Security Decommissioning Inspection Report No. 05000219/2021403 - Public Version IR 05000219/20210022021-07-27027 July 2021 NRC Inspection Report No. 05000219/2021002 and Independent Spent Fuel Storage Installation Report 07200015/2021002 IR 05000219/20210012021-05-18018 May 2021 NRC Inspection Report No. 05000219/2021001 and Independent Spent Fuel Storage Installation Report 07200015/2021001, Holtec Decommissioning International, LLC, Oyster Creek Nuclear Generating Station IR 05000219/20204022020-12-14014 December 2020 Security Decommissioning Inspection Report 05000219/2020402 (Public - No Findings) IR 05000219/20200032020-10-21021 October 2020 NRC Inspection Report No. 05000219/2020003, Holtec Decommissioning International, LLC, Oyster Creek Nuclear Generating Station, Forked River, New Jersey IR 05000219/20204012020-07-27027 July 2020 Security Baseline Inspection Report 05000219/2020401 IR 05000219/20200022020-07-20020 July 2020 NRC Inspection Report No. 05000219/2020002, Holtec Decommissioning International, LLC, Oyster Creek Nuclear Generating Station, Forked River, New Jersey IR 05000219/20200012020-04-20020 April 2020 Forked River, New Jersey, NRC Inspection Report 05000219/2020001 IR 05000219/20190042020-01-0606 January 2020 NRC Inspection Report 05000219/2019004, Holtec Decommissioning International, LLC, Oyster Creek Nuclear Generating Station, Forked River, New Jersey IR 05000219/20190032019-10-28028 October 2019 NRC Inspection Report No. 05000219/2019003, Holtec Decommissioning International, LLC, Oyster Creek Nuclear Generating Station, Forked River, New Jersey IR 05000219/20190022019-07-24024 July 2019 NRC Inspection Report 05000219/2019002 IR 05000219/20190012019-04-15015 April 2019 NRC Inspection Report No. 05000219/2019001, Oyster Creek Nuclear Generating Station IR 05000219/20194012019-03-25025 March 2019 NRC Inspection Report No. 05000219/2019401 (Public) IR 05000219/20180122019-02-19019 February 2019 NRC Inspection Report No. 05000219/2018012, Oyster Creek Nuclear Generating Station IR 05000219/20180032018-11-0808 November 2018 Integrated Inspection Report 05000219/2018003 IR 05000219/20180022018-08-0202 August 2018 Integrated Inspection Report 05000219/2018002 and Independent Spent Fuel Storage Installation Report 0700015/2018001 IR 05000219/20184102018-06-18018 June 2018 Security Inspection Report 05000219-2018410 (Cover Letter) IR 05000219/20180012018-05-0808 May 2018 Integrated Inspection Report 05000219-2018001 and Exercise of Enforcement Discretion IR 05000219/20170062018-02-28028 February 2018 Annual Assessment Letter for Oyster Creek Nuclear Generating Station (Reports 05000219/2017006 05000219/2017402 and 05000219/2017501) IR 05000219/20180102018-02-28028 February 2018 Design Bases Assurance Inspection (Programs) Report 05000219/2018010 IR 05000219/20170042018-01-24024 January 2018 NRC Integrated Inspection Report 05000219/2017004 IR 05000219/20170092017-11-30030 November 2017 Temporary Instruction 2515-191 Inspection Report 05000219/2017009 IR 05000219/20174052017-10-25025 October 2017 Problem Identification and Resolution Sample Security Inspection Report 05000219/2017405 (Cover Letter) IR 05000219/20170082017-10-17017 October 2017 Supplemental Inspection Report 05000219/2017008 and Assessment Follow-Up Letter IR 05000219/20170032017-10-17017 October 2017 Integrated Inspection Report 05000219/2017003 IR 05000219/20175022017-10-16016 October 2017 Evaluated Emergency Preparedness Exercise Inspection Report 05000219-2017502 IR 05000219/20170052017-08-28028 August 2017 Updated Inspection Plan Report 05000219 2017005 with Report 22 IR 05000219/20174042017-08-15015 August 2017 Problem Identification and Resolution Cyber Security Inspection Report 05000219/2017404 (Cover Letter) IR 05000219/20170022017-08-0303 August 2017 Integrated Inspection Report 05000219/2017002 IR 05000219/20174032017-05-0909 May 2017 Security Inspection Report 05000219-2017403 (Cover Letter) IR 05000219/20170012017-05-0808 May 2017 Integrated Inspection Report 05000219/2017001 IR 05000219/20170072017-05-0101 May 2017 IR 05000219/20160042017-04-13013 April 2017 Final Significance Determination for a White Finding with Assessment Follow-up and Notice of Violation - Inspection Report 05000219/2016004 IR 05000219/20160062017-03-0101 March 2017 Annual Assessment Letter for Oyster Creek Nuclear Generating Station (Report 05000219/2016006) with Report 22 IR 05000219/20164042016-12-22022 December 2016 Material Control and Accounting Program Inspection Report 05000219/2016404 IR 05000219/20160082016-12-14014 December 2016 Problem Identification and Resolution Inspection Report 05000219/2016008 2024-09-05
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Yage I or 3 Print I New Search I Home AR 00546049 Report Aff Fac: Oyster Creek AR Type: CR Status: APPROVED Aff Unit: NA Owed To: ACA PA LL Due Date: 12/01/2006 Aff System: 187 Event Date: 10/19/2006 CR LeveUClass: 3/D Disc Date: 10/19/2006 How Discovered: HO2 Orig Date: 10/19/2006 WWPIMS AR: A2152838 Component #: 187 Action Request Details
Subject:
WATER OBSERVED COMING INTO THE TRENCH I N BAY 5 OF DRYWELL
Description:
Originator: RALPH C LARZO Supv Contacted: SOM, OOM on night shift Condition
Description:
While performing an inspection of the drywell trenches, leakage into the bay 5 trench was observed to be approximately 1 quart per minute. The level in the trench would fill to approx. 5" and stabilize. The source of the leakage is not apparrent.
Immediate actions taken:
OCC was notified and an action plan prepared.
Recommended Actions:
- 1. Issue ACIT to prepare an action plan and evaluate impact of leakage.
2 . Issue AR t o perform the following: a) Test 1-8 sump for leakage by turning of sump pumps, raise level to high level setpoint (using a hose) and monitoring for level decrease. Monitor sump level for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. b)
Attempt to remove water from bay 5 trench until dry and c) I f unable to stop water coming into bay 5 trench, then Chemistry to evaluate use of tracing agent injected into 1-8 sump.
What activities, processes, or procedures were involved?
Drywell inspections Why did the condition happen?
Unknown a t this time What are the consequences?
Leakage could impact drywell Were any procedural requirements impacted?
No Were there any adverse physical conditions?
Unknown until leakage sourse identified.
List of knowledgeable individuals:
Chris Wilson, Howie Ray Repeat or similar condition?
No Operable Basis:
REB - Long term corrosion issue - Drywell is fully operable.
Reportable Basis:
N/A http://cccmvd0 1.ceco.corn:6 123/cap/servlet/ReportARServlet 10/30/2006
SOC Reviewed by: THOMAS A POWELL 10/21/2006 08:21:52 CDT SOC Comments:
10-19-06 REB Close to the PIMS AR.
IR 545422 is closed t o this IR.
Followup to ENG 10/21/06 TAP - Risk and Uncertainty of this condition screen as Medium and Medium. ACE evaluation to Egnineering to determine the source of water and evaluate the physical and regulatory consequences of this condition. PORC review of the ACE is a l R 2 l Restart Requirement.
Close t o PIMS AR and ACE evaluation.
lynamic AR Attributes OUTAGE RELATED: 1R21 ADD 10122 MEV14 rrend Codes TC1 TC2 TC3 Proc Rank EQM MM N ERlOO P
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&sign ments Assign #: 0.1 Assigned To: Status: COMPLETE Aff Fac: Oyster Creek Prim Grp: ACAPALL Due Date: 10/24/2006 Assign Type: TRKG Sec Grp: Orig Due Date: cIcI/cIcI/cIcIcIcI Priority:
Schedule Ref:
Unit Condition:
Subject/Description: WATER OBSERVED COMING INTO THE TRENCH I N BAY 5 OF DRYWELL Assign #: 02
- Assigned To: UOOlFHR Status: NTFY/ASG Aff Fac: Oyster Creek Prim Grp: A5352NESDM Due Date: 11/01/2006 Assign Type: ACIT Sec Grp: Orig Due Date: 11/01/2006 Priority:
Schedule Ref:
Unit Condition:
Subject/Description: Document Tech eval resuts of inleakage to the drywell floor trenches.
Assign #: 03
- Assigned To: Status: NTFY/PRI Aff Fac: Oyster Creek Prim Grp: A5301RAPR Due Date: 11/02/2006 Assign Type: CA Sec Grp: Orig Due Date:
Priority:
Schedule Ref:
Unit Condition:
Subject/Description: Perform PORC review of DW Trench ACE prior to 1R21 restart.
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Assign #: 04
- Assigned To: U999A02 Status: NTFY/PRI Aff Fac: Oyster Creek Prim Grp: A5063NER Due Date: 12/01/2006 Assign Type: ACIT Sec Grp: Orig Due Date: 12/01/2006 Priority:
Schedule Ref:
Unit Condition:
Determine effect on the License Renewal Application Based on the conditions found in the trench Subject/Description: determine the effect of this operating experience on the License Renewal Application and initiate appropriate actions as needed to support the ongoing efforts to renew the operating license.
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