ML052630173
| ML052630173 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 05/03/2004 |
| From: | Barber S NRC Region 1 |
| To: | Marc Ferdas, Mel Gray NRC Region 1 |
| References | |
| FOIA/PA-2004-0314 | |
| Download: ML052630173 (2) | |
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I Fred Power - RE: HC issues I I Fd
,e RPage 1 I From:
Scott Barber 8
To:
Marc Ferdas; Mel Gray Date:
Monday, May 03, 2004 4:36:17 PM
Subject:
RE: HC issues Just to add a different angle to the discussion. We have an alleaation response in which we questioned adequate oil supply in LO bubblers for various HC pumps. Tom Lake's response indicated that 42 bubblers were checked and there were no significant problems. Sounds like the original issue that was raised in the allegation may have more validity than was mentioned in the PSEG response.
Mel --
do you or Marc think we should be highlighting this to them and get them to submit a revised response or is this truly an isolated case?
>>> "Schoppy, Joseph G CDR" <joseph.schoppy~navy.mil> 04/29/04 10:18AM >>>
Thanks for the update. Relative to the H2 issue: yeah, when all was said and done they determined that hydrogen remained below the detonation limit in that pipe. However, all the conditions were present for the phenomenon to occur except for a continuous leakage path or a mechanism to allow hydrogen to accumulate over time. Engineering's subsequent investigation revealed that they did in fact have a leakage path back through the 52B valve to the HPCI drain pot following HPCI depressurization. Based on soundings though, the hydrogen pocket at the high point is not large enough to be of concern. I'm back to repeating my comments from an earlier e-mail: if they had the detonation event (which they were very close to having all the necessary ingredients for) then we would send an SIT or AIT a6nid try to fit to a or red find But because they werelfortaitous (through no action or evaluation of.their own) and hydrogen didnot accumulate to the point of a detonation ri~gger, hen the whole issue is not "more than inor?" Double or noThre's something gravely with ourassessment process. As always the inspector is left hanging out there trying to work within our process to get the licensee to "do the right thing" but God forbid something happens (like a Davis Besse near miss) and everyone wants to know "where was the NRC?"-Who's assessment process is-it anyway?l Bottor line: I'm fine with making it a PI&R sample (a workaroUnd juist t& get'th6 isiue in the report) and not making it a corrective action violation.
Mel - my comments concerning our assessment process were not aimed at you. I feel better for having stated my opinion and am moving on in search of other windmills to battle.
Don Q.
-:Original Message-From: Mel Gray [1]
Sent: Thursday, April 29, 2004 9:09 To: Schoppy, Joseph G CDR
Subject:
Re: HC issues Sorry, I've been swamped with emegent equipment issues here. Your issues not forgotten or discarded.
Quickly., on H2 issue, got some internal NRC pushback that more than minor threshold based on if left uncorrected, could be more significant..." This is time based and looks like, after all said and done with much prodding, would not have h2 potential conflaguration. I proposed to my mgt that we this be PIR sample in this IR since it has much insight into that area. Also some corrective actions still in progress (beleive they fixed HPCI leka a week ago). So Its fair game to keep tracking.
Second, C booster pump. PS?ops saw the light and cut a notification on operator performance in monitoring protected equipment, not just oil leak rrends. There is performance deificiency. I was reviewing more than minor threshold yesterday morning by going to MR a4 violation examples in the OEM Section 8.1.11 (draft still?) for gauidance when it all hit the fan around here. AM pulling PS MR a4
I Fred Bower - RE: FIG issues Page 21 Fre Xoe RE CisusPgq procedures also. Have it on my board as an issue to be pushed through 0612 to see where it falls.
Mel
>>> "Schoppy, Joseph G CDR" <joseph.schoppytnavy.mil> 04/29/04 07:47AM >>>
- Mel, What did you decide about the hydrogen buildup in the SCM piping (1 R12 in report ending 3/31/04)? 1 believe that their engineering folks are expecting at least a corrective action violation.
What do you think about the C spray water pump oil bubbler issue? It's definitely a case of weak PI&R (poor identification of empty bubbler, poor SRO follow-up Oust an N2 for trending, and slow resolution of oil leakage issue) but is it more than minor? This one seems like it could either way (and to think that our process Is purely objective). Glenn likes to use the following measure to break ties for these type of issues: what message are we trying to send, what has their performance been in this area, do they get it?
We've certainly have been beating on operators for lack of attention-to-detail and poor questioning aiftifude in the performance of their rounds (especially for protected equipment). Here's a case where they got a lot a bit closer to adversely impacting operability - do they want to be good or just lucky? Do they get it yet - look at the SRQ!4 response-for-a hint (NRC inspector calls you from the field to inform you that a protected pump has a bone dry oil bubbler and the extent of your actions are to have a NEO add oil ahnd initiate a N2 for trending).
Do you think that they'll ever get back to full power?
Please send response to my NRC e-mail.
Joe CC:
Daniel Holody; Fred Bower; Glenn Meyer; Joseph Schoppy; Lawrence Doerflein; Raymond Lorson; Schoppy, Joseph G CDR