ML051050240

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Event Investigation Personnel Statement, Transformer Breaker Issue Report
ML051050240
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 05/18/2004
From:
Regional Services Corp
To:
Office of Nuclear Reactor Regulation
References
FOIA/PA-2004-0282
Download: ML051050240 (5)


Text

920-755-ES57 REE SERUICES 526 P09

!RY 18 '04 13:22 Event Investization Personnel Statement Event Date: _

1_

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Handwritten statements are acceptable. Include the plant conditions prior to the event, your indications that a problem existed, your action as a result of those indications, noted equipment malfunctions or inadequacies, and any identified procedure deficiencies.

Also, include any information you consider imipbrtant to the review of this event and actions thai may prevent recurrence. Use additional paper as necessary.

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920-755-6857 REG SERU ICES N'iiIst:ir Moiilnlnlt el)llt z~L 0111%,lv 526 P12 MAY' 16 '04 13:23 I-. State Change History Initinto 0

by HEIM, MICHAEL AR Pre-Screen 5/18/2004 5:40:17 AM Owner (None)

I.,

(. Section 1 Activity Request Id:

Activity Type:

x One Line

Description:

4i Detailed

Description:

CAP056776 CAP Submit Date:

5/18/2004 5:40:17 AM 1X-04 Annuncitor Alarm Activated by DS2A Selector Switch Operation 511812004 5:40:17 AM - HEIM, MICHAEL:

On 5/1 7/2004 at approximately 2345, Power Selector Switch D52A was manipulated by a 1Mechanic Electrician (ME)-during the performance of breaker maintenance.

While performing PM breaker maintenance on H52-20 under W0ft0301793, a ME manipulated Power Selector Switch D52A, in an attempt to energize a breaker test stand. The manipulation of DS2A resulted in momentarily de-energizing power panel D52 which provides DC control power to 13.8kV equipment.

The Control Room received ai annunciator alarm indicating a lockout actuation associated with the 1 X-04 transformer. Operations paged Maintenance to begin determining the potential cause of the annunciator.

In progress testing on the Train B undervoltage relay testing was place on hold pending investigation. Maintenance craft working on troubleshooting D-08 were questioned and maintenance craft working on the H52-20 breaker in the 13.8kV were questioned by Operations.

Maintenance Supervision determined the cause of the Control Room indication to be a result of the switch manipulation.

Maintenance Supervision notified Operations.

A Human Performance Event Investigation was initiated by Maintenance.

HEIM, MICHAEL 0 Initiator Department:

PME PS Maintenance AL>J Electrical PB D initiator:

Date/Time of Discovery:

Identified By:

Equipment # (1st):

EquIpment Y (2nd):

Equipment # (3rd):

SltefUnit:

5118/2004 5:06:45 AM Site-identllied D-52 PS B (None)

(None)

Point Beach-Common Date/Time of Occurrence:

5/1812004 5:06:45 AM System:

Equipment Type (1st):

Equipment Type (2nd):

Equipment Type (3rd):

125VDC PB (None)

(None)

(None)

Why did this occur?:

511 8/2004 5:40:17 AM - HEIM, MICHAEL:

The Mechanic Electrician believed the switch provided power to the breaker test stand.

Immediate Action Taken: 5/1812004 5:40:17 AM - HEIM, MICHAEL:

The control room paged Electrical Maintenance to determine the potential cause of a control room annunciator Indicating a lockout on the 1X-04 transformer.

In progress testing on the Train B undervoltage relay testing was place on hold pending investigation. Maintenance craft working on troubleshooting D-08 were questioned and maintenance craft working on the H52-20 breaker in the 13.8kV were questioned by Operations.

Maintenance Supervision determined the cause of the Control Room indication to be a result of the switch manipulation.

Maintenance Supervision notified Operations.

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5/18/2004

920-755-6657 RES SERU ICES Nuvivai N

ni:wIllIIC1II I. CItJM1.arly 526 P13 M1RY 18 '04 13:24 I

Recommendations:

0) Notify Me During Eval?:

E Sectlon 2 A Human Performance Event Investigation was initiated by Maintenance.

5/18/2004 5:40:17 AM-HEIM, MICHAEL:

Complete the Human Performance Event Investigation as appropriate.

N d SRO Review Required?:

iN Operability Status:

(None) i3 Compensatory Actions: r Basis for Operabillty:

i Unplanned TSAC Entry: N h External Notification:

t W Section 3 Scieened?:

- N iD Significance Level: (None)

INPO OE Reqd?:

N Potential MRFF?:

N 4; OA/Nuclear Oversight?: N 4J Licensing Review?; N Good Calch/Well Doc'd?: NA "1 Section 4 q

N Inappropriate Action:

Process:

(None)

Activity:

(None)

Human ErrorType:

(None)

Human Pert Fall Mode: (None)

Equip Failure Mode:

(None)

Process Fall Mode:

(None)

Org/Mgt Failure Mode: (None) 4 Group Causing Prob:

(None)

Hot Buttons:

(None)

LF-Sectlon S

-CAP Admin:

PBNP-CAP Adminr C

Pres 4 Project:

Corrective Actn Program (CAP) AR id Siat i Active/inactive:

Active i5 Sub 0 Owner:

(None)

, LasI f; Last Modifier:

HEIM. MICHAEL 6j

£ Lasl e Last Stale Changer:

HEIM. MICHAEL L CIoD NUTRK ID:

H of Children:

D

References:

Update:

Prescreen Comments:

Import Memo Field:

OPR Completed?:

N OLDACTION-NUM:

sub-tsid:

0 orig original_lssue_;d:

Site; Point Beach Cartridge and Frame:

creener

(None) e:

- AR Pre-Screen mitter:

HEIM, MICHAEL 0

Modified Date

5/1812004 5:40:17 AM t State Change Date: 5118/2004 5:40:17 AM to Date:

Inal-project-id:

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5/18/2004