ML043230499

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G20040700/LTR-04-0644 - David Lochbaum Ltr. Re. Questioning, Not Appealing, the Directors Decision on the Riverkeeper and Union of Concerned Scientists Indian Point Containment Sump 2.206 Petition
ML043230499
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 12/21/2004
From: Lyons J
NRC/NRR/DLPM
To: Lochbaum D
Union of Concerned Scientists
Milano P, NRR/DLPM , 415-1457
Shared Package
ML043230512 List:
References
2.206, G20040700, LTR-04-0644, TAC MC4750, TAC MC4751
Download: ML043230499 (11)


Text

December 21, 2004 Mr. David Lochbaum Nuclear Safety Engineer Union of Concerned Scientists 1707 H Street, NW.

Suite 600 Washington, DC 20006-3919

Dear Mr. Lochbaum:

On behalf of the Nuclear Regulatory Commission (NRC), I am responding to your letter dated October 8, 2004, commenting on the June 18, 2004, Decision by the Director of the Office of Nuclear Reactor Regulation (Directors Decision). The Directors Decision was prepared in response to the Petition, pursuant to Section 2.206 of Title 10 of the Code of Federal Regulations (10 CFR 2.206), filed by you and Mr. A. Matthiessen of Riverkeeper, Inc., on September 8, 2003, regarding the emergency core cooling system (ECCS) recirculation sumps at Indian Point Nuclear Generating Unit Nos. 2 and 3 (Indian Point).

In your letter, you stated that you provided these comments because the NRC does not have a process that allows appealing a Directors Decision. You are correct in that the 10 CFR 2.206 review process does not include a means to appeal the final decision, although the process includes an opportunity for the petitioner to comment on the proposed decision. As you are aware, the Commission, at its discretion, may determine to review the Directors Decision within 25 days of the date of the decision and may direct the staff to take some other action than that in the decision. However, the Commission did not review the decision in response to your Petition.

Notwithstanding the unavailability of an appeal of Directors Decisions, the NRC staff has reviewed the comments presented in your letter, and the staffs responses to these comments are enclosed. You concluded your letter by stating that the NRC should not delay resolving the sump clogging issue for all pressurized-water reactors (PWRs), nor should we allow any schedule milestones to be delayed. The staff agrees with you and I can assure you that the staff is working diligently to complete the implementation of a resolution to this issue in all operating PWRs by December 2007.

Please feel free to contact me if you have any other questions regarding this matter.

Sincerely,

/RA/

James E. Lyons, Deputy Director Division of Licensing Project Management Office of Nuclear Reactor Regulation

Enclosure:

As stated

December 21, 2004 Mr. David Lochbaum Nuclear Safety Engineer Union of Concerned Scientists 1707 H Street, NW.

Suite 600 Washington, DC 20006-3919

Dear Mr. Lochbaum:

On behalf of the Nuclear Regulatory Commission (NRC), I am responding to your letter dated October 8, 2004, commenting on the June 18, 2004, Decision by the Director of the Office of Nuclear Reactor Regulation (Directors Decision). The Directors Decision was prepared in response to the Petition, pursuant to Section 2.206 of Title 10 of the Code of Federal Regulations (10 CFR 2.206), filed by you and Mr. A. Matthiessen of Riverkeeper, Inc., on September 8, 2003, regarding the emergency core cooling system (ECCS) recirculation sumps at Indian Point Nuclear Generating Unit Nos. 2 and 3 (Indian Point).

In your letter, you stated that you provided these comments because the NRC does not have a process that allows appealing a Directors Decision. You are correct in that the 10 CFR 2.206 review process does not include a means to appeal the final decision, although the process includes an opportunity for the petitioner to comment on the proposed decision. As you are aware, the Commission, at its discretion, may determine to review the Directors Decision within 25 days of the date of the decision and may direct the staff to take some other action than that in the decision. However, the Commission did not review the decision in response to your Petition.

Notwithstanding the unavailability of an appeal of Directors Decisions, the NRC staff has reviewed the comments presented in your letter, and the staffs responses to these comments are enclosed. You concluded your letter by stating that the NRC should not delay resolving the sump clogging issue for all pressurized-water reactors (PWRs), nor should we allow any schedule milestones to be delayed. The staff agrees with you and I can assure you that the staff is working diligently to complete the implementation of a resolution to this issue in all operating PWRs by December 2007.

Please feel free to contact me if you have any other questions regarding this matter.

Sincerely,

/RA/

James E. Lyons, Deputy Director Division of Licensing Project Management Office of Nuclear Reactor Regulation

Enclosure:

As stated Accession No.: ML043230499 Incoming: ML042920083 Package: ML043230512 OFFICE PDI-1/PM PDI-1/LA PDI-1/SC DSSA/DD DRP/RI NRR/PRB OGC NAME PMilano SLittle RLaufer MJohnson BHolian HBerkow SLewis DATE 12/20/04 12/20/04 11/23/04 11/19/04 11/30/04 11/23/04 12/09/04 OFFICE PDI/D DLPM/D ADPT/NRR DLPM/D NAME CHolden TMarsh BSheron JLyons DATE 12/08/04 12/08/04 12/20/04 12/21/04 OFFICIAL RECORD COPY

DISTRIBUTION: G20040700/LTR-04-0644, Letter to D. Lochbaum, Union of Concerned Scientists, dated December 21, 2004, in response to his letter of October 8, 2004 PUBLIC PDI-1 Reading EDO EDO Reading File L. Reyes W. Kane M. Virgilio P. Norry E. Merschoff W. Dean K. Cyr/S. Burns J. Dyer/R. Borchardt B. Sheron S. Collins, R-I L. Marsh/J. Lyons S. Black M. Johnson C. Holden H. Berkow J. Hannon R. Laufer P. Milano S. Little D. Solorio G. Matakas, R-I B. McDermott, R-I D. Skay S. Lewis, OGC OPA OCA NRR Mail Room L. Cox

Enclosure RESPONSE TO COMMENTS FROM UNION OF CONCERNED SCIENTISTS REGARDING THE JUNE 18, 2004, DIRECTORS DECISION CONCERNING EMERGENCY CORE COOLING SYSTEM SUMPS AT INDIAN POINT NUCLEAR GENERATING UNIT NOS. 2 AND 3 (IP2 AND 3)

The comments presented in the October 8, 2004, letter from the Union of Concerned Scientists (UCS) and the Nuclear Regulatory Commission (NRC) staff responses are as follows:

Comment 1:

In its October 8, 2004, letter, UCS indicated that the Directors Decision stated that the Petition was denied because there is currently no basis to conclude that IP2 and 3 are operating unsafely. The staff noted that there are sources of safety margin in plant design, compensatory measures were taken to mitigate potential risks associated with the issue, and the occurrence of any accident, especially one that could potentially challenge the sump, is very unlikely.

Regarding the sources of safety margin in plant design, UCS referred to the results from an inspection conducted at Indian Point from April 1 to June 30, 2004, that cited Entergy for violating the containment sump design basis. UCS noted that the inspection report stated that the inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for Entergys failure to translate the emergency core cooling system (ECCS) design basis into recirculation sump modification instructions. Specifically, Entergy added penetration cover plates and alignment collars around several small pipes that penetrated the sump deck plating, and the annular gap between the collars and pipes exceeded the sump screen size. This finding is more than minor because it potentially affected the mitigating systems cornerstone objective of assuring the availability, reliability, and capability of ECCS.

Based on this information, UCS concludes that the NRC staff knew, or should have known, that Entergy had not taken actions required by Federal regulations to mitigate the known risks associated with the issue when the staff denied the Petition.

Staff Response:

On February 19, 2004, the NRC staff forwarded the proposed Directors Decision to the Petitioners for comment. The final Directors Decision was issued on June 18, 2004.

On March 30, 2004, the Petitioners provided their comments on the proposed Directors Decision. Consistent with the agencys Petition review process (as described in Management Directive 8.11), the Petitioners comments were dispositioned, and the final Directors Decision was issued on June 18, 2004. The inspection report referenced by UCS was issued on August 11, 2004, and as noted in the letter transmitting it to the licensee, the results were discussed with the licensee on July 22, 2004. The NRC staff reviewing the Petition were not aware of the findings at the time the Decision was issued. However, the inspection finding would not have significantly changed the final Directors Decision because, as stated in the inspection report cited by UCS, [t]his finding is considered to be of very low safety significance because there was no loss of safety function. The NRC staff further concluded that the finding was of very low safety significance (Green) by the SDP Phase 1 screening worksheet for Mitigating Systems because the containment sump screen qualification deficiency was evaluated in accordance with NRC Generic Letter 91-18 (CR-IP2-2004-1948) and was confirmed not to result in a loss of the long-term heat removal function. Additionally, the licensee took appropriate corrective action to resolve the finding. In summary, this finding was appropriately evaluated under the Reactor Oversight Program and would not have significantly changed the Directors Decision if it had been referenced.

The NRC staff further notes that, while it is true that compliance with all NRC regulations provides reasonable assurance of adequate protection of the public health and safety, the converse is not correct. Failure to fully comply with a regulation is not an indication of the absence of adequate protection, at least in a situation where the Commission has reviewed the noncompliance and found that it does not pose an undue risk to the public health and safety.

As discussed above, the inspection finding was of a very low safety significance, and thus, it does not pose an undue risk to the health and safety of the public.

Comment 2:

The NRC did not know whether compensatory measures suggested in NRC Bulletin 2003-01 or recommended by the Westinghouse Owners Group (WOG) had been taken by Entergy when it denied the Petition.

Staff Response:

The comment presented by UCS regarding NRC staff performance has been forwarded to the NRCs Office of the Inspector General (OIG).

The NRC staff did not deny the Petition based on one reason (i.e., compensatory measures) or despite the fact it lacked the knowledge as to whether the measures had been taken. Rather, there was a combination of reasons for denying the Petition. As noted in the Directors Decision, the staff disagreed with the technical basis provided by the Petitioners in the Petition.

In the Directors Decision, the staff also pointed out the actions taken by the licensee, prior to the Bulletins issuance, that provide significant risk reduction benefit when considered in lieu of the compensatory measures requested in the Bulletin. The actions requested by the staff in Bulletin 2003-01 do not solely constitute the staffs basis for denying the Petition or for allowing PWR licensees to continue operating while the staff resolves Generic Safety Issue (GSI) 191.

The Bulletin measures are prudent measures intended to enhance safety (i.e., enhance each plants defense-in-depth) and heighten licensee awareness of the issue. The Bulletin also informed licensees that, in addition to the measures in the Bulletin, licensees may also consider plant-specific compensatory measures.

It is true that NRC staff followup on the Bulletin responses was not complete at the time of issuance of the final Directors Decision. However, the staff did review the licensees response to NRC Bulletin 2003-01 prior to issuing the Directors Decision and found it to contain existing plant features and operator training which the staff believes greatly reduces the risk from sump clogging at IP2 and 3.

Of the measures requested in the Bulletin for consideration by licensees, the NRC staff believes the greatest risk reduction benefit is achieved by ensuring that alternative water sources are available, and that operators are trained in the use of alternate water sources.

Entergys response to the Bulletin stated that each of the Indian Point units has an additional containment sump that is separate from the recirculation sumps. The containment sumps do not utilize the recirculation pumps and are physically separate in the containment (by 90 degrees). As such, these sumps serve as an alternate water source. In addition, existing operator training already includes the conditions and procedures for use of the separate containment sump as an alternate water source and for monitoring of erratic recirculation pump flow that could be symptomatic of sump clogging. Furthermore, in its response to the Petition, the licensee identified actions taken before the issuance of the Bulletin that provided a substantial risk reduction benefit. Specifically, the licensee stated that it had removed most of the calcium silicate insulation from containment and made modifications to the low pressure ECCS to improve their available net positive suction head. Based on this information, the NRC staff concluded that, although the staffs review of the licensees response to the Bulletin is still ongoing, the licensees actions combined with their existing design information were sufficient to demonstrate that a significant risk reduction had already been achieved.

Comment 3:

UCS was told during a telephone conversation with the NRC staff that the staff deliberately waited until after denying our Petition before they evaluated Entergys response.

Staff Response:

The UCS comment regarding NRC staff performance has been forwarded to the OIG.

The NRC staff did not deliberately wait until after denying your Petition before evaluating the licensees response. Moreover, the Petition was not a factor in the Bulletin review schedule.

Pursuant to the 10 CFR 2.206 process, the NRC placed a high priority on the completion of the staffs evaluation of the Petition. It is not uncommon for the staff to review all of the responses to a generic communication before issuing requests for additional information (RAIs) because the staff may identify concerns in one licensees response that may raise questions about other responses. In this case, the staff reviewed all of the Bulletin 2003-01 responses, and the proposed measures identified by the WOG, before issuing the RAIs to licensees. There were some delays in the review schedule to give the WOG time to develop its suggested compensatory measures, receive utility review and comment on the suggested measures, and resolve utility comments. The staffs original schedule for Bulletin responses did not account for the WOGs effort. However, many licensee responses to the Bulletin indicated that they would not finalize their planned compensatory measures until they saw the WOGs report. These were the factors affecting the NRC staffs review of the Bulletin responses. Since the Petition focused on requested actions directed at the operation of a specific facility, the NRC treated the Petition with a high priority and appropriately set a schedule for staff review that was independent of the Bulletin and in advance of the final resolution.

Comment 4:

When the NRC finally got around to the Entergy response, they found it incomplete. By letter dated September 30, 2004, the NRC staff requested additional information (RAI) from Entergy about their response to Bulletin 2003-01.

Staff Response:

The NRC staff did review the licensees response to Bulletin 2003-01 for IP2 and 3 prior to issuing its proposed Directors Decision and found that the licensee had (a) already taken significant measures to reduce the risk of sump clogging and (b) had plant-specific capabilities that reduced the risk associated with potential sump clogging. These measures were discussed in the Directors Decision (see response to Comment 2 above). The staff notes that it is a common practice for the staff to request a further clarification of a licensees response by an RAI on measures to be implemented in response to a generic communication. The staffs RAI does not necessarily mean that the licensees response to the Bulletins requested actions is inadequate. The staff routinely requests additional information to ensure that its understanding of licensee actions is complete and to verify implementation of the requested actions by the licensee.

Comment 5:

Point: The NRC staff does not yet know if Entergys operating training is sufficient, but gave full credit for operator training when denying our petition.

Staff Response:

As noted in the staffs response to Comments 2 and 4 above, the NRC staff was aware that the licensee had existing procedures and operator training that included the ability to use the separate containment sump. The staff only requested clarification in its RAI regarding the licensees Bulletin response.

Comment 6:

Point: Based on materials received from Entergy before we even submitted our petition, the NRC suspects that Entergys operator training is incomplete and/or deficient, but gave full credit when denying our petition.

Staff Response:

As noted in the response to Comment 4 above, the NRC staff requested clarification from the licensee regarding operator actions and training. The fact that the staff requested this information did not mean that the staff found the training deficient. Moreover, as previously stated, the staff decision to deny your Petition was based on numerous factors that gave the staff confidence that the plant could continue to operate safely and was not based on any one factor.

Comment 7:

The NRC staff does not yet know if Entergy implemented any of the recommended changes to the Emergency Operating Procedures, but gave full credit for all when denying our petition.

Comment 8:

The NRC staff does not know if Entergys justification for not adopting recommended compensatory measures is valid, but gave full credit when denying our petition.

Staff Response to Comments 7 and 8:

As with any generic communication from the NRC, licensees can propose alternative ways to accomplish the goals of the requested actions (in this case, to reduce the risk associated with the potential for sump clogging). As pointed out in the Directors Decision, the licensee for IP2 and 3 had already taken significant steps to reduce the risk for the plants before the NRC issued Bulletin 2003-01. Further, the licensee had existing plant design features and operator training in place to provide an alternate water source in addition to the ECCS recirculation sump. Licensees do not necessarily have to implement all of the requested actions in the Bulletin in order to provide an adequate Bulletin response.

Comment 9:

The NRC staff does not know what nature, scope, or timing of compensatory measures, but did not let that lack of knowledge prevent them from giving full credit for compensatory measures when denying our petition.

Staff Response:

As stated in the responses to Comments 2, 7, and 8 above, there were a number of reasons presented by the staff in its Directors Decision. In this regard, the staff found that it had sufficient information to conclude that the actions requested by the Petitioners were not necessary.

Comment 10:

The NRC staff had EntergysBulletin 2003-01 response dated August 7, 2003, before we submitted our petition dated September 8, 2003, and throughout their entire deliberations on our petition. Yet the NRC staff intentionally waited until after denying our petition before reviewing Entergys response about compensatory measures. [...] Had the NRC staff processed Entergys August 7, 2003, response in a timely manner, they would have been unable to rely on compensatory measures in the Directors Decision.

Staff Response:

As noted in the response to Comment 3, the UCS comments about staff performance have been referred to the OIG.

In Comment 3, the NRC staff stated that the timing of the its RAI was not directly tied to the staffs response to the Petition. Furthermore, as discussed in the responses to Comments 2 and 4, the staff had a strong basis on which to determine that IP2 and 3 already had:

(1) procedures in place, (2) the availability of alternate water sources, and (3) taken sufficient measures to reduce the risk of sump clogging (e.g., removing calcium silicate insulation from containment). The staff believes that these measures demonstrate that the licensee has already made a significant reduction in the risk associated with sump clogging. The staff will continue its followup, however, in order to see if there are additional measures that may be taken to further reduce risk.

Comment 11:

The NRC staff behaved disturbingly similar to how it misbehaved in the Davis-Besse debacle.

In November 2001, the NRC staff decided not to issue an order requiring FirstEnergy to shut down the Davis-Besse reactor in Ohio for safety inspections based largely on compensatory measures promised by the company. When the NRC staff examined the merits of the compensatory measures after the decision had been made, they judged them to have no safety value. [...] The NRC staff must evaluate the merits of compensatory measures BEFORE making regulatory decisions relying upon them.

Staff Response:

The comments presented by UCS regarding NRC staff performance have been forwarded to the NRCs Office of the Inspector General (OIG).

Regarding the assertion that the NRC staff must evaluate the merits of compensatory measures before making regulatory decisions, the staff agrees. As discussed above, and in the Directors Decision, this aspect was adequately addressed during the staffs consideration of the requested actions and supporting basis in the Petition. The Petitioners failed to provide a sufficient technical basis for concluding that operation of IP2 and 3 presented an undue risk to public health and safety. In fact, the staff pointed out in the Directors Decision numerous reasons why the Petitioners technical basis was erroneous and had not provided an adequate foundation for any conclusion about the adequacy of the Indian Point sump design. In addition, the staff pointed out plant-specific design features such as the additional containment sump that reduced the risk at IP2 and 3. The staff also pointed out that the licensee had taken additional measures before the issuance of Bulletin 2003-01 that helped reduce the risk (i.e., removal of calcium silicate, pump modifications to upgrade the net positive suction head available on the low pressure ECCS pumps). The staff believes that the actions already taken by the licensee provided a significant risk benefit. Additional measures implemented by the licensee in response to Bulletin 2003-01 will provide further risk benefit.

Regarding the comments on the staffs review of the Davis-Besse reactor pressure vessel head penetration nozzle inspection schedule, UCS continues to mischaracterize the staffs review decision as being... based largely on compensatory measures... and that the measures were subsequently found to have no safety value. The staff did consider and credit the compensatory measures in its decision; however, the staff clearly stated that its decision was based on the entire amount of information available to it. Unfortunately as has been previously noted in other correspondence, the NRC staff did not include its evaluation, which would have 1LA-UR-01-4083 was later published as NUREG/CR-6762 better explained its decision with its letter dated December 4, 2001, to the Davis-Besse licensee concerning the inspection schedule.

Comment 12:

In developing our petition, we relied on information about PWR containment sump vulnerabilities in a parametric study documented by the Los Alamos National Laboratory (LANL) and issued by the NRC as NUREG/CR-6771. The Directors Decision took us to task for using this outdated LANL information: [...] So, the NRC staff criticized us in June 2004 because we had used the risk information from superceded NUREG/CR-6771 in our September 2003 petition. We find it extremely curious, then, that the NRC staff used the risk information from NUREG/CR-6771 - not - from LA-UR-02-7562 - in its September 2004 Regulatory Analysis (RA) for Bulletin 2004-02.

Staff Response:

In September 2001, the NRCs Office of Nuclear Regulatory Research (RES) conducted a cost-benefit analysis for GSI 191 as part of the Technical Assessment phase of the NRCs Generic Issue Process (as described in Management Directive 6.4 Generic Issues Program).

To perform the analysis, RES utilized risk information from LANL Report LA-UR-01-4083,1 GSI-191: Parametric Evaluations for Pressurized Water Reactor Recirculation Sump Performance, and adjusted the data to account for operator action. RES used the revised data to estimate cost-benefit associated with resolving GSI-191. It should be noted that RES performed their cost-estimate before LANL had completed its work on LA-UR-02-7562. In order to perform a cost-benefit analysis, the number of plants that might need to make a modification is estimated. To make this estimate, RES made a generic estimate based on the information contained in LA-UR-01-4083. RES did not make any conclusions about any specific plants. Instead RES simply estimated a range for the number of plants that might make modifications.

Cost-benefit analyses are typically performed to better inform and support NRCs generic communication process. As such, when Generic Letter 2004-02 was prepared for issuance, the cost-benefit analysis performed in 2001 was simply updated to bring the costs in line with current cost information.

Comment 13:

What is relevant is that the NRC staff already had detailed analysis or valid assessment in hand and opted to overlook this information when crafting their Directors Decision.

NRC inspectors at Indian Point between April 1st and June 30th 2004 identified that (a) Entergy was operating Indian Point outside the design basis for the containment sumps, and (b) Entergy violated federal regulations by failing to prevent debris from residing in containment and even on the containment sump screens.

NRC staff had received Entergys response dated August 7, 2003, to Bulletin 2003-01 that failed to adequately address operator training and compensatory measures.

[...] NRC senior management seems pre-disposed to reject any assertion that nuclear plants might be unsafe regardless of information to the contrary.

Staff Response:

Regarding the UCS assertion that NRC senior management seems pre-disposed to reject any assertion that nuclear plants might be unsafe, the comment has been forwarded to OIG. As noted in previous responses, the UCS assertions about staff performance were also forwarded to the OIG. The UCS concluding statement about the findings in the NRC inspection report and its assertion that Entergys response failed to adequately address operator training and compensatory measures in Bulletin 2003-01 were answered in response to the earlier UCS comments discussed above.