|
---|
Category:Letter
MONTHYEARIR 05000336/20240032024-11-0707 November 2024 Integrated Inspection Report 05000336/2024003 and 05000423/2024003 and Apparent Violation and Independent Spent Fuel Storage Installation Inspection Report 07200008/2024001 IR 05000318/20240072024-11-0606 November 2024 Assessment Follow-Up Letter for Calvert Cliffs Nuclear Power Plant, Unit 2 (Report 05000318/2024007) IR 05000317/20240032024-10-22022 October 2024 Integrated Inspection Report 05000317/2024003, 05000318/2024003, and Independent Spent Fuel Storage Installation Report 07200008/2024001 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24283A0012024-10-0909 October 2024 Senior Reactor and Reactor Operator Initial License Examinations IR 05000317/20245012024-10-0707 October 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000317/2024501 and 05000318/2024501 ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000317/20240052024-08-29029 August 2024 Updated Inspection Plan for Calvert Cliffs Nuclear Power Plant, Units 1 and 2 (Report 05000317/2024005 and 05000318/2024005) ML24240A2462024-08-27027 August 2024 Submittal of the Reactor Vessel Material Surveillance Program Capsule Technical Report ML24240A1112024-08-27027 August 2024 Registration of Use of Casks to Store Spent Fuel ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition IR 05000317/20240022024-08-0606 August 2024 Integrated Inspection Report 05000317/2024002 and 05000318/2024002 IR 05000317/20240102024-07-31031 July 2024 Age-Related Degradation Inspection Report 05000317/2024010 and 05000318/2024010 ML24179A3262024-07-23023 July 2024 LTR - Constellation - SG Welds and Nozzles (L-2023-LLR-0053, L-2023-LLR-0054, L-2023-LLR-0055, L-2023-LLR-0056) ML24198A0442024-07-16016 July 2024 Inservice Inspection Report IR 05000317/20244012024-07-0909 July 2024 Security Baseline Inspection Report 05000317/2024401 and 05000318/2024401 ML24177A1832024-06-25025 June 2024 Inservice Inspection Report RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24161A0012024-06-0909 June 2024 Independent Spent Fuel Storage Installation, Annual Radioactive Effluent Release Report ML24150A0522024-05-29029 May 2024 Operator Licensing Examination Approval ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 ML24136A1962024-05-15015 May 2024 Independent Spent Fuel Storage Installation - Annual Radiological Environmental Operating Report IR 05000317/20240012024-05-0707 May 2024 Integrated Inspection Report 05000317/2024001 and 05000318/2024001 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests 05000317/LER-2024-002, Emergency Diesel Generators Automatic Start Due to Loss of a 13kV Bus2024-04-29029 April 2024 Emergency Diesel Generators Automatic Start Due to Loss of a 13kV Bus 05000318/LER-2024-001, Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip2024-04-24024 April 2024 Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip ML24101A1942024-04-22022 April 2024 Closeout Letter for GL 2004-02 ML24114A0182024-04-18018 April 2024 Electronic Reporting of Occupational Exposure Reporting 05000318/LER-2023-004-01, Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer2024-04-12012 April 2024 Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition IR 05000317/20240402024-04-11011 April 2024 95001 Supplemental Inspection Report 05000317/2024040 and Follow-Up Assessment Letter RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report ML24082A0082024-03-22022 March 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 ML24078A1152024-03-18018 March 2024 10 CFR 50.46 Annual Report ML24059A0632024-03-15015 March 2024 Authorization and Safety Evaluation for Alternative Request ISI-05-021 (EPID L-2023-LLR-0006) - Non-Proprietary IR 05000317/20230062024-02-28028 February 2024 Annual Assessment Letter for Calvert Cliffs Nuclear Power Plant, Units 1 and 2, (Reports 05000317/2023006 and 05000318/2023006 ML24052A0072024-02-14014 February 2024 Core Operating Limits Report for Unit 1, Cycle 27, Revision 0 ML24040A0962024-02-0909 February 2024 Notification of Readiness for NRC 95001 Inspection ML24040A1492024-02-0909 February 2024 Response to NRC Request for Additional Information Regarding Final Response to Generic Letter 2004-02 IR 05000317/20230042024-02-0101 February 2024 Integrated Inspection Report 05000317/2023004 and 05000318/2023004 ML24029A0102024-01-29029 January 2024 Request for Information and Notification of Conduct of IP 71111.21.N.04, Age-Related Degradation, Reference Inspection Report 05000317/2024010 and 05000318/2024010 ML24003A8872024-01-19019 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0033 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML24011A0732024-01-11011 January 2024 Proposed Alternative to the Requirements for Repair/Replacement of Saltwater (SW) System Buried Piping 05000318/LER-2023-003, Forward LER 2023-003-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Manual Actuation of Auxiliary Feedwater System Due to 22 Steam Generator Feedwater Pump Trip2024-01-0808 January 2024 Forward LER 2023-003-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Manual Actuation of Auxiliary Feedwater System Due to 22 Steam Generator Feedwater Pump Trip ML24005A0222024-01-0505 January 2024 Revised Steam Generator Tube Inspection Reports ML23304A0642024-01-0202 January 2024 Issuance of Amendment No. 349 to Modify the Long-Term Coupon Surveillance Program RS-23-125, Request for Exemption from 10 CFR 2.109(b)2023-12-0707 December 2023 Request for Exemption from 10 CFR 2.109(b) ML23331A2992023-11-27027 November 2023 Submittal of Condition Prohibited by Technical Specifications Due to Failure to Sample Diesel Generator Fuel Oil Storage Tank IR 05000317/20230102023-11-20020 November 2023 Biennial Problem Identification and Resolution Inspection Report 05000317/2023010 and 05000318/2023010 2024-09-06
[Table view] Category:Licensee 30-Day Written Event Report
MONTHYEARML19045A2422019-02-13013 February 2019 Reactor Vessel Level Monitoring System Special Report ML14114A5462014-04-23023 April 2014 CFR 50.46 30-day Report for Changes to the Emergency Core Cooling System Performance Analysis ML14080A3072014-03-20020 March 2014 10 CFR 50.46 30-day Report and Annual Report for Changes to the Emergency Core Cooling System Performance Analysis ML13115A2792013-04-22022 April 2013 10 CFR 50.46 30-day Report and Annual Report for Changes to the Emergency Core Cooling System Performance Analysis ML1212203062012-04-30030 April 2012 CFR 50.46 30-day Report and Annual Report for Changes to the Emergency Core Cooling System Performance Analysis ML12094A1002012-03-29029 March 2012 Submittal of Containment Water Level Indication Special Report ML12024A3912012-01-19019 January 2012 CFR 50.46 30-day Report for Changes to the Emergency Core Cooling System Performance Analysis ML1006105262010-02-22022 February 2010 LER Calvert Cliffs, Special Report: Noncompliance with Effluent Limitations ML0818206982008-06-30030 June 2008 Containment Tendon Surveillance - 30 Day Report ML0510200112005-04-0606 April 2005 10 CFR 50.46 30-Day Report for Changes to the Plant Emergency Core Cooling System Performance Analysis ML0424501002004-08-25025 August 2004 Units I & 2 - Special Report: National Pollutant Discharge Elimination System Discharge Permit 02-DP-01 87 2019-02-13
[Table view] Category:Written Event Report (30 or 60 day)
MONTHYEARML21022A4192021-01-22022 January 2021 Reactor Vessel Level Monitoring System and Wide Range Pressurizer Pressure System Special Report ML0510200112005-04-0606 April 2005 10 CFR 50.46 30-Day Report for Changes to the Plant Emergency Core Cooling System Performance Analysis ML0424501002004-08-25025 August 2004 Units I & 2 - Special Report: National Pollutant Discharge Elimination System Discharge Permit 02-DP-01 87 2021-01-22
[Table view] |
Text
4 X Kevin J. Nietmann 1650 Calvert Cliffs Parkway Plant General Manager Lusby, Maryland 20657 Calvert Cliffs Nuclear Power Plant 410 495-4101 Constellation Generation Group, LLC 410 495-4787 Fax Constellation Energy Group August 25, 2004 U. S. Nuclear Regulatory Commission Washington, DC 20555 ATTENTION: Document Control Desk
SUBJECT:
Calvert Cliffs Nuclear Power Plant Unit Nos. I & 2; Docket Nos. 50-317 & 50-318 Special Report: National Pollutant Discharge Elimination System Discharge Permit 02-DP-01 87 Calvert Cliffs Nuclear Power Plant
REFERENCE:
(a) Calvert Cliffs Nuclear Power Plant, Appendix B, Environmental Protection Plan (Non-Radiological) Technical Specifications, Section 3.2.1 In accordance with Reference (a), Attachment (1), provides a copy of a Calvert Cliffs Nuclear Power Plant Report to the Maryland Department of the Environment. This report documents the discovery of a lack of monitoring for the auxiliary boiler blowdown effluent (monitoring point 103 A) between June 1, 2004, when the permit requirement became effective, and July 30, 2004, when the lack of monitoring was discovered.
The cause of the unanticipated discharge was determined to be an incorrect pump line-up (automatic vs.
manual). Revisions to site procedures will ensure compliance with the applicable monitoring frequency and analysis type.
Should you have questions regarding this matter, we will be pleased to discuss them with you.
Very truly yours for Kevin J. Nietmann Plant General Manager KJN/JTJ/bjd
Attachment:
Letter to Maryland Department of the Environment, dated August 4, 2004, NPDES Discharge Permit 02-DP-0187, Calvert Cliffs Nuclear Power Plant cc: J. Petro, Esquire S. J. Collins, NRC J. E. Silberg, Esquire Resident Inspector, NRC R. V. Guzman, NRC R. l. McLean, DNR I-,--
-1 e 2-.S-
ATTACHMENT (1)
Letter to Maryland Department of the Environment, dated August 4, 2004, NPDES Discharge Permit 02-DP-0187, Calvert Cliffs Nuclear Power Plant Calvert Cliffs Nuclear Power Plant, Inc.
August 25, 2004
1650 Calvert Cliffs Parkway Lusby, Maryland 20657 Constellation Calvert Cliffs Nuclear Power Plant A Member of the Constellation Energy Group August 4, 2004 Mr. Jack Bowen Maryland Department of the Environment Water Management Administration 1800 Washington Boulevard Baltimore, Maryland 21230 RE: NPDES Discharge Permit 02-DP-0187 Calvert Cliffs Nuclear Power Plant On July 30, 2004 Calvert Cliffs Nuclear Power Plant personnel identified that the auxiliary boiler blowdown effluent (Monitoring point 103 A) had been discharged Intermittently from the CCNPP site in Lusby, MD without monitoring as required by NPDES permit 02-DP-0187. This permit requires flow, total suspended solids, and oil and grease monitoring to be performed monthly, with pH to be monitored during each discharge from monitoring point 103 A. No monitoring was performed between June 1, 2004 when the permit requirement became effective, and July 30, 2004, when the lack of monitoring was discovered.
Approximately 5000 gallons of auxiliary boiler blowdown effluent was discharged to the Chesapeake Bay between June 1, 2004 and July 30, 2004. When plant staff identified that the discharges had occurred, the auxiliary boiler blowdown discharge was sampled for pH, total suspended solids, and oil and grease. Ail values .were within permit limits; oil and grease and total suspended solids results were both less than detectable concentrations. Based on the relatively small discharge volume and the satisfactory analysis results the impact of this discharge on public health and the waters of the state is negligible.
The cause of the unanticipated discharge was the auxiliary boiler blowdown tank discharge pump controls were in the 'automatic' positions when they should have been in the 'manual' position. This caused the tank to discharge whenever a set volume was reached without site personnel being aware of the discharge. Upon discovery the controls were immediately placed in the 'manual' position. A note has been placed on the controls to ensure they are not put back into the 'automatic' mode. Site procedures are being revised to require the auxiliary boiler blowdown tank discharge pump controls be maintained in the 'manual' position and to monitor each discharge as required by the permit.
If you have any questions, please contact Brenda Nuse at (410) 495-4913.
Sincerely gl-rj Kevin J. Nietmann Plant General Manager KJN/BDN cc: B.D. Nuse T.G. Ringger (CGG-ES)
. I .. .: