ML042100250
| ML042100250 | |
| Person / Time | |
|---|---|
| Site: | Duane Arnold |
| Issue date: | 07/13/2004 |
| From: | Peifer M Nuclear Management Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| GL-97-002, NG-04-0436 | |
| Download: ML042100250 (3) | |
Text
Nuie Committed to Nuclear Excellene Duane Arnold Energy Center Operated by Nuclear Management Company, LLC July 13, 2004 NG-04-0436 TS 5.6.4 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station 0-Pl-17 Washington, DC 20555-0001 DUANE ARNOLD ENERGY CENTER DOCKET 50-331 LICENSE No. DPR-49 MONTHLY OPERATING REPORT Please find enclosed the Duane Arnold Energy Center Monthly Operating Report.
The report has been prepared in accordance with the guidelines of NRC Generic Letter 97-02: "Revised Contents Of The Monthly Operating Report," and distribution has been made in accordance with DAEC Technical Specifications, Section 5.6.4.
This letter makes no new commitments or changes to any existing commitments.
Sincerely, Mark A. Peifer Site Vice President, Duane Arnold Energy Center CC Regional Administrator, USNRC, Region III Project Manager, USNRC, NRR NRC Resident Inspector (DAEC)
Enclosure:
OPERATING DATA REPORT
,~~~
!1 e'I
- ~~
~
~
1.
1-- TIG4-
3277 DAEC Road
- Palo, Iowa 52324-9785 Telephone: 319.851.7611
July 13, 2004 Enclosure to NG-04-0436 Page 1 of 2 OPERATING DATA REPORT DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIOD:
50-331 Duane Arnold July 2, 2004 Mike Fairchild (319) 851-7642 June 2004 1.
2.
Design Electrical Rating (MWe)
Maximum Dependable Capacity (MWe-Net) 581.40 565.50
- 3. Number of Hours the Reactor was Critical
- 4. Number of Hours Generator On-line
- 5. Reserve Shutdown Hours
- 6. Net Electrical Energy Generated (MWHrs)
This Month 720.00 720.00 0.00 412,259.40 Yr-to-Date 4,295.57 4273.23 0.00 2,470.631.70 Cumulative 205,973.84 201,558.75 192.80 94,425,907.38 UNIT SHUTDOWNS Type Method F: Forced of Cause & Corrective S:
Duration Shutting Action No.
Date Scheduled tHours)
Reason 1 Down Comments
.Y I.
'Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain) 2Method:
I Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
July 13, 2004 Enclosure to NG-04-0436 Page 2 of 2 NARRATIVE
SUMMARY
During the month of June departures from full power operation occurred for the following:
- 1) June 5-6, a sequence exchange.
- 2) June 7, a load line adjustment.