ML040970333
| ML040970333 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 04/06/2004 |
| From: | Thomas C NRC/RGN-III |
| To: | |
| References | |
| MR 3-2004-0027 | |
| Download: ML040970333 (1) | |
Text
Morning Report Date: APR 06, 2004 PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION III Licensee/Facility:
Notification:
3-2004-0027 04/06/2004 MR Number:
FIRSTENERGY NUCLEAR OPERATING CO.
[1] B&W-L-LP Date:
Davis-besse RIII-Via Teleconf. with Site Oak Harbor, Ohio 050-00346 Dockets:
Davis-Besse Synchronized to Grid
Subject:
This information is current as of 10:00 a.m. (EDT) on April 6, 2004. The plant is currently in Mode 1 at 100% percent power. The plant performed a down-power evolution April 5 to establish plant conditions to support de-energizing the D2 non-essential 4.16 kV switchgear bus and replacement of a faulty feeder breaker to the D2 bus. The feeder breaker was identified as faulty when, during a routine breaker swap preventive maintenance evolution, the breaker failed to open using the remote control switch. Following the down-power evolution, the D2 bus was de-energized, and the breaker was removed from the enclosure. The D2 bus was re-energized via the normal alternate power source, and the plant returned to 100% power. The replacement breaker will be installed following completion of trouble-shooting efforts on the faulty breaker. Around-the-clock resident inspector coverage was utilized to monitor plant evolutions and maintenance activities.
The Davis-Besse Oversight Panel will continue to monitor plant activities utilizing enhanced inspection oversight coverage. For non-routine evolutions occurring after normal working hours, enhanced inspection oversight coverage will continue to be expanded to monitor these activities.
Regional Action:For Information Only Discussion:
Contact:
Email:
Phone No:
Org:
THOMAS, C S CST1@nrc.gov (419) 244-4494 R3