ML040970333

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Synchronized to Grid
ML040970333
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 04/06/2004
From: Thomas C
NRC/RGN-III
To:
References
MR 3-2004-0027
Download: ML040970333 (1)


Text

Morning Report Date: APR 06, 2004 PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION III Licensee/Facility:

Notification:

3-2004-0027 04/06/2004 MR Number:

FIRSTENERGY NUCLEAR OPERATING CO.

[1] B&W-L-LP Date:

Davis-besse RIII-Via Teleconf. with Site Oak Harbor, Ohio 050-00346 Dockets:

Davis-Besse Synchronized to Grid

Subject:

This information is current as of 10:00 a.m. (EDT) on April 6, 2004. The plant is currently in Mode 1 at 100% percent power. The plant performed a down-power evolution April 5 to establish plant conditions to support de-energizing the D2 non-essential 4.16 kV switchgear bus and replacement of a faulty feeder breaker to the D2 bus. The feeder breaker was identified as faulty when, during a routine breaker swap preventive maintenance evolution, the breaker failed to open using the remote control switch. Following the down-power evolution, the D2 bus was de-energized, and the breaker was removed from the enclosure. The D2 bus was re-energized via the normal alternate power source, and the plant returned to 100% power. The replacement breaker will be installed following completion of trouble-shooting efforts on the faulty breaker. Around-the-clock resident inspector coverage was utilized to monitor plant evolutions and maintenance activities.



The Davis-Besse Oversight Panel will continue to monitor plant activities utilizing enhanced inspection oversight coverage. For non-routine evolutions occurring after normal working hours, enhanced inspection oversight coverage will continue to be expanded to monitor these activities.



Regional Action:For Information Only Discussion:

Contact:

Email:

Phone No:

Org:

THOMAS, C S CST1@nrc.gov (419) 244-4494 R3