ML040200234
| ML040200234 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 01/15/2004 |
| From: | Jefferson W Florida Power & Light Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| GL-97-002, L-2004-005 | |
| Download: ML040200234 (3) | |
Text
0 FPL Florida Power & Light Company, 6501 S. Ocean Drive, Jensen Beach, FL 34957 January 15, 2004 L-2004-005 10 CFR 50.36 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 Re:
St. Lucie Units 1 and 2 Docket Nos. 50-335 and 50-389 Monthly Operating Report Pursuant to Technical Specification 6.9.1.6, and the guidance of Generic Letter 97-02, attached are the December 2003 Operating Data Report, Summary of Operating Experience Report, and Unit Shutdowns for St. Lucie Units I and 2.
Please contact us should there be any questions regarding this information.
Very truly yours, William J rson, r
%/ino Mrcldn fsr-WJ/KWF Attachments
j:Lq an FPL Group company
L-2004-005 Attachment Page 1 of 2 OPERATING DATA REPORT DOCKET NO.
50 UNIT NAME St DATE Ja COMPLETED BY W.
TELEPHONE (77 REPORTING PERIOD:
-335
. Lucie I nuary 13, 2004 D. Mead, Jr.
- 72) 467-7293 December 2003
- 1. Design Electrical Rating
- 2.
Maximum Dependable Capacity (MWe-Net) 830.00 839.00 3.
4.
5.
6.
Number of Hours the Reactor was Critical Number of Hours Generator On-line Reserve Shutdown Hours Net Electrical Energy Generated (MWHrs)
This Month Yr-to-Date Cumulative 744.00 8,760.00 193,544.00 744.00 8,760.00 191,710.30 0.00 0.00 0.00 639,980.00 7,504,813.00 157,100,947.0 UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action No.
Date S: Scheduled (Hours)
Reason I Down 2 Comments
SUMMARY
- Unit I operated at essentially full power through the entire month of December. In accordance with the requirements of Technical Specification 6.9.1.6, there were no challenges to the Power Operated Relief Valves (PORVs) or the safety valves during the report period.
I 2
Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain)
Method:
I Manual 2
Manual Trip/Scram 3 Automatic Trip/Scram 4
Continuation 5
Other (Explain)
I I.
L-2004-005 Attachment Page 2 of 2 OPERATING DATA REPORT DOCKET NO.
50 UNIT NAME St DATE Ja COMPLETED BY W.
TELEPHONE
_77 REPORTING PERIOD:
-389
. Lucie 2 nuary 13, 2004
.D. Mead, Jr.
- 72) 467-7293 December 2003 1.
2.
Design Electrical Rating Maximum Dependable Capacity (MWe-Net) 830.00 839.00 3.
4.
5.
6.
Number of Hours the Reactor was Critical Number of Hours Generator On-line Reserve Shutdown Hours Net Electrical Energy Generated (MWHrs)
This Month 603.77 552.72 0.00 439,036.00 Yr-to-Date 7,277.97 7,122.17 0.00 5,888,263.00 Cumulative 156,036.57 154,122.47 0.00 127,046,976.0 UNIT SHUTDOWNS Cause & Corrective Action Comments Reactor and Turbine were manually tripped by operators following problems with 2C condensate pump.
Automatic trip following loss of generator excitation.
Unit 2 removed from service to conduct additional troubleshooting of the main generator excitation switchgear.
SUMMARY
- On December 4, 2003, the Unit 2 reactor and Turbine were manually tripped due to impending failure of the 2C condensate pump. Unit 2 was returned to full power on December 6. 2003.
On December 20, Unit 2 was automatically tripped from hot full power following a loss of excitation to the main generator. Unit 2 returned to full power on December 24, 2003.
On December 26, 2003, the Unit 2 turbine and reactor were shutdown to facilitate further troubleshooting of the generator excitation switchgear. On December 29, 2003, Unit 2 returned to full power.
In accordance with the requirements of Technical Specification 6.9.1.6, there were no challenges to the Power Operated Relief Valves (PORVs) or the safety valves during the report period.
I 2
Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain)
Method:
I Manual 2
Manual TriplScram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)