ML032270214

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July 2003 Monthly Operating Report for Davis-Besse, Unit 1
ML032270214
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 08/13/2003
From: Bezilla M
FirstEnergy Corp
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
CCN: P-6-03-07
Download: ML032270214 (4)


Text

FA rstEn r

~Davis-Besse Nudear Power Stafion gy 5501 North State Route 2 Oak Harbor, Ohio 43449-9760 August 13, 2003 CCN: P6-03-07 Docket No. 50-346 License No. NPF-3 Document Control Desk U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Rockville, MD 20852-2738 Ladies and Gentlemen:

Monthly Operating Report, July 2003 Davis-Besse Nuclear Power Station Unit 1 Enclosed is a copy of the Monthly Operating Report for the Davis-Besse Nuclear Power Station for the month of July 2003.

If you have any questions, please contact Brian D. Bowles, Manager - Plant Engineering at (419) 321-7302.

Very truly yours, Mark B. Bezilla Plant Manager Davis-Besse Nuclear Power Station MDZ/ljk Enclosures cc: J. B. Hopkins DB-1 NRC/NRR Senior Project Manager NRC Region m Administrator C. S. Thomas DB-I Senior Resident Inspector

Docket Number 50-346 License Number NPF-3 P-63-07 Page 1 of I COMMITMENT LIST The following list identifies those actions committed to by Davis-Besse Nuclear Power Station in this document. Any other actions discussed in the submittal represent intended or planned actions by Davis-Besse. They are described only as information and are not regulatory commitments. Please notify the Manager - Regulatory Affairs (419-321-8450) at Davis-Besse of any questions regarding this document or any associated regulatory commitments.

Commitments Due Date None

OPERATING DATA REPORT DOCKET NO.

UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIOD 50-0346 Davis-Besse Unit 1 8/01/03 M.D. Zawacki 419-321-7692 July, 2003 MONTH YEA DATE 906 I

Design Electrical Rating (Rlwe-Net).

The nominal net electrical output of the unit specified by the utility and used for the purpose of plant design.

2 Maximum Dependable Capacity (lwe-Net)

The gross electrical ouput as measured at the output terminals of the turbine-generator during the most restrictive seasonal conditions minus the normal station service loads.

3 Number of Hours the Reactor Was Critical.

The total number of hours during the gross hours of the reporting period that the reactor was critical.

4 Number of Hours the Generator Was On LUne.

(Also called Service Hours). The total number of hours during the gross hours of the reporting period that the unit operated with breakers closed to the station bus.

The sum of the hours the gerator was on line plus the total outage hours should equal the gross hours in the reporting period.

5 Unit Reserve Shutdown Hours The total number of hours during the gross hours of the reporting period that the unit was removed from service for economic or similar reasons but was available for operation 882 0.0 0.0 0.0 0.0 0.0 147,634.3 145,037.1 0.0 5,532.0 6 Net Electrical Energy (MWH).

The gross electrical output of the unit measured at the output terminals of the turbine-generator minus the normal station service loads during the gross hour of the reporting period, expressed in mega-watt hours. Negative quantities should not be used.

0 0.0 119,131.798

UNIT SHUTDOWNS DOCKET NO.

50-346 UNIT NAME Davis-Besse #1 DATE 8/01103 COMPLETED BY M.D. Zawacki REPORTING PERIOD:

July, 2003 TELEPHONE (419) 321-7692 NO.

DATE TYPE DURATION REASON (1)

METHOD OF CAUSEICORRECTIVEACTIONS F: FORCED (HOURS)

SHUTTING S: SCHEDULED DOWN (2)

COMMENTS 1

2/16/02 S: SCHEDULED 744.0 C, H 1.4 13 RFO work on the reactor vessel pressure retaining head revealed degradation and corrosion. As a result the head was replaced and all boric acid was removed from containment. The plant remained shutdown due to modifications of the Decay Heat Valve Pit, the Emergency Sump, Containment Air Coolers, etc. The plant is currently involved in the resolution of issues with it's High Pressure Injection Pumps along with additional work.

SUMMARY

The reactor was shutdown on February 16, 2002 to begin the 13th refueling outage. Corrosion and degradation was found on the head and it has since been replaced. The plant remained shutdown through the month of July due to continuing work.

(1) Reason:

A-Equipment Failure (Explain)

B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training & License Exam F-Administrative G-Operational Error (Explain)

H-Other (Explain)

(2) Method:

1-Manual 2-Manual Trip/Scram 3-Automatic Trip/Scram 4-Continuation 5-Other (Explain)