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MONTHYEARML0231700222002-11-13013 November 2002 Summary of Conference Calls with Florida Power and Light Regarding Reactor Vessel Head Inspection Results Project stage: Other ML0301607982003-01-16016 January 2003 Withholding from Public Disclosure, WCAP-15945-P, MB5917 Project stage: Other 2002-11-13
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Category:Memoranda
MONTHYEARML23166A0042023-06-15015 June 2023 Summary of Meeting Concerning 2023 Annual Assessment of the Saint Lucie and the Turkey Point Nuclear Plants ML22188A0862022-07-0707 July 2022 SLRA - Audit Report ML22145A3932022-05-25025 May 2022 Public Meeting Summary 2021 Annual Assessment Meeting 20220434 ML21337A1962021-12-16016 December 2021 Public Scoping Meeting Summary for the Environmental Review of the Subsequent License Renewal Application for St. Lucie Plant, Units 1 and 2 ML21159A1352021-06-0808 June 2021 Public Meeting Summary Regarding the Saint Lucie Nuclear Plant, Units 1 and 2, Docket No. 50-335 and 389, and the Turkey Point Nuclear Generating Station Units 3 and 4, Docket No. 50-250 and 50-251; Meeting Number 20210505 ML20150A4732020-05-29029 May 2020 EOC Meeting Summary ML19121A6102019-05-0101 May 2019 Public Meeting Summary - St Lucie Nuclear Plant, Docket Nos. 50-389 and 50-335 ML18144A1452018-05-24024 May 2018 Public Meeting Summary - St. Lucie Nuclear Plant Docket Nos. 50-335 and 50-389 ML17103A0342017-04-12012 April 2017 Summary of Category 1 Public Meeting to Discuss the Significance Determination Process for a Finding at St. Lucie, Unit 1 ML16097A1302016-04-0404 April 2016 March 29, 2016 Summary of Public Meeting - 2015 Annual Assessment Regarding Saint Lucie ML15320A5512015-11-23023 November 2015 SER MF5835 ML15240A1542015-09-0808 September 2015 Staff Observations of Sump Strainer Head Loss Testing at Alden Laboratory for Generic Safety Issue 191 ML14163A6522014-06-19019 June 2014 Summary of May 29, 2014, Public Meeting with NextEra Energy, Inc. and Florida Power & Light Company Regarding Proposed Amendment to Transition Fuel Type at St. Lucie Unit 2 ML14156A2132014-06-0404 June 2014 Public Meeting Summary - St. Lucie Nuclear Plant Docket Nos. 50-335 and 50-389 ML13059A5522013-03-0101 March 2013 3/14/13 - Forthcoming Meeting with Florida Power and Light Company Regarding Steam Generator Performance at St. Lucie Nuclear Plant, Units 1 and 2 ML12222A0392012-08-0909 August 2012 8/16/2012 Cancellation Notice of Forthcoming Conference Call with NextEra Energy and Florida Power and Light Concerning Generic Letter 2004-02 and Request for NRC Staff Review of Draft Proposed Guideline for Strainer Fiber Bypass Test Proto ML12213A0612012-08-0101 August 2012 8/16/12 Forthcoming Conference Call with NextEra Energy and Florida Power & Light Concerning Generic Letter 2004-02 and Request for NRC Staff Review of Draft Proposed Guideline for Strainer Fiber Bypass Test Protocol ML12150A2992012-06-0505 June 2012 May 17, 2012, Summary of Teleconference Held Between the U.S. Nuclear Regulatory Commission, U.S. Fish and Wildlife Service, and Florida Power & Light Co. to Discuss the Terms of the Biological Opinion at the St. Lucie Plant, Units 1 and 2 ML1204005162012-02-0909 February 2012 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection ML11251A0052011-09-0909 September 2011 9/21/11 Notice of Forthcoming Meeting with Florida Power and Light Regarding St. Lucie Nuclear Plant, Units 1 and 2 Extended Power Uprate ML11231A7172011-08-25025 August 2011 Notice of Forthcoming Meeting with Florida Power and Light Company (FPL) Regarding Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized-Water Reactors. ML11182A0142011-07-0101 July 2011 Forthcoming Meeting with Florida Power & Light Company Regarding St. Lucie Nuclear Plant, Unit 1 to Discuss Extended Power Uprate License Amendment Request That Is Currently Under Review ML1109006712011-04-21021 April 2011 Acceptance of License Amendment Request for an Extended Power Uprate (Epu), St Lucie Nuclear Plant ML1106104272011-03-0707 March 2011 Notice of Forthcoming Pre-Application Meeting with Florida Power & Light Company and NextEra Energy Regarding Turkey Point, Units 3 and 4, St. Lucie, Units 1 and 2, Point Beach, Units 1, and 2, and Duane Arnold ML1035405732010-12-21021 December 2010 Acceptance of License Amendment Request for an Extended Power Uprate (Epu), St. Lucie Nuclear Plant, Unit 1 ML1025601362010-09-0707 September 2010 Notice of Meeting with Florida Power & Light Company to Discuss the Florida Power & Light Company'S Forthcoming Applications for the Extended Power Uprates of St. Lucie Units 1 & 2 and Turkey Point Units 3 & 4, Focusing on the Topic of Spen ML0921805182009-08-0606 August 2009 Notice of Public Meeting with Florida Power & Light Energy ML0909705822009-04-0707 April 2009 Phone Call Summary with Licensees and Alion Science and Technology on April 2, 2009 to Address NRC Staff Position on Chemical Effects Refinements ML0832502332008-12-0202 December 2008 Summary of Public Meeting with Operators of Vogtle Units 1 & 2, San Onofre Units 2 & 3, St. Lucie Unit 1, Turkey Point Unit 3, Indian Point Units 2 & 3, Nuclear Energy Institute, and Alion Science and Technology ML0826006252008-09-16016 September 2008 Draft Request for Additional Information on Relief Request No. 2 Regarding Structural Weld Overlays ML0820008422008-07-18018 July 2008 Memorandum of the Secretary (Referring a Petition to Intervene to the ASLBP) ML0807400842008-03-14014 March 2008 Draft Regulatory Guide for Comment ML0810502852008-03-11011 March 2008 NDE Report, on PSL-1 Pressurizer Nozzles, Attachment 3 ML0635602592006-12-27027 December 2006 Forthcoming Meeting with Florida Power and Light to Discuss Proposed License Amendment Request to Adopt Alternate Source Term at the St. Lucie Nuclear Plant ML0633303802006-11-29029 November 2006 Forthcoming Meeting with Florida Power & Light Regarding Proposed License Amendment Request to Adopt Alternate Source Term at St. Lucie Nuclear Plant ML0614505922006-05-26026 May 2006 Wits 200600198 - Actions to Be Taken in Response to Hurricane Lessons Learned Task Report ML0609602052006-04-0606 April 2006 Meeting Notice, Florida Power & Light, St. Lucie Unit 2, Steam Generator Tube Inspection During Refueling ML0523704412005-08-31031 August 2005 Closeout Letter for Bulletin 2003-01, Potential Impact of Debris Blockage on Emergency Sump Recirculation at Pressurized-Water Reactors. ML0517402732005-06-23023 June 2005 Notice of Meeting with Florida Power and Light Company (FPL) & Westinghouse LAR to Increase SG Tube Plugging at St. Lucie ML0502701092005-01-25025 January 2005 Safety Evaluation on the Relief Request 2 Associated with the Third 10-year Inservice Inspection Interval - Inservice Inspection Program for St. Lucie Unit 2 ML0419005722004-07-0101 July 2004 Ltr, Temporary Change in Personnel Assignment ML0326809972003-10-0909 October 2003 Renewal of Full-Power Operating Licenses for St. Lucie, Units 1 and 2 ML0324005942003-08-25025 August 2003 June 10-11, 1997, Summary of NRC Senior Management Meeting to Review Performance of Operating Nuclear Power Plants and Materials Facilities Licensed by Nrc. Partially Withheld ML0321800032003-08-0606 August 2003 08/20-21/2003 Notice of Meeting with Florida Power and Light Regarding Increased Steam Generator Tube Plugging and Reload Methodology at St. Lucie, Unit 2 ML0316210252003-06-11011 June 2003 Peer Review of Risk-informed Safety Evaluation of the Suppression Capability in the Cable Spreading Room at St. Lucie Nuclear Power Plant Unit 1 ML0312702872003-05-0707 May 2003 Submission of Draft Request for Additional Information and Summary of a Conference Call Regarding Steam Generator Tubesheet Amendment ML0309808612003-04-0909 April 2003 Corrected Notice for Meeting with FPL to Discuss Requests for Relaxation from Reactor Pressure Vessel Head Inspection Order at St.Lucie, Unit 2 ML0309306732003-04-0303 April 2003 Meeting with FPL to Discuss Requests for Relaxation from Reactor Pressure Head Inspection Order at St. Lucie ML0306902142003-03-0606 March 2003 Halon 1301 Fire Suppression System ML0305806052003-02-26026 February 2003 Memo - Submission of Draft Request for Additional Information Regarding Risk Informed Inservice Inspection 2023-06-15
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARML23243A9862023-08-31031 August 2023 NRR E-mail Capture - Draft RAIs for EP Staff Augmentation Times LAR (L-2022-LLA-0166) ML23226A0762023-08-14014 August 2023 NRR E-mail Capture - Request for Additional Information - St. Lucie Plant, Units 1 and 2 - Adopt 10 CFR 50.69 (L-2022-LLA-0182) ML23173A1522023-06-22022 June 2023 Request for Additional Information NextEra Fleet Emergency Plan Amendment Request ML23254A4022023-01-24024 January 2023 RP Inspection_2023-001_Document Request ML22311A5582022-11-22022 November 2022 Supplemental Information Needed for Acceptance of Requested Licensing Action Amendment Request for Cep ML22325A0692022-11-18018 November 2022 RAI Set 4 ML22270A1482022-09-26026 September 2022 SLRA Second Round RAI Letter 2 - Class 1 Fatigue (Final) ML22217A0022022-08-0404 August 2022 Email from Brian Harris (NRC) to Robert Coffey (FPL) - St. Lucie SLRA Second Round RAI Letter 1) ML22217A0032022-08-0404 August 2022 SLRA Second Round RAI Letter 1) ML22193A0872022-07-11011 July 2022 Letter RAI Set 3 (Final) ML22133A0032022-05-12012 May 2022 SLRA Rai'S Set 1 ML22101A2322022-05-0202 May 2022 Summary of the Environmental Remote Audit Related to the Review of the Subsequent License Renewal Application Enclosure RCIs and RAIs ML22094A1672022-04-0101 April 2022 2022 St. Lucie POV Inspection Information Request ML22075A1212022-03-16016 March 2022 Stl Problem Identification and Resolution (Pi&R) Information Request Final Report ML21350A4262021-12-21021 December 2021 Supplemental Information Needed for Acceptance of Licensing Amendment Request Concerning Technical Specification Conversion to NUREG-1432, Revision 5 ML21119A3142021-04-28028 April 2021 Requests for Additional Information Regarding License Amendment Requests to Apply Risk Informed Completion Times (RICT) for the 120-Volt AC (EPID L-2020-LLA-0283) (Email) ML21063A3192021-03-0404 March 2021 Request for Additional Information Regarding Relief Request RR 15 - Extension of RPV Welds from 10 to 20 Years ML20092G3442020-04-0101 April 2020 RAIs for LAR to Revise Technical Specifications 6.8.4.o, Reactor Coolant Pump Flywheel Inspection Program ML20094G2022020-03-30030 March 2020 Request for Additional Information Regarding License Amendment Request to Adopt EAL Schemes Pursuant to NEI 99-01 (L-2019-LLA-0210) ML19225D3152019-08-13013 August 2019 NRR E-mail Capture - St. Lucie Plant, Unit No. 2, Request for Additional Information Regarding License Amendment Request to Relocate the MOV Thermal Overload Bypass Devices (L-2019-LLA-0106) ML19218A2742019-08-0606 August 2019 Notification of Inspection and Request for Information ML19193A1982019-07-12012 July 2019 Emailed St. Lucie Heat Sink RFI ML19192A1372019-07-11011 July 2019 NRR E-mail Capture - Request for Additional Information - St. Lucie Plant, Unit No. 2, Fall 2018 Refueling Outage Steam Generator Tube Inspection Report ML19192A1352019-06-25025 June 2019 NRR E-mail Capture - Draft Request for Additional Information - 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Text
November 13, 2002 LICENSEE: Florida Power and Light FACILITY: Saint Lucie Unit 1
SUBJECT:
SUMMARY
OF CONFERENCE CALLS WITH FLORIDA POWER AND LIGHT REGARDING REACTOR VESSEL HEAD INSPECTION RESULTS (TAC NO. MB5917)
During October 10-14, 2002, the Nuclear Regulatory Commission (NRC) staff participated in several conference calls with the Florida Power and Light (FPL) to discuss the ongoing reactor vessel head penetration (RVHP) inspection activities at the Saint Lucie Plant Unit 1 (STL1).
The following summary highlights the interactions between the licensee and the NRC staff.
OCTOBER 10, 2002, OUTAGE CONFERENCE CALLS On October 10, 2002, the NRC staff participated in a conference call with FPL to discuss the status of ongoing RVHP inspection activities at STL1. The licensee indicated that they were conducting ultrasonic testing (UT), and bare metal visual testing (BMV) in accordance with their response to NRC Bulletin 2002-02, Reactor Pressure Vessel Head Penetration Nozzle Inspection Programs. FPL indicated that between 80-90 percent of the testing had been complete and at the time of the call had found no boric acid leakage or vessel head wastage.
The NRC staff asked several questions which are attached to this summary. The licensee indicated that the reply to these questions would be addressed in FPLs 30-day post-outage response for Saint Lucie Unit 1 to Bulletin 2002-02.
The licensee identified three issues with the ongoing STL1 RPVH inspections. These issues concerned encountering an impediment to BMV due to debris, lift-off of the probe during UT, and interference due to bent guide sleeves on two control element drive mechanism (CEDM) nozzles. The licensee briefly discussed these issues and the contingencies planned if the issues could not be resolved.
FPL supplied written information in support of these conference calls which was comprehensive and is attached to this summary. At the conclusion of this conference call, a follow-up call was scheduled for October 12, 2002, to discuss the inspection results once additional testing had been completed.
OCTOBER 12, 2002, OUTAGE CONFERENCE CALLS On October 12, 2002, the NRC staff participated in a conference call with FPL to discuss the ongoing RPVH inspection activities at STL1. FPL indicated that they had completed UT on 67 of 69 CEDMs. At the time of the call, the licensee had completed more of the inspections and several CEDM nozzles were identified with anomalous results due to either probe lift-off, debris, or guide sleeve interference. The licensee discussed their plan with the staff to resolve the anomalous results. FPL indicated that a UT scan using a rotating probe would be performed on
nozzles with bent guide sleeves after removal of the guide sleeve. The licensee indicated that one nozzle which was missing some UT data due to obstructions would be analyzed to determine the acceptability of continued operation without completion of the testing, and that debris identified on four out of eight in-core instruments would be cleaned on top of the reactor vessel head and visually re-inspected. In addition the licensee indicated that an analysis of the debris was conducted, which revealed that the debris was composed mainly of paint flakes as well as asbestos.
Given the licensees position concerning the missing UT data, the NRC staff indicated it would discuss the issue internally and discuss the results of those internal discussions with the licensee. This discussion was held later in the day. The staff indicated that there were no additional questions concerning the test results presented to date. However, the staff requested that the licensee provide an update upon completion of the testing. In addition the staff requested that the licensee include any exceptions to complete coverage and FPLs disposition of those exceptions, as well as a flaw analysis of the one nozzle identified by the licensee to have an obstruction which precluded satisfactory testing, in FPLs 30-day post-outage response to Bulletin 2002-02 for STL1. FPL indicated agreement with the NRC staffs request.
FPL supplied written information in support of this conference call which was comprehensive and is attached to this summary. The staff indicated their intention to contact the licensee with a status of the staffs review of the updated test results.
OCTOBER 14, 2002, OUTAGE CONFERENCE CALL The staff contacted FPL to briefly discuss the staffs review of a summary of the results for the RPVH testing. At the conclusion of the conference call on October 14, 2002, the licensee indicated that they would submit an update upon completion of testing. After review, the staff informed the licensee that the staff had no more questions on the information provided at this time. In accordance with Bulletin 2002-02, the staff will perform a more comprehensive review of the test results and FPLs disposition of the anomalous results as a result of debris, obstructions or interference upon receiving FPLs 30-day post-outage response. FPL indicated that a completed copy of a draft matrix of the results provided for the staffs review would be submitted along with the 30-day post-outage response.
/RA/
Brendan T. Moroney, Project Manager, Section 2 Project Directorate II Division of Licensing Project Management Office of Nuclear Reactor Regulation Docket No. 50-335 Attachments: 1. Request for Additional Information
- 2. Handout dated October 10, 2002
- 3. Handout dated October 12, 2002 cc w/atts: See next page
ML023170022 OFFICE PDII-2/PM PDII-2/PM PDII-2/LA EMCB/SC PDII-2/SC NAME EBrown BMoroney BClayton TChan AHowe DATE 10/31/02 10/31/02 10/31/02 11/06/02 11/08/02 Mr. J. A. Stall ST. LUCIE PLANT Florida Power and Light Company cc:
Senior Resident Inspector Mr. R. E. Rose St. Lucie Plant Plant General Manager U.S. Nuclear Regulatory Commission St. Lucie Nuclear Plant P.O. Box 6090 6351 South Ocean Drive Jensen Beach, Florida 34957 Jensen Beach, Florida 34957 Craig Fugate, Director Mr. Kelly Korth Division of Emergency Preparedness Licensing Manager Department of Community Affairs St. Lucie Nuclear Plant 2740 Centerview Drive 6351 South Ocean Drive Tallahassee, Florida 32399-2100 Jensen Beach, Florida 34957 M. S. Ross, Attorney Mr. William Jefferson Florida Power & Light Company Vice President, Nuclear Operations Support P.O. Box 14000 Florida Power & Light Company Juno Beach, FL 33408-0420 P.O. Box 14000 Juno Beach, FL 33408-0420 Mr. Douglas Anderson County Administrator Mr. Rajiv S. Kundalkar St. Lucie County Vice President - Nuclear Engineering 2300 Virginia Avenue Florida Power & Light Company Fort Pierce, Florida 34982 P.O. Box 14000 Juno Beach, FL 33408-0420 Mr. William A. Passetti, Chief Department of Health Mr. J. Kammel Bureau of Radiation Control Radiological Emergency 2020 Capital Circle, SE, Bin #C21 Planning Administrator Tallahassee, Florida 32399-1741 Department of Public Safety 6000 SE. Tower Drive Mr. Donald E. Jernigan, Site Vice President Stuart, Florida 34997 St. Lucie Nuclear Plant 6351 South Ocean Drive Jensen Beach, Florida 34957
REQUEST FOR ADDITIONAL INFORMATION REACTOR PRESSURE VESSEL (RPV) HEAD AND VESSEL HEAD PENETRATION (VHP)
INSPECTIONS RELATIVE TO RECENT INSPECTION FINDINGS SAINT LUCIE UNIT 1, DOCKET NUMBER 50-335
- 1) As a result of recent inspection findings, the NRC has concerns about the combination and scope of inspection methods used during RPV head and VHP nozzle inspections implemented in response to Bulletin 2002-02. The concern is that through-weld cracks in the J-groove welds may provide the conditions that could lead to circumferential cracking in the nozzle base material at or above the J-groove weld with no visual indications of leakage deposits on the RPV head.
North Anna Unit 2 has identified circumferential cracks in nozzles examined with UT and indications were identified on the J-groove weld of a high percentage of the penetrations. According to the licensee for North Anna, there were no visual indications of boric acid deposits on the surface of the RPV head at all of these nozzles. This finding, if verified, indicates that cracks in the J-groove welds may provide the conditions that could lead to circumferential cracking in the nozzle base material at or above the J-groove weld with no visual indications of leakage deposits on the surface of the RPV head.
Considering the discussion above, include a written discussion of whether the findings at North Anna Unit 2 alter your justification for continued reliance on visual examinations and the decision not to directly examine the J-groove welds.
- 2) Provide your RPV and VHP heat data for Saint Lucie Unit 1.
- 3) Provide a copy of the Condition Reports generated as a result of issues with the bare metal, ultrasonic, or visual testing conducted in accordance with Bulletin 2002-02.
Attachment 1