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Category:Letter
MONTHYEARML24032A1112024-02-0101 February 2024 Owner'S Activity Report for North Anna, Unit 2, Refueling Outage N2R29 - First Period of the Fifth ISI Interval ML24032A4662024-01-16016 January 2024 Response to Comments on Draft Vpdes Permit No. VA0052451 ML24017A0802024-01-11011 January 2024 Notification of Licensed Operator Initial Examination 05000338/2024301 and 05000339/2024301 ML24003A8372024-01-0909 January 2024 Letter to Elizabeth Toombs, Thpo, Cherokee Nation, Notice of Availability of the Draft Site-Specific EIS for North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8412024-01-0909 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8502024-01-0909 January 2024 Letter to Wenonah Haire, Thpo, Catawba Indian Nation, Notice of Availability of the Draft Site-Specific EIS for North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML23332A7272024-01-0909 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8382024-01-0909 January 2024 Letter to G. Anne Richardson, Chief, Rappahannock Tribe, Inc., Notice of Availability of Draft Site-Specific Environmental Impact Statement for North Anna Power Station Units 1 and 2, Subsequent License Renewal ML24003A8482024-01-0909 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8392024-01-0909 January 2024 Letter to Gerald Stewart, Chief, Chickahominy Indian Tribe, Eastern Division Re Re Notice of Availability of the Draft Site-Specific Environmental Impact Statement for North Anna Power Station Subsequent License Renewal ML24003A8472024-01-0909 January 2024 Letter to Tom Jonathan, Chief, Tuscarora Nation, Notice of Availability of the Draft Site-Specific EIS for North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8492024-01-0909 January 2024 Letter to W. Frank Adams, Chief, Upper Mattaponi Tribe Re Re Notice of Availability of the Draft Site-Specific Environmental Impact Statement for North Anna Power Station Subsequent License Renewal ML24003A8462024-01-0909 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8352024-01-0909 January 2024 Letter to Acee Watt, Thpo, United Keetoowah Band of Cherokee Indians in Oklahoma Re Notice of Availability of the Draft Site-Specific Environmental Impact Statement for North Anna Power Station Subsequent License Renewal ML24003A8422024-01-0909 January 2024 Letter to Paul Barton, Thpo, Eastern Shawnee Tribe of Oklahoma, Notice of Availability of Draft Site-Specific Environmental Impact Statement for North Anna Power Station Units 1 and 2, Subsequent License Renewal ML24003A8432024-01-0909 January 2024 Letter to Robert Gray, Chief, Pamunkey Indian Tribe, Notice of Availability of the Draft Site-Specific EIS for North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8362024-01-0909 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML24003A8442024-01-0909 January 2024 Letter to Russell Townsend, Thpo, Eastern Band of Cherokee Indians ML24003A8402024-01-0909 January 2024 Letter to Katelyn Lucas, Thpo, Delaware Nation, Oklahoma, Notice of Availability of Draft Site-Specific Environmental Impact Statement for North Anna Power Station Units 1 and 2, Subsequent License Renewal ML24003A8452024-01-0909 January 2024 Letter to Stephen Adkins, Chief, Chickahominy Indian Tribe, Notice of Availability of Draft Site-Specific Environmental Impact Statement for North Anna Power Station Units 1 and 2, Subsequent License Renewal ML23332A1852024-01-0404 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML23332A0872024-01-0404 January 2024 Notice of Availability of the Draft Site-Specific Environmental Impact Statement for the North Anna Power Station, Units 1 and 2, Subsequent License Renewal ML23360A6352024-01-0404 January 2024 Letter to Dominion Availability for North Anna Units 1 and 2 Draft Site Specific Environmental Impact Statement ML23332A1472023-12-21021 December 2023 Issuance of Environmental Scoping Summary Report Associated with the Staff'S Review of the North Anna Power Station, Units 1 and 2, Subsequent License Renewal Application ML23283A3052023-12-20020 December 2023 Review of Appendix F to DOM-NAF2, Qualification of the Framatome ORFEO-GAIA and ORFEO-NMGRID CHF Correlations in the Dominion Energy VIPRE-D Computer Code (EPID L-2022-LLT-0003) (Nonproprietary) ML23346A0972023-12-11011 December 2023 License Amendment Request to Revise the Emergency Plan Relocation of the Technical Support Center - Response to NRC Request for Additional Information ML23346A1022023-12-11011 December 2023 2024 North Anna Power Station Brq Inspection Notification Letter ML24012A0942023-12-0707 December 2023 GL Report from Dominion Virginia Power Regarding Transfer of Devices ML24012A0892023-12-0707 December 2023 GL Registration from Dominion Virginia Power ML23334A2432023-11-30030 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23362A0602023-11-29029 November 2023 ISFSI, Submittal of Cask Registration for Spent Fuel Storage IR 05000339/20234022023-11-27027 November 2023 Security Baseline Inspection Report 05000338 and 05000339/2023402 IR 05000338/20230032023-11-13013 November 2023 Integrated Inspection Report 05000338/2023003 and 05000339/2023003 ML23311A2042023-10-0909 October 2023 Annual Submittal of Technical Specification Bases Changes Pursuant to Technical Specification 5.5.13.d IR 05000338/20234032023-10-0505 October 2023 Reissue - North Anna Power Station - Cyber Security Inspection Report 05000338/2023403 and 05000339/2023403 (Cover Letter) ML23279A0612023-10-0505 October 2023 Paragon Energy Solutions LLC, Part 21 Final Report Re Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23230A0502023-10-0202 October 2023 5 of the Quality Assurance Topical Report - Review of Program Changes ML23275A0992023-09-28028 September 2023 Subsequent License Renewal Application Third 10 CFR 54.21(b) Annual Amendment IR 05000338/20230112023-09-26026 September 2023 Quadrennial Focused Engineering Inspection Commercial Grade Dedication Report 05000338/2023011 and 05000339/2023011 ML23242A3482023-09-11011 September 2023 Cyber Security Inspection Report 05000338/2023403 and 05000339/2023403 - Cover ML23254A0242023-09-0606 September 2023 Paragon Energy Solutions LLC, Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23249A2592023-09-0606 September 2023 Core Operating Limits Report Cycle 30, Pattern Ukr, Revision 0 ML23214A2022023-09-0505 September 2023 Staff Assessment of Updated Seismic Hazards Following the NRC Process for the Ongoing Assessment of Natural Hazards Information 2024-02-01
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000339/LER-2016-0012016-09-21021 September 2016 Technical Specification Required Shutdown Due to Reactor Coolant System Leak, LER 16-001-00 for North Anna Power Station, Unit 2 Regarding Technical Specification Required Shutdown Due to Reactor Coolant System Leak 05000338/LER-2016-0032016-06-16016 June 2016 1 OF 3, LER 16-003-00 for North Anna, Unit 1, Regarding Engineered Safety Feature Actuation Due to Loss of Power to "A" Reserve Station Service Transformer 05000338/LER-2016-0022016-05-0505 May 2016 , Chemical Addition System Outside of Technical Specification Due to Excessive Unseating Thrust on MOVs, LER 16-002-00 for North Anna, Unit 1, Regarding Chemical Addition System Outside of Technical Specification Due to Excessive Unseating Thrust on MOVs 05000338/LER-2016-0012016-03-16016 March 2016 1 OF 3, LER 16-001-00 for North Anna, Units 1 and 2, Regarding Emergency Diesel Generators Automatic Start Due to Loss of Power to "C" Reserve Station Service Transformer ML0229604192002-10-11011 October 2002 Ventilation Radiation Monitor System Special Report 2016-09-21
[Table view] Category:Significant Event Report
MONTHYEARML0229604192002-10-11011 October 2002 Ventilation Radiation Monitor System Special Report 2002-10-11
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VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND,VIROINIA 23261 October 11, 2002 United States Nuclear Regulatory Commission Serial No.02-631 Attention: Document Control Desk NAPS: MPW Washington, D.C. 20555 Docket Nos. 50-338 50-339 License Nos. NPF-4 NPF-7 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION UNITS I & 2 VENTILATION RADIATION MONITOR SYSTEM SPECIAL REPORT On September 29, 2002, Process Vent Radiation Monitor 1-GW-RM-178 (RM) experienced a sample flow fault and the RM was subsequently declared inoperable.
Technical Requirement 3.3.7, Radiation Monitoring Instrumentation, Action E.1 requires initiation of a preplanned alternate method of monitoring within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> when a required RM is inoperable. The RM must also be restored to operability within 7 days or submit a Special Report within 7 days. On October 6, 2002, the 7 day allowed outage time for the RM expired without returning the component to service. As such, a special report is required to be submitted in accordance with Technical Requirement 3.3.7, Radiation Monitoring Instrumentation, Action F.1.
During investigation of the sample flow fault, it was found that sections of sample flow tubing on the RM skid were 87 to 89 degrees Fahrenheit (F) when measured with a contact pyrometer. Condensation was found in the sample flow tubing on the RM skid.
Condensation in the RM skid tubing is affecting the sample flow elements which have proven to be extremely sensitive to even minute amounts of moisture. Moisture causes the flow elements to indicate a fault condition which in certain cases shuts down the machine. Corrective actions implemented as a result of the root cause evaluation, referenced in Special Report Supplement dated August 22, 2002, replaced heat tracing on sample lines within the station up to the RM skid. This was intended to heat the sample stream high enough to allow the sample to pass through the RM skid tubing without dropping below the dewpoint. The new heat trace installed has not completely prevented condensation in some portions of the RM skid tubing, even though the sample temperature was successfully elevated to the maximum allowable temperature based on the resultant effect on detector temperature. The RM skid tubing is insulated but it does not have heat trace. Recent experience has identified under certain conditions ambient temperatures allow portions of the RM skid tubing to cool to a temperature close to or below the dew point of the sample. In the near term, we are
evaluating erecting a temporary enclosure to maintain consistent ambient temperatures around the RM skid tubing. Monitoring the enclosure and RM skid tubing temperatures will improve our ability to prevent unwanted condensation from occurring in the machine. When consistent temperature control is achieved, the RM will be declared operable and returned to service. Long term actions include evaluating installing a permanent enclosure and/or installing heat trace on the RM skid tubing.
As part of the preplanned alternate method of monitoring while 1-GW-RM-178 is out of service the normal range Westinghouse monitor remains in service, as does the high range Nuclear Research Corporation monitor, which can be used in either MIDAS or emergency procedures to perform dose projection. The results of these projections can be used to classify an event in accordance with the Emergency Action Levels described in the station Emergency Plan procedures. Grab sample capability on the Process Vent will also be maintained so that supporting sample analysis can be performed.
The Station Nuclear Safety and Operating Committee has reviewed this report and it will be provided to the Management Safety Review Committee. Should you have any questions regarding this report, please contact us.
Very truly yours, D. A. Heacock Site Vice President Commitments made in this letter: None
cc: U. S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center Suite 23T85 61 Forsyth St., SW, Atlanta, Georgia 30303 Mr. M. J. Morgan NRC Senior Resident Inspector North Anna Power Station