ML022000340
| ML022000340 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 07/11/2002 |
| From: | Byrne S South Carolina Electric & Gas Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| Download: ML022000340 (5) | |
Text
Stephen A. Byrne Senior Vice President, Nuclear Operations 803.345.4622 A SCANA COMPANY July 11, 2002 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Attention: Director, Office of Resource Management Ladies and Gentlemen:
Subject:
VIRGIL C. SUMMER NUCLEAR STATION DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 JUNE MONTHLY OPERATING REPORT Enclosed is the June 2002 Monthly Operating Report for the Virgil C. Summer Nuclear Station Unit No. 1. This submittal is made in accordance with the requirements of Technical Specifications, Section 6.9.1.10.
If there are any questions, please call me at your convenience.
Very truly yours, Stephen A. Byrne Oý' S, SAB/mbb Attachment c:
G. H. Halnon T. G. Eppink (w/o Attachment)
R. J. White L. A. Reyes K. R. Cotton T. D. Gatlin NRC Resident Inspector K. M. Sutton Paulette Ledbetter INPO Records Center J&H Marsh & McLennan William G. Wendland (ANI)
Pat Haught (Westinghouse)
RTS (0-L-99-0350-1)
File (818.03-1, RR 4100)
DMS (RC-02-0120)
SCE&G I Virgil C. Summer Nudeor Station
- P. 0. Box 88. Jenkinsville, South Carolina 29065 -T (803) 345.5209
- www.scona.com
Director, Office of Resource Management June Monthly Operating Report RC-02-0120 Page 1 of 4 ATTACHMENT I AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
UNIT DATE COMPLETED BY TELEPHONE Jun-02 AVERAGE DAILY POWER LEVEL (Mwe-Net) 0 0
41 287 418 790 919 378 938 974 968 958 961 960 971 973 DAY 17 18 19 20 21 22 23 24 25 26 27 28 29 30 50/395 V. C. SUMMER I July 2,2002 W. H. BELL (803) 345-4389 AVERAGE DAILY POWER LEVEL (Mwe-Net) 765 0
183 905 980 981 980 975 974 977 937 867 942 974 DAY 1
2 3
4 5
6 7
8 9
10 11 12 13 14 15 16
Director, Office of Resource Management June Monthly Operating Report RC-02-0120 Page 2 of 4 ATTACHMENT II OPERATING DATA REPORT DOCKET NO.
UNIT DATE COMPLETED BY TELEPHONE 50/395 V. C. SUMMER I July 2,2002 W. H. BELL (803) 345-4389 OPERATING STATUS 1
Reporting Period:
Ju Gross Hours in Reporting Period:
2 Currently Authorized Power Level (MWt):
Max. Depend. Capacity (MWe-Net):
Design Electrical Rating (MWe-Net):
3 Power Level to Which Restricted (If Any) (MWe-Net):
4 Reasons for Restrictions:
THIS MONTH YR TO DATE CUMULATIVE Number of Hours Reactor Critical Reactor Reserve Shutdown Hours Hours Generator On Line Unit Reserve Shutdown Hours Gross Thermal Energy Generated (MWH)
Gross Electrical Energy (MWH)
Net Electrical Energy Generated (MWH)
Reactor Service Factor Reactor Availability Factor Unit Service Factor Unit Availability Factor Unit Capacity Factor (Using MDC)
Unit Capacity Factor (Using Design)
Unit Forced Outage Rate 664.4 0.0 612.8 0.0 1596210 552490 527357 92.3 92.3 85.1 85.1 75.8 75.3 6.2 3283.0 0.0 3229.0 0.0 9149242 3203380 3079970 75.6 75.6 74.3 74.3 73.4 72.9 1.2 19 Shutdowns Scheduled Over Next 6 Months (Type, Date, & Duration of Each):
None 20 If Shutdown at End of Report Period, Estimated Date of Startup: N/A 21 Units in Test Status (Prior to Commercial Operation):
N/A in-02 720 2900 966 972.7 N/A N/A 5
6 7
8 9
10 11 12 13 14 15 16 17 18 134732.3 0.0 132853.4 0.0 358035650 120752129 115351151 83.1 83.1 81.9 81.9 78.5 77.4 3.2
Director, Office of Resource Management June Monthly Operating Report RC-02-0120 Page 3 of 4 ATTACHMENT III UNIT SHUTDOWNS AND POWER REDUCTION DOCKET NO.
UNIT DATE COMPLETED BY TELEPHONE 50/395 V. C. SUMMER I July 2,2002 W. H. BELL (803) 345-4389 DATE TYPE DURATION REASON METHOD CORRECTIVE ACTION/COMMENTS 1
04/20/2002 S
2 06/08/2002 S
3 06/17/2002 F
61.2 5.8 40.2 C
B A
1 Complete Refueling 1
Conduct Main Turbine Overspeed Test 3
Repair C Main Feedwater Pump and Reprogram Control System Logic REASON A: Equipment Failure B: Maintenance or Test C: Refueling D: Regulatory Restriction E: Operator Training and License Examination F: Administrative G: Operational Error H: Other (Explain) 2 METHOD 1: Manual 2: Manual Trip/Scram 3: Automatic Trip/Scram 4: Continuation (Use Initial Date) 5: Power Reduction (Duration 0.0) 9: Other (Explain)
SUMMARY
NO.
Jun-02
Director, Office of Resource Management June Monthly Operating Report RC-02-0120 Page 4 of 4 ATTACHMENT IV NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
50/395 UNIT V. C. SUMMER I DATE July 2,2002 COMPLETED BY W. H. BELL TELEPHONE (803) 345-4389 Jun-02 At the beginning of the month V. C. Summer Station was in Mode 2 while beginning the initial startup after the 13th refueling outage. The reactor became critical at 02:46 on 06/01/2002. The reactor automatically tripped due to a spike in intermediate range nuclear instrumentation channel NI 36. After replacing a circuit card in NI 36 the reactor was restarted and became critical at 18:57 on 06/02/2002. The main generator breaker was closed at 13:11 on 06/03/2002.
At 03:39 on 06/08/2002 the main generator breaker was opened to permit the performance of a main turbine overspeed test. The test was successfully completed and the breaker was closed at 09:24 on 06/08/2002. The reactor remained critical throughout this test evolution.
At 19:02 on 06/17/2002 the reactor tripped on lo lo level in the A steam generator. The low level was caused by the trip of the C main feedwater pump in conjunction with a feedwater digital control system logic error that inadvertently caused the feed pump recirculation valves to go full open. After the feed pump was repaired and the control logic corrected the reactor was restarted and became critical at 23:38 on 06/18/2002. The main generator breaker was closed at 11:16 on 06/19/2002. The plant remained on line for the remainder of the month.