ML021160009

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March 2002 Monthly Operating Report for Dresden Nuclear Power Station Units 2 and 3
ML021160009
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 04/15/2002
From: Swafford P
Exelon Generation Co, Exelon Nuclear
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
PSLTR: #02-0022
Download: ML021160009 (8)


Text

Exel nl.

Exelon Generation Dresden Generating Station www.exeloncorp.com Nuclear 6500 North Dresden Road Morris, IL 60450-9765 Tel 815-942-2920 April 15, 2002 PSLTR: #02-0022 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555-0001 Dresden Nuclear Power Station, Units 2 and 3 Facility Operating License Nos. DPR-19 and DPR-25 Docket Nos. 50-237 and 50-249

Subject:

Monthly Operating Report for March 2002 In accordance with Technical Specifications, Section 5.6.4, "Monthly Operating Reports," we are submitting the March 2002 - Monthly Operating Report for Dresden Nuclear Power Station, Units 2 and 3.

Should you have any questions concerning this letter, please contact Mr. Bob Rybak, Regulatory Assurance Manager, at (815) 416 - 2800.

Respectfully, Preston Sw Site Vice President Dresden Nuclear Power Station Attachment cc: Regional Administrator- NRC Region III NRC Senior Resident Inspector - Dresden Nuclear Power Station

ATTACHMENT DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3 MONTHLY OPERATING REPORT FOR MARCH 2002 EXELON GENERATION COMPANY, LLC FACILITY OPERATING LICENSE NOS. DPR-19 AND DPR-25 NRC DOCKET NOS. 50-237 AND 50-249 I

TABLE OF CONTENTS I. Introduction II. Summary of Operating Experience A. Unit 2 Monthly Operating Experience Summary B. Unit 3 Monthly Operating Experience Summary IIl. Operating Data Statistics A. Operating Data Report - Dresden Unit 2 B. Operating Data Report - Dresden Unit 3 IV. Unit Shutdowns A. Unit 2 Shutdowns B. Unit 3 Shutdowns V. Amendments to Facility Licenses or Technical Specifications No Amendments to Facility Licenses or Technical Specifications were issued in the month of March VI. Unique Reporting Requirements A. Main Steam Relief and/or Safety Valve Operations 2

1. Introduction Dresden Nuclear Power Station (DNPS) is a two reactor generating facility owned and operated by the Exelon Generation Company, LLC. DNPS is located at the confluence of the Kankakee and Des Plaines Rivers, in Grundy County, near Morris, Illinois.

DNPS Unit 2 is a General Electric Boiling Water Reactor. DNPS Unit 2 is licensed at 2957 megawatts thermal. The gross electrical output is 912 megawatts, with design net electrical output ratings of 864 megawatts. The commercial service date for Unit 2 is August 11, 1970.

DNPS Unit 3 is a General Electric Boiling Water Reactor. DNPS Unit 3 is licensed at 2527 megawatts thermal. The gross electrical output of Unit 3 is 834 megawatts, with design net electrical output ratings of 795 megawatts. The commercial service date for Unit 3 is October 30, 1971.

Waste heat is rejected to a man-made cooling lake using the Kankakee River for make up and the Illinois River for blowdown.

The Architect-Engineer for DNPS Units 2 and 3 was Sargent and Lundy of Chicago, Illinois.

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II.

SUMMARY

OF OPERATING EXPERIENCE FOR MARCH 2002 A. UNIT 2 MONTHLY OPERATING EXPERIENCE

SUMMARY

From March 01 through March 05, 2002, Unit 2 operated between 725 and 850 MWe, for planned maintenance on Feedwater, Condensate, and Condensate Booster Pumps. Operation at full uprated power requires all of these pumps to be in operation. Therefore periods have been scheduled for power derates in order to perform routine maintenance on these pumps. With the exception of the above description and scheduled surveillances, Unit 2 operated at full power for the remainder of the period.

B. UNIT 3 MONTHLY OPERATING EXPERIENCE

SUMMARY

Unit 3 was shutdown from March 15 through March 24, 2002 to replace Jet Pump hold-down beams. This action was taken in response to a failed jet pump beam at the Quad Cities Nuclear Power Station. With the exception of the above, Unit 3 operated throughout the remaining periods at full power except for short periods for maintenance and surveillances.

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III. OPERATING DATA STATISTICS A. Dresden Unit 2 Operating Data Report for March 2002 DOCKET NO. 050-237 DATE April 03, 2002 COMPLETED BY Don Hamilton TELEPHONE (815) 416-3585 OPERATING STATUS

1. REPORTING PERIOD: March 2002
2. CURRENTLY AUTHORIZED POWER LEVEL (MWth): 2,957 MAXIMUM DEPENDABLE CAPACITY (MWe NET): 850 (estimated)

DESIGN ELECTRICAL RATING (MWe Net): 864

3. POWER LEVEL TO WHICH RESTRICTED (MWe Net): No Restrictions
4. REASONS FOR RESTRICTIONS (IF ANY): See Section II.A of this report.

Unit Two Monthly Operating Status This Month Year to Date Cumulative

5. Hours in Period 744 2,160 277,320
6. Reactor Critical - Hours 744 2,160 209,798
7. Reactor Reserve Shutdown - Hours 0 0 0
8. Hours Generator On-Line 744 2,160 201,309
9. Unit Reserve Shutdown - Hours 0 0 4 10.Thermal Energy Generated - MWHt Gross 2,076,208 6,054,133 435,438,797
11. Electrical Energy Generated - MWHe Gross 667,990 1,946,751 139,626,259
12. Electrical Energy Generated - MWHe Net 639,922 1,859,169 132,341,850
13. Reactor Service Factor - Percent 100.0% 100.0% 75.7%
14. Reactor Availability Factor - Percent 100.0% 100.0% 75.7%
15. Generator Service Factor- Percent 100.0% 100.0% 72.6%
16. Generator Availability Factor- Percent 100.0% 100.0% 72.6%
17. Capacity Factor- (Using MDC Net) Percent 101.2% 101.3% 56.1%
18. Capacity Factor - (Using DER Net) Percent 99.5% 99.6% 55.2%

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III. OPERATING DATA STATISTICS B. Dresden Unit 3 Operating Data Report for March 2002 DOCKET NO. 050-249 DATE April 03, 2002 COMPLETED BY Don Hamilton TELEPHONE (815) 416-3585 OPERATING STATUS

1. REPORTING PERIOD: March 2002
2. CURRENTLY AUTHORIZED POWER LEVEL (MWth): 2,527 MAXIMUM DEPENDABLE CAPACITY (MWe Net): 773 DESIGN ELECTRICAL RATING (MWe Net): 795
3. POWER LEVEL TO WHICH RESTRICTED: No Restrictions
4. REASONS FOR RESTRICTIONS (IF ANY): See Section II.B of this report.

Unit Three Monthly Operating Status This Month Year to Cumulative Date

5. Hours in Period 744 2,160 266,640
6. Reactor Critical - Hours 566 1,982 197,000
7. Reactor Reserve Shutdown - Hours 0 0 0
8. Hours Generator On-Line 547 1,963 189,124
9. Unit Reserve Shutdown - Hours 0 0 1 10.Thermal Energy Generated - MWHt Gross 1,343,770 4,911,475 409,087,822
11. Electrical Energy Generated - MWHe Gross 438,339 1,601,352 131,302,794
12. Electrical Energy Generated - MWHe Net 422,365 1,546,950 124,849,485
13. Reactor Service Factor- Percent 76.1% 91.8% 73.9%
14. Reactor Availability Factor - Percent 76.1% 91.8% 73.9%
15. Generator Service Factor - Percent 73.5% 90.9% 70.9%
16. Generator Availability Factor - Percent 73.5% 90.9% 70.9%
17. Capacity Factor- (Using MDC Net) Percent 73.4% 92.6% 60.6%
18. Capacity Factor- (Using DER Net) Percent 71.4% 90.1% 58.9%

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IV. UNIT SHUTDOWNS A. Unit 2 Shutdowns for March 2002 NO DATE TYPE DURATION REASON (2) METHOD OF CORRECTIVE ACTIONS/

(1) (HOURS) SHUTTING DOWN COMMENTS REACTOR(3)

None B. Unit 3 Shutdowns for March 2002 NO DATE TYPE DURATION REASON (2) METHOD OF CORRECTIVE ACTIONS/

(1) (HOURS) SHUTTING DOWN COMMENTS REACTOR(3)

D3M09 3-15-02 5 197 B 1 Scheduled Maintenance Outage to replace Jet Pump hold-down beams.

LEGEND:

(1) Type: (2) Reason (3) Method F - Forced A. Equipment Failure (Explain) 1. Manual S - Scheduled B. Maintenance or Test 2. Manual Scram C. Refueling 3. Automatic Scram D. Regulatory Restriction 4. Other (Explain)

E. Operator Training & Licensing Exam 5. Load Reduction F. Administrative G. Operational Error H. Other (Explain)

V. Amendments to Facility Licenses or Technical Specifications During the month of March there were no Facility Licenses or Technical Specification changes.

VI. Unique Reportin2 Requirements A. Main Steam Relief and/or Safety Valve Operations Unit 2 - None Unit 3 - None 7