ML021000111

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the University of Michigan Report on Reactor Operations
ML021000111
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Site: University of Michigan
Issue date: 03/28/2002
From: Becker C
University of Michigan
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Document Control Desk, NRC/FSME
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MICHIGAN MEMORIAL -PHOENIX PROJECT PHOENIX MEMORIAL LABORATORY FORD NUCLEAR REACTOR ANN ARBOR, MICHIGAN 48109-2100 March 28, 2002 Document Control Desk United States Nuclear Regulatory Commission Washington, D.C. 20555 Re: License R-28 Docket 50-2

Dear Sir:

The enclosed REPORT ON REACTOR OPERATIONS, is for the period of January 1,2001 to December 31, 2001 as required by Technical Specification 6.6.1 Annual OperatingReport.

Sincerely, Christopher W. Becker Reactor Laboratory Manager xc: U.S. Nuclear Regulatory Commission ATTN: Theodore Michaels, Project Manager Mail Stop 012-D3, REXB Washington, DC 20555-0001 Thomas F. Dragoun, Inspector U.S. Nuclear Regulatory Commission Region I 775 Allendale Road King of Prussia, PA 19406-1415 American Nuclear Insurers Tower Center, Suite 300S 29 South Main Street West Hartford, CT 06107-2430 Enclosure (1)

Phone: (734) 764-6220 Fax: (734) 936-1571 www.umich.edu/-mmpp/

REPORT OF REACTOR OPERATIONS January 1, 2001 - December 31, 2001 FORD NUCLEAR REACTOR MICHIGAN MEMORIAL - PHOENIX PROJECT THE UNIVERSITY OF MICHIGAN ANN ARBOR Prepared For The U.S. Nuclear Regulatory Commission

FORD NUCLEAR REACTOR Docket No. 50-2 License No. R-28 REPORT OF REACTOR OPERATIONS This report reviews the operation of the University of Michigan's Ford Nuclear Reactor for the period January 1 to December 31, 2001. The report is to meet the requirement of Technical Specifications for the Ford Nuclear Reactor. The format for the sections that follow conforms to Section 6.6.1 of Technical Specifications.

The Ford Nuclear Reactor is operated by the Michigan Memorial Phoenix Project of the University of Michigan. The Project, established in 1948 as a memorial to students and alumni of the University who served and the 588 who died in World War II, encourages and supports research on the peaceful uses of nuclear energy and its social implications. In addition to the Ford Nuclear Reactor (FNR), the Project operates the Phoenix Memorial Laboratory (PML). These laboratories, together with a faculty research grant program, are the means by which the Project carries out its purpose.

The operation of the Ford Nuclear Reactor provides major assistance to a wide variety of research and educational programs. The reactor provides neutron irradiation services and neutron beamport experimental facilities for use by faculty, students, and researchers from the University of Michigan, other universities, and industrial research organizations. Reactor staff members teach classes related to nuclear reactors and the Ford Nuclear Reactor in particular and assist in reactor-related laboratories.

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_ -w Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 OPERATIONS

SUMMARY

In January, 1966, a continuous operating cycle was adopted for the Ford Nuclear Reactor at its licensed power level of two megawatts. The cycle consisted of approximately 25 days at full power followed by three days of shutdown maintenance. In June, 1975, a reduced operating cycle consisting of ten days at full power followed by four days of shutdown maintenance was adopted. A typical week consisted of 120 full-power operating hours. In July, 1983, the reactor operating schedule was changed to Monday through Friday at licensed power and weekend shutdowns. Periodic maintenance weeks were scheduled during the year. In January, 1985, a cycle consisting of four days or 96 full-power operating hours per week at licensed power followed by three days of shutdown maintenance was established in order to eliminate the periodic shutdown maintenance weeks needed in the previous cycle. Beginning July 1, 1987, the reactor operating cycle returned to ten day operation at full power followed by four days of shutdown maintenance. This calendar year began with cycle 454 and ended with cycle 466. A typically cycle covers four weeks; two of the ten day - four day sequences.

The reactor operates at a maximum power level of two megawatts which produces a peak thermal flux of approximately 2x1 013 n/cm 2/sec. An equilibrium core configuration consists of approximately 41 standard and 4 control, 19.75% enriched, plate-type fuel elements. Standard elements contain 167 gmn of U235 in 18 aluminum clad fuel plates. Control elements, which have control rod guide channels, have nine plates and contain 83 gm of U235. Overall active fuel element dimensions are approximately 3"x 3"x 24".

Fuel elements are retired after burnup levels of approximately 35-40% are reached. Fuel burnup rate is approximately 2.46 gm U235/day at two megawatts.

1.1 Facility Design Changes Modification Request #144, Installation of a 25 h.p. Pump-Motor Set into the Primary Coolant System. The installed 20 h.p. primary coolant pump failed in earl February 2001. A replacement 25 h.p. pump-motor set was installed Testing showed that is was capable of providing over 1100 gallons per minute of primary coolant flow.

While performing the Safety Evaluation, a review of the Safety Analysis Report (SAR) found the the description of the primary coolant system states in part that: "The flow rate is between 900 and 1000 gallons per minute." The SAR also gives values of core excess reactivity and power defect, among other core parameters. Increased flow are expected to reduce power below the SAR stated value. This affects the determination of core excess reactivity.

The safety evaluation concluded that, until the power defect-core excess reactivity issue is resolved, it was best to throttle primary flow at about 1050 nominal gallons per minute under a Temporary Operating Instruction.

1.2 Equipment and Fuel Performance Characteristics The reactor was refueled on April 13-16, 2001. Three new regular fuel assemblies and one new control fuel assembly were installed. Three regular fuel assemblies and one control fuel assembly were retired. The core excess reactivity, after refueling and performing rod calibrations, was 3.89% Delta K/K.

Four new regular fuel assemblies and one new regular fuel assembly were received on April 19, 2001 (ZBF-ZMZ-19) 2

Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 The reactor was refueled on September 4-5, 2001. Three new regular fuel assemblies and one new control fuel assembly were installed. Three regular fuel assemblies and one control fuel assembly were retired. The core excess reactivity, after refueling and performing rod calibrations, was 3.89% Delta K/K.

Five new fuel assemblies were received on October 5, 2001. (ZBF-ZMZ-20)

Two new regular fuel assemblies and two new regular fuel assemblies were received on December 13, 2001. (ZBF-ZMZ-21)

No irradiated fuel shipments were made in 2001.

1.3 Safety-Related Procedure Changes Safety-related procedures are those associated with operation, calibration, and maintenance of the primary coolant, the reactor safety system, the shim-safety rods, all scram functions, the high temperature auto rundown function, and the pool level rundown.

Calibration and Maintenance Procedures

1. CP- 101 ReactorMaintenance Schedule, Rev 21 dated 08 Jan 01 Identify the frequency requirements for routine maintenance items, and to set guidelines for scheduling routine and non-routine maintenance for shutdown periods.

No substantial changes were made.

The notable changes were 1) addition of SNM Inventory 2) addition of SNM-179 inventory 3) addition of calibrations for Keithley 261 I, Fluke 83 DVM, Fluke 83 III DVM, Ludlum 500 Pulser and Keithley 485 Picoammeter 4) addition of Cleaning Secondary Chemical Piping 5) LCR Hose-Cable replacement (even years) 6) addition of Map Pump Vane Replacement and 7) editing changes.

2. CP-218 Magnet Power Supply Calibration,Rev 4 dated 04 Jun 01.

Provides a safe and consistent method for calibrating the scram system magnet power supply.

No substantial changes were made.

The notable changes were 1) relaxed limits on over current trip 2) spaces for Millimeter Model and Calibration dates and 3) editing changes for ease of understanding the procedure.

Operating Procedures

1. OP-102 ReactorShutdown, Rev 18 dated 13 Jan 01.

Provide consistent manipulation of controls and sequence of operations for routine reactor shutdown at the conclusion of an operating cycle or for a holiday.

No substantial changes were made.

The notable change was adding: "perform security checks per MP-203 Security Area Surveillance".

2. OP-201 Building Checklist, Rev 42 dated 16 May 01.

Provide for specific requirements for items on the Building Checklist.

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Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 No substantial changes were made.

The notable change was adding data taking for an experiment.

3. OP-102 ReactorShutdown, Rev 19 dated 2 Jun 01.

Provide consistent manipulation of controls and sequence of operations for routine reactor shutdown at the conclusion of an operating cycle or for a holiday.

No substantial changes were made.

The notable change was reordering of steps.

4. OP-301 Building Power Failure,Rev 7 dated 2 Jun 01.

Lists the checks that must be made if a power failure is judged to have occurred.

No substantial changes were made.

The notable change was to add channel checks of Level Safety Channels A and B, Period Safety Channel C and Power Flow Coincidence Scrams to ensure Tech Spec 4.2.1 is satisfied.

1.4 Maintenance, Surveillance Tests, and Inspection Results as Required by Technical Specifications.

Maintenance, surveillance tests, and inspections required by Technical Specifications were completed at the prescribed intervals. Procedures, data sheets, and a maintenance schedule/record provide documentation.

1.5 Summary of Changes, Tests, and Experiments for Which NRC Authorization was Required.

None 1.6 Operating Staff Changes The following reactor operations staff changes occurred:

New Hire Position Date Shane Rye Reactor Operator March 12, 2001 John Dasch Reactor Operatory (50%) September 10, 2001 Terminated Position Date Benjamin Huck Engineering Tech III January 3, 2001 Safety Review Committee Changes The following Safety Review Committee Changes occurred:

New Appointees Position Date John Lee Chairman February 2, 2001 John King Faculty Member (ex-chairman) February 2, 2001 William R. Martin Faculty Member July 5, 2001 Removed Appointees Position Date James E. Martin Faculty Member February 2, 2001 4

Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001

2. POWER GENERATION

SUMMARY

The following table summarizes reactor annual power generation.

Operating Full Power Megawatt Percent Cycle Inclusive Dates Hours Operating Hours Hours Availability 454 01/07/01 - 02/0/01 492.9 481.5 967.2 71.7 455 02/04/01 - 03/03/01 449.2 423.3 850.4 63 456 03/04/01 - 03/31/01 257.3 242.6 487.1 36.1 457 04/01/01 - 04/28/01 493.2 441.7 912.6 65.7 458 04/29/01 - 05/26/01 499.1 480.7 964.2 71.5 459 05/27/01 - 06/23/01 473.2 427.4 859.9 63.6 460 06/24/01 - 07/21/01 467.3 456.8 898.1 68 461 07/22/01 - 08/18/01 496.2 484.6 974.1 72.1 462 08/19/01 - 09/15/01 421.6 331.3 670.9 49.3 463 09/16/01 - 10/13/01 491.5 478.3 960.9 71.2 464 10/14/01 - 11/10/01 474.2 458.1 920.8 68.2 465 11/11/01 - 12/08/01 421.6 405.9 816.4 60.4 466 12/09/01 - 01/05/01 247.1 242.3 486.3 36.1 Totals: 1 5684.4 1 5354.5 I 10768.9 1 65.1

3. UNSCHEDULED REACTOR SHUTDOWN

SUMMARY

The following table summarizes unscheduled reactor shutdowns.

3.1 Shutdown Type Definitions Single Rod Drop and Multiple Rod Drop (NAR) - An unscheduled shutdown caused by the release of one or more of the reactor shim-safety rods from its electromagnet, and for which at the time of the rod release, no specific component malfunction and no apparent reason (NAR) can be identified as having caused the release.

Operator Action - A condition exists (usually some minor difficulty with an experiment) for which the operator on duty judges that shutdown of the reactor is required until the difficulty is corrected.

Operator Error - The operator on duty makes a judgment or manipulative error which results in shutdown of the reactor.

Process Equipment Failure - Shutdown caused by a malfunction in the process equipment interlocks of the reactor control system.

Reactor Controls - Shutdown initiated by malfunction of the control and detection equipment directly associated with the reactor safety and control system.

Electrical Power Failure - Shutdown caused by interruption in the reactor facility electric power supply.

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Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 3.2 Summary of Unscheduled Shutdowns 12 Feb 01 The reactor was shut down due to a loss of external electrical power. The reactor was restarted without difficulty after electrical power was restored to the building. Electrical Power Failure.

04 April 01 The reactor was shut down due to a building alarm that was inadvertently actuated while an operator was checking the stack alarm relay. The reactor was restarted without difficulty after the relay was reset to normal.

Operator Error.

26 April 01 The reactor was shut down due to a loss of external electrical power. The reactor was restarted without difficulty after electrical power was restored to the building. Electrical Power Failure.

11 Sept 01 The reactor was shut down in response to terrorist activity in the United States. Additional security precautions were implemented immediately. The reactor was restarted without difficulty. Additional security precautions continue to be in place. No actual security violations, breaches or threats have been experienced. Operator Action.

19 Sept 01 The reactor was shut down due to a loss of external electrical power. The reactor was restarted without difficulty after electrical power was restored to the building. Electrical Power Failure.

04 Oct 01 The reactor was shut down due to operator interpretation of technical specifications after the radiation recorder chart paper motor stopped functioning. Further inspection revealed that the connector to the chart drive motor was loose, probably jostled when the chart paper was replaced. The connector was tightened and the chart drive returned to normal. The reactor was then restarted without difficulty. Operator Action.

3.3 Characterization of Unscheduled Shutdowns Single Rod Drop (NAR) 0 Multiple Rod Drop (NAR) 0 Operator Action 2 Operator Error 1 Process Equipment Failure 0 Reactor Controls 0 Electric Power Failure 3 Total Unscheduled Shutdowns 6

4. CORRECTIVE MAINTENANCE ON SAFETY RELATED SYSTEMS AND COMPONENTS 24 Jan 01 Capstan drive for the filter paper on #2 Stack Map was found to be inoperable. The capstan was sanded where galling was occurring. The shear pin was also replaced.

02 Feb 01 The shear pin for #2 Stack Map failed. The shear pin was replaced.

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Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 05 Mar 01 While performing a calibration on magnet power supply S/N T0792673 for routine maintenance, Channel B high current trip circuit began oscillating.

Replacement of the diode in the trip circuit was performed.

26 Mar 01 Pressure boundary on primary heat exchanger was broken for cleaning of the heat exchanger. The primary end bell was remounted then torqued to 20 ft lbs, then 30 ft-lbs and finally to 45 ft-lbs.

02 Apr 01 Failure of magnet current on C rod when magnet cable was moved, during a fuel move. Repair was accomplished by replacing C magnet and cable with a spare.

30 Apr 01 Linear Level compensating voltage display was reading zero. A loose edge connection was found and replaced on the indicating circuit.

12 May 01 #2 Log Count Rate fission chamber was reading erratic. A new detector and connection were installed. The signal cable and hose were trimmed back due to degradation. In addition a new o-ring was installed.

26 Jun 01 Cooling water for the reactor air compressor would not shut off when the compressor stopped. The automatic shutoff solenoid valve was replaced.

27 Jun 01 The temporary rate meter for the Beam Hole Floor Map was replaced with a permanent rate meter.

17 Sep 01 Failure of #2 Primary Flow digital display. Proper operation of the rest of #2 Primary Flow instrument was verified by DC and AC voltage readings. The digital display was replaced and proper indication was noted with the primary pump on.

15 Oct 01 Random noise observed on all channels of the Temperature Recorder.

Analog Gain and Analog/Digital conversion card was replaced with a spare card. The spare card would not function properly after recorder calibration and setup. The original card was installed and re-calibrated.

16 Oct 01 The Basement door alarm circuit, red light socket on the control console shorted to ground. This caused current overload to bum up theannunciator flasher. The flasher (discrete components) was replaced with a new flasher (modular design) with equivalent function. The Basement door alarm light socket was replaced. The other light sockets on the control console were also checked.

29 Oct 01 Random noise continued to be observed on all channels of the Temperature Recorder. The 15 volt power supply on the Analog Gain and Analog/Digital conversion card was refurbished with replacement parts: Q, Q2, VRl, VR2, VR3, VR4, VR7, VR8, VR9, C25, C26.

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__-w Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 29 Oct 01 Due to a NRC concern of the test signal current being >2.45 MW indicated, The scram setpoint was lowered to 2.30-2.40 Mw range and the test current signal adjusted to 2.40-2.45 Mw range on Safety Channel "A".

12 Nov 01 Due to a NRC concern of the test signal current being >2.45 MW indicated, the scram setpoint was lowered to 2.30-2.40 Mw range and the test current signal adjusted to 2.40-2.45 Mw range on Safety Channel "B".

5. CHANGES, TESTS, AND EXPERIMENTS CARRIED OUT WITHOUT PRIOR NRC APPROVAL PURSUANT TO 10CFR50.59(a)

Modification Request #144, Installation of a 25 h.p. Pump-Motor Set into the Primary Coolant System. The installed 20 h.p. primary coolant pump failed in earl February 2001. A replacement 25 h.p. pump-motor set was installed Testing showed that is was capable of providing over 1100 gallons per minute of primary coolant flow.

While performing the Safety Evaluation, a review of the Safety Analysis Report (SAR) found the the description of the primary coolant system states in part that: "The flow rate is between 900 and 1000 gallons per minute." The SAR also gives values of core excess reactivity and power defect, among other core parameters. Increased flow are expected to reduce power below the SAR stated value. This affects the determination of core excess reactivity.

The safety evaluation concluded that, until the power defect-core excess reactivity issue is resolved, it was best to throttle primary flow at about 1050 nominal gallons per minute under a Temporary Operating Instruction.

6. RADIOACTIVE EFFLUENT RELEASE Quantities and types of radioactive effluent releases, environmental monitoring locations and data, and occupational personnel radiation exposures are provided in this section.

6.1 Gaseous Effluents - 4'Ar Releases Gaseous effluent concentrations are averaged over a period of one year.

Quantity [Unit

a. Total gross radioactivity. 4.31x10 7 gCi
b. Average concentration released. 1.27x 10-7 ýtCi/ml
c. Average release rate. 1.37 ýtCi/sec
d. Maximum instantaneous concentration during Not jtCi/ml special operations, tests, and experiments. Applicable
e. Percent of 4'Ar ERL (Effluent Release Limits) 1274 Percent (1.0x 10 8 ý,Ci/ml) without dilution factor.
f. Percent of 4'Ar ERL with 400 dilution factor. 3.18 Percent 6.2 Radiohalogen Releases
a. Total iodine radioactivity by nuclide based upon a representative isotopic analysis. (Required if iodine is identified in primary coolant samples or if 8

Report of Reactor Operations Ford Nuclear Reactor January 1 -December 31, 2001 fueled experiments are conducted at the facility). Based on this criteria, this section of the report is not required. The analysis is based on primary coolant activity following one week of decay.

Iodine-131 was not identified in the one week count of the primary coolant samples.Xenon-133 was not identified in the one week count of the primary coolant samples.

The pool water analyses show no indication of leaking fuel.

b. "1'Iodine releases related to steady state reactor operation (Sample C-3, main reactor exhaust stack).

Quantity Unit

1. Total 1311 release. 26 pLCi
2. Average concentration released. 1.19xI0-113 pCi/ml
3. Percent of 131IERL (2.0x10-O' jCi/ml) 0.06 Percent without dilution factor.
4. Percent of 1311 ERL with 400 dilution factor. 0.00015 Percent
c. Radiohalogen releases related to combined steady state reactor operation and radiation laboratory activities (Sample C-2; combined secondary reactor exhaust and partial radiation laboratory exhaust.
1. Total C-2 stack radiohalogen releases.

Br-80m 2495 pLCi Br-82 2542 [LCi 1-131 501 pCi Hg-203 8 gCi

2. Average concentration released.

[Quantity Unit Br-80m 2.07x10-" pCi/ml Br-82 2.10xlO-1" Ci/ml 1-131 4.15x10 -2 pCi/ml Hg-203 6.33x10-14 jtCi/ml

3. Percent of ERL without the dilution factor.

Br-80m 0.10 Percent Br-82 0.42 Percent 1-131 2.07 Percent Hg-203 0.01 Percent 9

Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001

4. Percent of ERL with factor of 400 dilution factor.

Br-80m 0.00025 Percent Br-82 0.00105 Percent 1-131 0.00518 Percent Hg-203 0.00002 Percent

d. Total Facility Release of Radiohalogens.
1. Total facility radiohalogen releases.

Br-80m 2,168 ptCi Br-82 3,885 ýtCi 1-125 727 ýtCi 1-131 2,920 gCi Hg-203 48 gCi I1. Average concentration released.

Br-80m 3.42x10- 2 gCi/ml Br-82 6.13x10 1 2 gCi/ml 1-125 1.15x10 1 2 ptCi/ml 1-131 4.61x1 0-12 ptCi/ml Hg-203 7.59x101 3 vtCi/ml

3. Percent of ERL without the dilution factor.

Quantity Unit Br-80m 0.07 Percent Br-82 0.123 Percent 1-125 0.302 Percent 1-131 2.305 Percent Hg-203 0.008 Percent TOTAL 2.755 Percent

4. Percent of ERL with factor of 400 dilution factor.

Br-80m 0.00004 Percent Br-82 0.00031 Percent 1-125 0.00096 Percent 1-131 0.00576 Percent Hg-203 0.00002 Percent TOTAL 0.00709 Percent 6.3 Particulate Releases Particulate activity for nuclides with half lives greater than eight days.

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Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001

a. Total gross radioactivity. 103 pLCi
b. Average concentration. 1.64x10-13 gCi/ml
c. Percent of ERL (1.0x 10-12 Ci/ml) without 16.41 Percent dilution factor.
d. Percent of ERL with 400 dilution factor. 0.041 Percent Gross alpha activity is required to be measured if the operational or experimental program could result in the release of alpha emitters.
e. Gross alpha radioactivity. I Not Required I 6.4 Liquid Effluents No radioactive liquid effluents were released from the facility in 2000.

6.5 Accident Evaluation Monitoring The accident evaluation monitoring program for the Ford Nuclear Reactor facility consists of direct radiation monitors (TLD), air sampling stations located around the facility, and selected water and sewer sampling stations.

a. TLD Monitors TLDs located at stations to the north (lawn adjacent to the reactor building),

northeast (fluids), east (Beal Avenue), south (Glazier Way), and west (School of Music) of the reactor facility are collected and sent to a commercial dosimetry company for analysis. The final dosimetry reports for environmental TLDS during calendar year 2001 have not been received from the processor in time for this report. A revision to this report will be submitted shortly after the data is available Annual Quarterly Total Mean Location Direction (mrem) (mrem)

FNR Lawn North Fluids Northeast Beal East Glazier Way South School of Music West Environmental Control (UM Botanical Gardens)

b. Dust Samples Five air grab samples are collected weekly from continuously operating monitors located to the north (Northwood Apartments), east (Industrial and Operations Engineering), northeast (Laundry), south (Institute of Science and Technology),

and west (Media Union) of the reactor facility. Each filter sample is counted for net beta activity. There are 51 samples included in this report for each location except Laundry. The Laundry monitoring station has been discontinued. It was shut down on October 29, 2001 and only has 42 samples for 2001. Gas 11

Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 proportional counter backgrounds have been subtracted from the concentrations reported. Environmental background (University of Michigan Botanical Gardens) has not been subtracted from the mean radioactivity concentrations shown below.

Mean Station Description Concentration Unit Northwood (N) 1.86x 10- 14 jICi/ml Industrial and Operations Engineering (E) 2.28x 10-14 jICi/ml Media Union (W) 2.15xl 0- 14 gCi/ml Institute of Science and Technology (S) 2.1 1x10-1 4 PCi/ml Laundry (NE) 1.92x 10-14 gtCi/ml Environmental Control (Background) 2.34x1 0-14 4Ci/ml The result of air sampling expressed in percentages of the Effluent Release Limits are shown below.

Percent Station Description ERL Unit Northwood (N) 1.86 Percent Industrial and Operations Engineering (E) 2.28 Percent Media Union (W) 2.15 Percent Institute of Science and Technology (S) 2.11 Percent Laundry (NE) 1.95 Percent Environmental Control (Background) 2.34 Percent

c. Water Samples No Radioactive liquid effluents were released from the facility in 2000.
d. Sewage Samples No Radioactive liquid effluents were released from the facility in 2000.
e. Maximum Cumulative Radiation Dose The maximum cumulative radiation dose which could have been received by an individual continuously present in an unrestricted area during reactor operations from direct radiation exposure, exposure to gaseous effluents, and exposure to liquid effluents:
1. Direct radiation exposure to such an individual is negligible since a survey of occupied areas around the reactor building shows insignificant radiation dose rates above background from the reactor.
2. Airborne Effluents The airborne effluents from the reactor and the contiguous laboratory facility are as follows:

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Report of Reactor Operations Ford Nuclear Reactor January 1 - December 31, 2001 Total %ERL  % ERL Isotogpe Release Concentration Undiluted Diluted (GtCi) (ýtCi/ml)

Ar-41 43100000 1.27x10-0 7 1,273.64 3.18410 Br-80m 2168 342x 10-12 0.02 0.00004 Br-82 3885 6.13x 10-12 0.12 0.00031 Hg-203 48 7359x10- 14 0.01 0.00002 1-125 727 1.15x 10-12 0.38 0.00096 1-131 2920 4.61x10"12 2.31 0.00576 Gross Particulate 103 1.64x10 1 3 16.41 0.04104 TOTAL 1,292.89 3.23223 Equivalent Radiation Dose (mrem) 1.62 The total airborne effluent releases are well within the allowed release concentrations when the conservative dilution factor of 400 is applied.

The equivalent total dose from all airborne effluent releases is well below the 10 mrem per year constraint described in NRC Information Notice 97-04, "Implementation of a New Constraint on Radioactive Air Effluents."

3. Liquid Effluents No radioactive liquid effluents were released from the reactor and the contiguous laboratory facility in 2001.

f, If levels of radioactive materials in environmental media, as determined by an environmental monitoring program, indicate the likelihood of public intake in excess of 1% of those that could result from continuous exposure to the concentration values listed in Appendix B, Table 2, 10CFR20, estimate the likely resultant exposure to individuals and to population groups and the assumptions upon which those estimates are based. Exposure of the general public to 1 ERL would result in a whole body dose of 50 mirem. The maximum public dose based on airborne and liquid effluent releases of 3.23% ERL is 1.62 mrem. This dose is based on a member of the public being continuously present at the point of minimum dilution near the reactor building.

6.6 Occupational Personnel Radiation Exposures Individuals for whom the annual whole body radiation exposure exceeded 500 mrem (50 mrem for person under 18 years of age) during the reporting period:

The final dosimetry reports for calendar year 2001 have not been received from the processor in time for this report. A revision to this report will be submitted shortly after the data is available.

This includes facility personnel including faculty, students, or experimenters.

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