LR-N02-0092, February 2002 Monthly Operating Report for Salem, Unit 1

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February 2002 Monthly Operating Report for Salem, Unit 1
ML020850726
Person / Time
Site: Salem PSEG icon.png
Issue date: 03/14/2002
From: Garchow D
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N02-0092
Download: ML020850726 (4)


Text

PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 MAR 1 4 2002 LR-N02-0092 o PSEG Niuclear LLC U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

MONTHLY OPERATING REPORT SALEM GENERATING STATION UNIT 1 DOCKET NO. 50-272 In compliance with Section 6.9, Reporting Requirements for the Salem Unit 1 Technical Specifications, the operating statistics for February 2002 are being forwarded.

Sincerely, D. F. Garclpow Vice President - Operations RAR Attachments C Distribution 1'

95-2168 REV. 7/99

INDEX NUMBER SECTION OF PAGES Operating Data Report...............................................................................

1 Monthly Operating Summary......................................................................

1

DOCKET NO.:

UNIT:

DATE:

COMPLETED BY:

TELEPHONE:

50-272 Salem 1 03/08/02 F. Todd (856) 339-1316 Reporting Period February 2002 OPERATING DATA REPORT Design Electrical Rating (MWe-Net)

Maximum Dependable Capacity (MWe-Net)

No. of hours reactor was critical No. of hours generator was on line (service hours)

Unit reserve shutdown hours Net Electrical Energy (MWH) 1130 1096 Month Year-to-oate t;umulatlve 672 1416 135644 672 1416 131111 0

0 0

717096 1556237 132839635 UNIT SHUTDOWNS (1) Reason (2) Method A - Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training/License Examination F - Administrative G - Operational Error (Explain)

H - Other 1 - Manual 2 - Manual Trip/Scram 3 - Automatic Trip/Scram 4 - Continuation 5 - Other (Explain)

NO.

DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTION/

F=FORCED (HOURS)

(1)

SHUTTING COMMENT S=SCHEDULED DOWN THE REACTOR (2)

DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 03/08/02 COMPLETED BY: R. Ritzman TELEPHONE: (856) 339-1445 Summary Of Monthly Operating Experience Salem 1 began the month at 100% power.

" On February 15, power was reduced to approximately 37% power to adjust the steam generator low level setpoint. The unit returned to 100% power on February 18.

On February 26, power was reduced to approximately 72%. This power reduction was due to both circulators in the same water box being out of service. One of the circulators was out of service for maintenance; the other one was taken out of service due to unexpected environmental conditions.

The unit returned to 100% power on February 27.

On February 28, power was reduced to approximately 75%. This power reduction was due to both circulators in the same water box being out of service. One of the circulators was out of service for maintenance; the other one was taken out of service due to unexpected environmental conditions.

"* At the end of the month, Salem 1 completed 135 days of continuous operation.