L-96-154, Forwards Response to Violations Noted in Insp Repts 50-250/96-04 & 50-251/96-04.Corrective Actions:Two Operations Personnel Removed from Shift for Remedial Training

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Forwards Response to Violations Noted in Insp Repts 50-250/96-04 & 50-251/96-04.Corrective Actions:Two Operations Personnel Removed from Shift for Remedial Training
ML17353A761
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 07/01/1996
From: Hovey R
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
RTR-NUREG-1600, RTR-REGGD-01.033, RTR-REGGD-1.033 L-96-154, NUDOCS 9607080262
Download: ML17353A761 (6)


Text

CATEGORY 1 REGULATO Y INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9607080262 DOC.DATE: 96/07/01 NOTARIZED: NO DOCKET FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4, Florida Power and Iight C 05000251 AUTH.NAME AUTHOR AFFILIATION HOVEY,R.J.

Florida Power a Light Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to violations noted in insp repts 50-250/96-04 6

50-251/96-04.Corrective actions:issued night order re importance of procedural compliance a

removed two operations personnel from shift for remedial training.

DISTRIBUTION CODE: IEOID COPIES RECEIVED:LTR I

ENCL L SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:

INTERNAL:

aZZERNAL:

RECIPIENT ID CODE/NAME PD2-3 PD AEOD/SPD/RAB-DEDRO NRR/DISP/PIPB NRR/DRPM/PECB NUDOCS-ABSTRACT OGC/HDS3 LITCO BRYCEPJ H

NRC PDR COPIES LTTR ENCL 1

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1 1

1 1

1 RECIPIENT ID CODE/NAME CROTEAU,R

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NRR/DRCH/HHFB NRR/DRPM/PERB OE DIR RGN2 FILE 01 NOAC COPIES LTTR ENCL 1

1 1

1 1

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NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE!

CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083)

TO ELIMINATE YOUR NAME FROM t

DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED(

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 17 ENCL 17

JUL 11996 L-96-154 10 CFR 2.201 U. S. Nuclear Regulatory Commission Attn:

Document Control Desk Washington, D. C.

20555 Gentlemen:

Re:

Turkev Point Units 3

6 4

Docket Nos.

50-250/251 Re 1

to Notice of Violation Florida Power

& Light Company has reviewed the subject inspection report

and, pursuant to 1U CFR 2.201, the required response is attached.

If there are any questions, please contact us.

Very truly yours, R. J.

Hov y Vice President Turkey Point Plant JEK Attachment cc:

Stewart D. Ebneter, Regional Administrator, Region II, USNRC T. P.

Johnson, Senior Resident Inspector,
USNRC, Turkey Point Nuclear Plant 9607080262

'rr60701 t

PDR ADQCK 05000250 an FPL Group company

. Attachment to L-96-154 Page 1

RE:

Turkev Point Units 3 and 4

Docket'os.

50-250 and 50-251 NRC Inspection Report 96-04 ZIHDIHG "During an NRC inspection conducted on March 24 through May 4,

1996, a violation of NRC requirements was identified.

In accordance with "General Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the violation is listed below:

Technical Specification 6.8.1 requires that written procedures be established, implemented, and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.

Item 3.n of Regulatory Guide 1.33, Revision 2, February

1978, Appendix A, recommends the use of procedures for activities involving the Chemical and Volume Control System (CVCS).

Procedure O-OP-046, Chemical and Volume Control System Boron Concentration Control, section 5.3, Dilution, reguires the operator to select either dilute or alternate di3.ute methods for sending pure water to the blender Contrary to the above, on March 26

1996, the Unit 3 RCO failed to adequatelv implement section 5.5 of procedure O-OP-046, as neither dilute nor alternate dilute method was selected for sendincr pure water to the blender.
Instead, the RCO opened the respecCive blender inlet and outlet valves.

This is a Severity Level IV violation (Supplement I)."

2.

3.

Florida Power

& Light Company (FPL) concurs with the finding.

Reason for the violation:

This evolution is normally performed from memory, as is allowed bv administrative procedures controlling frequent evolutions.

The operator in this case attempted to perform the boration and a subseauent manual flush operation from memory.

However, the manual flush operation was no longer part of the procedure.

0-OP-046, CVCS Boron Concentration Control had been changed to delete the blender flush in 1991 as a result of the lowering of boric acid concentration requirements in the chemical volume and control system (CVCS).

But the change to the blender operation was not effectively communicated at the time of the procedure change and Training summary sheets did not adequately indicate deletion of the flush requirement.

Corrective steps which have been taken and the results achieved:

Immediate actions are as follows:

A night order was issued that stressed the importance of procedural compliance.

The two operations personnel were removed from shift for remedial training.

Attachment to L-96-154 Page 2

4

~

5.

Additional senior reactor operators and key line managers were assigned as management on shift, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> a day for 3 weeks, to capture needs for procedure enhancements and other activities requiring a procedure.

The importance of procedural compliance has been stressed by completion of the first two immediate actions.

Condition Report 96-722 was issued and completed requiring the identification of the cause of this event and the implementa-tion of corrective actions.

Investigation of the extent of this condition has been com-leted.

No evidence of other operators performing a manual lush has been found.

Other evolutions performed from memory were investigated.

Minor potential enhancements in some memorized evolution procedures were identified.

Corrective actions which will be taken to prevent further violations:

All licensed operators normally assigned responsibility as unit reactor control operator have been requalified on the required CVCS operations.

A shift supervisor meeting was held immediately after the event to discuss the event.

Management expectations for supervisory oversight and procedural adherence during routine evolutions were reinforced.

FPL is evaluating a plan to have operators periodically perform routine evolutions (which may be performed from memory), with the procedure in hand, to ensure operators remain current with the requirements.

Those procedures identified as potential enhancement candi-

dates, in Item 3 above, will be further reviewed and revised, as appropriate, by December 15, 1996.

The date when full compliance was or will be achieved:

Full compliance was completed on June 4,

1996, with the re-training of operators on the CVCS evolution.